ML20215E263

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Notice of Violation from Insp on 860805 & 20
ML20215E263
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 10/06/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20215E248 List:
References
50-482-86-18, NUDOCS 8610150177
Download: ML20215E263 (3)


Text

4 APPENDIX A NOTICE OF VIOLATION Kansas Gas and Electric Corr.pany Docket: 50-482/86-18 Wolf Creek Generating Station License: NPF-42 During an NRC inspection conducted on August 5 and 20, 1986, two violations of NRC requirements were identified. The violations involved a failure to comply with licensee's temporary modification procedure and a failure to lock a valve as required. In accordance with the " General Statement of Policy and Procedure for hRC Enforcement Actions," 10 CFR Part 2, Appendix C (1986), the violations are listed below:

A. Failure To Comply With Licensee's Temporary Modification Procedure Technical Specification (TS) 6.8.1 requires that, " Written procedures shall be established, implemented, and maintained covering . . . a. The applicable procedures recommended in f.ppendix A of Regulatory Guide (RG) 1.33, Revision 2, February 1978."

Appendix A of RG 1.33, Revision 2, February 1978, states that "The following . . . safety-related activities . . . should be covered by written procedures . . 1.c. Equipment control (e.g. , locking and tagging) and "1.d Procedure Adherence and Temporary Change Method."

Administrative Procedure (ADM)02-101, Revision 15, " Temporary Modifications," has been established and implemented in accordance with the above TS to control temporary modifications to ensure an accurate control of station equipment is maintained and to ensure the return of a system to its permanent configuration.

5-ection 6.1.1.1 of ADM 02-101, Revision 15, May 27, 1986, states that, "The type of temporary modification shall be indicated in the activity to be performed block. Information to be recorded in Section D and on each temporary modification tag should be as follows:

  • Lifted lead-cabinet name/ location, terminal block number and terminal number, wire number, and tag number."

Section 6.1.6.1 of ADM 02-101, Revision 15, May 27, 1986, states that, ". . . After the tag (s) are placed, the installer will sign the tag (s), initial the appropriate space on the temporary modification order, and sign Section B, installed by."

Section 6.1.6.2 of ADM 02-101, Revision 15, May 27, 1986, states that, ". . . The person performing the independent verification will sign'the tag (s), initial the appropriate space on the temporary modification order, and sign Section B, independent verification by."

ADM 01-001, Revision 12, " Introduction To Wolf Creek Generating Procedures," has been established and implemented in accordance with 8610150177 861006 -

PDR ADOCK 05000482 G PDR

the above TS to establish the administrative controls required of various organizations to carry out their assigned responsibilities.

Section 4.2.4 of ADM 01-001, Revision 12, April 1,1986, states that, "Those participating in any activity shall be made aware of, and use, proper and current instructions, procedures, drawings, and engineering requirements for performing the activity as applicable."

Contrary to the above, on August 5, 1986, the NRC inspector reviewed Temporary Modification Orders 86-72KC and 86-81KC. The NRC inspector observed that ADM 02-101 had not been followed in that the required information for a lifted lead had not been recorded in Section D of Temporary Modification Order 86-81KC, and that Temporary Modification Tag 86-72-KC-01 had been hung but the appropriate space on the temporary modification order was missing initials for tag installation and verification. -The NRC inspector also observed that ADM 01-001 had not been followed in that Temporary Modification Order 86-72KC, prepared on July 10, 1986, used out-of-date ADM 02-101, Revision 14, versus the then current Procedure ADM 02-101, Revision 15, May 27, 1986.

This is a Severity Level IV violation (Supplement I.D) (482/8618-01).

B. Failure To Lock Valve In Accordance With Procedure TS 6.8.1 requires that, " Written procedures shall be established, and maintained covering . . .-a. The applicable procedures recommended in Appendix A of RG 1.33, Revision 2, February 1978."

Appendix A of RG 1.33, Revision 2,' February 1978,- states that, "The following . . . safety-related activities . . . should be covered by written procedures . . 1.c. equipment control (e.g. , locking and tagging)."

Checklist CKL AL-120, Revision 8, " Auxiliary Feedwater Normal Lineup," has been established and implemented in accordance with the above TS.

Checklist A of CKL AL-120 requires, in part, that the handwheels to Valves AL HV-006, AL HV-008, AL HV-010, and AL HV-012 be lockwired in the neutral positions.

Contrary to the above, on August 20, 1986, the NRC inspectors observed that 3 out of the 4 turbine driven auxiliary feedwater pump (TDAFWP) discharge valve handwheels were in the required neutral position but were not properly lockwired. Valve ALHV-006 had its lockwire broken and twisted back together, ALHV-008 was not lockwired, and ALHV-010 was lockwired so loosely that the valve could.be operated.

This is a Severity Level IV violation (Supplement I.D) (482/8618-02).

Pursuant to the provisions of 10 CFR 2.201, Kansas Gas and Electric Company is hereby required to submit to this Office, within 30 days of the date of the letter transmitting this Notice, a written statement or explanation in reply,

i including for each violation: (1).the reason.for the violations if admitted,

,(2) the corrective steps-which have been taken and the results achieved; (3) the corrective steps which will'be taken to avoid furf.her violations; and (4) the date when full compliance will be achieved. Wher>3 good cause is-shown,

, consideration will be given to extending the response tire.

l 4 . DatedatArlingtan,TexashAh this (n* day of ( J 1986 T

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