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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20216C8821998-04-0808 April 1998 Safety Evaluation Supporting Amend 32 to License DPR-7 ML20129J4311996-10-18018 October 1996 Safety Evaluation Approving Corporate Restructuring & Establishment of Holding Company Under Temporary Name PG&E Parent Co.,Inc of Which PG&E Would Become Wholly Owned Subsidiary ML20151G2361988-07-19019 July 1988 Safety Evaluation Supporting Amend 23 to License DPR-7 ML20210C5311987-04-30030 April 1987 SER Re Decommissioning of Facility ML20211C5721987-02-11011 February 1987 Safety Evaluation Supporting Amend 22 to License DPR-7 ML20212N4921986-08-26026 August 1986 Safety Evaluation Supporting Amend 21 to License DPR-7 ML20206H1771986-06-16016 June 1986 Safety Evaluation Supporting Amend 20 to License DPR-7 ML20128M6691985-07-16016 July 1985 Safety Evaluation Supporting Amend 19 to License DPR-7 1998-04-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20211J6651998-12-31031 December 1998 10CFR50.59 Annual Rept of Changes,Tests & Experiments for 980101-981231 for Humboldt Bay Power Plant,Unit 3 DCL-99-045, 1998 Annual Financial Rept for PG&E Corp. with1998-12-31031 December 1998 1998 Annual Financial Rept for PG&E Corp. with ML20151U1691998-08-28028 August 1998 Rev 2 to DSAR for Humboldt Bay Power Plant,Unit 3 ML20216C8821998-04-0808 April 1998 Safety Evaluation Supporting Amend 32 to License DPR-7 ML20203J6601998-02-28028 February 1998 Post-Shutdown Decommissioning Activities Rept for Humboldt Bay Power Plant,Unit 3 ML20195F4541997-12-31031 December 1997 10CFR50.59 Annual Rept of Changes,Tests & Experiments for Jan-Dec 1997 ML20217G5151997-12-31031 December 1997 1997 PG&E Corp Annual Rept HBL-97-013, Annual Rept of Changes,Tests & Experiments for Plant for Jan-Dec 1996,per 10CFR50.591997-12-19019 December 1997 Annual Rept of Changes,Tests & Experiments for Plant for Jan-Dec 1996,per 10CFR50.59 ML20205F5881997-07-24024 July 1997 Decommissioning Cost Estimate for Diablo Canyon Power Plant,Units 1 & 2 ML20205F5991997-04-12012 April 1997 Decommissioning Cost Estimate for Humboldt Bay Power Plant, Unit 3 DCL-97-045, Pacific Gas & Electric Co 1996 Annual Rept1996-12-31031 December 1996 Pacific Gas & Electric Co 1996 Annual Rept ML20129J4311996-10-18018 October 1996 Safety Evaluation Approving Corporate Restructuring & Establishment of Holding Company Under Temporary Name PG&E Parent Co.,Inc of Which PG&E Would Become Wholly Owned Subsidiary ML20058P6281993-08-31031 August 1993 Rev 6 to Pacific Gas & Electric Co Humboldt Bay Power Plant Unit 3 - Safstor QA Plan ML20141M0471991-12-31031 December 1991 Pge Annual Rept - 1991 ML20236E0581988-12-31031 December 1988 Pacific Gas & Electric Co Annual Rept 1988 ML20151G2361988-07-19019 July 1988 Safety Evaluation Supporting Amend 23 to License DPR-7 ML20151P6951988-04-30030 April 1988 Pacific Gas & Electric Co,Humboldt Bay Power Plant,Unit 3 Safstor QA Plan ML20196F3641988-01-31031 January 1988 Monthly Operating Rept for Jan 1988 ML20148Q3281987-12-31031 December 1987 PG&E 1987 Annual Rept HBL-87-086, Annual Rept of Design Changes,19861987-12-29029 December 1987 Annual Rept of Design Changes,1986 ML20237H7861987-07-31031 July 1987 Monthly Operating Rept for Jul 1987 ML20236G8241987-07-31031 July 1987 QA Plan for Humboldt Bay Power Plant Unit 3 - Safstor ML20237K8471987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML20235C9311987-06-23023 June 1987 Rept to ACRS Re Humboldt Bay Unit 3 - Core II ML20237K4221987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20210C5311987-04-30030 April 1987 SER Re Decommissioning of Facility ML20237K5311987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20211C5721987-02-11011 February 1987 Safety Evaluation Supporting Amend 22 to License DPR-7 ML20205C0891987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20204H4331986-12-31031 December 1986 PG&E Annual Rept for 1986 ML20212P8841986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 ML20211Q0541986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20211H3401986-10-31031 October 1986 PG&E Responses to Public Comments on Des for Decommissioning Humboldt Bay Unit 3 ML20212L8991986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20207F8221986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20207D6041986-08-31031 August 1986 Monthly Operating Rept for Aug 1986 ML20212N4921986-08-26026 August 1986 Safety Evaluation Supporting Amend 21 to License DPR-7 ML20215D4281986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20214L7861986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20206H1771986-06-16016 June 1986 Safety Evaluation Supporting Amend 20 to License DPR-7 ML20206C3131986-06-15015 June 1986 Comments on Des for Decommissioning Humboldt Bay Power Plant,Unit 3. Monetary Cost Estimates & Data on Contamination from Early Pool Leak Should Be Provided ML20205Q0061986-05-31031 May 1986 Rev 2 to Safstor QA Plan ML20205D6071986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20154Q0541986-03-31031 March 1986 Rev 1 to Safstor QA Program ML20197D1711986-02-28028 February 1986 Monthly Operating Rept for Feb 1986 ML20203E0151986-01-31031 January 1986 Monthly Operating Rept for Jan 1986 ML20210F2361985-12-31031 December 1985 Monthly Operating Rept for Dec 1985 ML20138C5521985-12-31031 December 1985 1985 Annual Rept ML20138L8501985-12-31031 December 1985 Rev 1 to Humboldt Bay Power Plant Unit 3 - Safstor QA Plan ML20137U3771985-11-30030 November 1985 Monthly Operating Rept for Nov 1985 1998-08-28
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\...../ l SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR kEGULATION SUPP0? TING AMENDMENT N0.21 TO FACILITY OPERATING LICENSE N0. DPR-7 PACIFIC GAS AND ELECTRIC COMPANY HUMBOLDT BAY POWER PLANT, UNIT NO. 3 DOCKET NO. 50-133
1.0 INTRODUCTION
Humboldt Bay Power Plant, Unit No. 3 (the facility) is permanently shut down. By Amendment No. 19 issued on July 16, 1985 License No. DPR-7 was amended to possess-but-not-operate status.
All fuel has now been removed from the reactor vessel and placed in !
the spent fuel storage pool. The reactor cooling system'and .
associated tanks and pipes have been drained and sealed. The suppression pool, below the reactor vessel, has been drained. The ,
l only water containing radionuclides that remains en site is the water ,
in the spent fuel pool, its associated systems'and in the radwaste tanks.
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0 Pacific Gas and Electric Company (the licensee) requested an amendment to the Technical Specifications (TS) to: 1) upgrade requirements for the stack gas monitoring system to be more sensitive to radior.uclides
- present at the facility, and 2) reduce the required number of condensate demineralizer beds from three to two to allow one of the beds to be used as a spent fuel pool demineralizer.
2.0 EVALUATION The present stack gas monitoring systeni is sensitive to halogens (radioiodine) and particulates. In addition, two gamma monitoring systems detect noble gases. With the plant permanently shut down for over 10 years, radionuclides with relatively short half lives such as radiofodines are no longer present. In addition the gamma monitoring system was designed to be sensitive to noble gas mixtures expected during reactor operations, such as xenon-138 and 135, and is relatively insensitive to krypton-85. Krypton-85 is currently the dominant noble gas in the spent fuel. The proposed stack monitoring system will be modified to ha more sensitive to krypton-85 and will continue to monitor radionuclide particulates. Radioiodine (halogen) monitoring will.be discontinued since these radionuclides are ro longer present at the facility.
We have determined that this change will improve the capability of the stack monitoring system to detect and measure radionuclides now present.
We also agree that halogen radforiuclides are no longer present at the facility due to their short half lives and no longer need to be monitored.
Thus, this change is acceptable.
8608280253 860826 PDR ADOCK 05000133 p PDR
The condensate demineralizer bed; are no longer needed for the reactor cooling system since it is now dry. Furthermore, the use of one of these beds as a spent fuel pool deminaralizer will allow the pool water to be maintained at a higher quality with a reduced radionuclide content and results in an improvement in the facility in its present permanently shutdown status. Thus, this change is acceptable.
3.0 ENVIRONMENTAL CONSIDERATION
This amendment involves changes in the installation or use of facility components located within the restricted areas as defined in 10 CFR 20. The staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite and that there is no significant increase in individual or cumulative occupational l radiation exposure. The Commission has previously issued a proposed i finding that this amendment involves no significant hazards consideration and there has been no public comment on such finding.
Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 651.22(c)(9). Pursuant to 10 CFR 951.22(b), no environmental impact statement or environmental -
assessment need be prepared in connection with the issuance of,this amendment.
4.0 CONCLUSION
We have concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by maintenance of the facility in the proposed manner, and (2) such activities will be conducted in compliance with the Commission's regulations, and the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
5.0 ACKNOWLEDGEMENT ,
This evaluation was prepared by Peter B. Erickson Dated: August 26, 1986 i
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