ML20212M190
| ML20212M190 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 01/16/1987 |
| From: | Jerrica Johnson, Prell J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20212M155 | List: |
| References | |
| 50-244-86-22, NUDOCS 8701300033 | |
| Download: ML20212M190 (5) | |
See also: IR 05000244/1986022
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report No.
50-244/86-22
Docket No.
50-244
License No.
Licensee:
Rochester Gas and Electric Corporation
49 East Avenue
Rochester, New York 14649
Facility Name: Ginna Station
Inspection At: Ontario, New York
Inspection Conducted:
December 15-19, 1986
Inspectors: _kM
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J
rell, Reactor Engineer
date
11. 16kwtS A
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Approved by:
U
J. Johnson, Chief,
date
Operational Programs Section, OB, DRS
Inspection Summary:
Routine, announced inspection on December 15-19, 1986
(Inspection Report No. 50-244/86-22).
Areas Inspected:
Licensee's response to previous inspection findings and the
effectiveness of the licensee's correction action program.
Results: No violations or deviations were identified.
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8701300033 870116
ADOCK 05000244
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DETAILS
1.0 Persons Contacted
Rochester Gas and Electric Co.
C. Anderson, QA Manager
D. Baker, Electrician
J. Bodine, Nuclear Assurance Manager
D. Bryant, QA Engineer
- K. Easterbrook, QA Engineer
- R.
Kober, Vice President Electrical Production
- T. Meyer, Superintendent-Ginna Support Service
- K. Nassauer, QC Supervisor
R. Smith, Chief Engineer
- B. Snow, Superintendent Nuclear Production
- W. Stiewe, QC Engineer
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- Denotes those present at exit meeting.
2.0 Licensee Action on Previous Inspection Items
(0 pen) Violation (50-244/86-02-03)
Inadequate inspection of welds on the
reactor vessel head lifting rig and reactor vessel lifting rig.
In response to this violation the licensee performed the following actions:
Reviewed and revised the refueling procedures to assure QC hold
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points relative to Material Handling Equipment (MHE) procedures were
established.
Provided a formal training program to assure MHE personnel had
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received indoctrination and training on procedural requirements.
Modified the ISI Maintenance and Materials Engineering computerized
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tracking program to include special lifting device inspections.
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Conducted training of QA personnel to ensure an effective verification
inspection program.
The inspector verified that the last three items were satisfactorily
completed.
The first item, establishing appropriate QC hold points in the
MHE procedures, had not yet been completed. This item remains open until
revision of and verification of appropriate QC hold points in Westinghouse
procedure RF-62.
(Closed) Violation (50-244/86-02-04) A safety related stainless steel
wire rope was purchased from an unqualified supplier and accepted by the
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licensee without a receipt inspection. Calibration services for direct
readout gauges for hydraulic torque wrenches were purchased from an
unqualified supplier.
In response to this violation the licensee performed the following:
Contacted the vendor of the stainless steel wire rope to receive
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documentation to correlate the rope with the purchase order and to
correct a typographical error in the guarantee letter.
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Revised the procurement program to add a statement to purchase
orders (P.O.s) to ensure that any requested test reports are
traceable to the specific P.O. and that receipt inspectors verify
the same.
Clarified the QA Manual section related to receipt inspections to
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address various acceptable inspection methods.
Revised the appropriate administrative procedures to reflect the
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changes made to the QA Manual.
Provided training on the procurement and control of commercial grade
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items.
Reviewed for clarity the administrative procedures related to
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tagging of bulk items arriving on site.
Prepared and dispositioned a nonconformance report for the received
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unqualified torque wrenches.
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Evaluated suppliers of gauge / torque wrench calibrations, and
Informed receiving personnel of requirements to tag bulk items.
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The inspector verified that all the above actions were taken by the
licensee and found them acceptable.
This item is closed.
(Closed) Violation (50-244/86-02-08) The procedure used for performing
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maintenance of the circuit breakers for component cooling system "B"
pump
did not specify acceptance criteria for measuring the resistance of the
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circuit breaker; and the technician and QA inspector performing the
activity were not proficient in that they failed to verify the calibration
status of the measuring instrument used.
The licensee responded to this violation by taking the following actions:
The mega deck calibrator, used for calibrating meggers, is now being
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controlled as Category II M&TE and has been scheduled to be
recalibrated annually.
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All Electric Shop meggers are now being controlled as Category III
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M&TE and are scheduled to recalibrated annually.
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Records, logs and recall sheets are being maintained per administra-
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tive procedures.
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M&TE not previously under the control of the M&TE calibration
program were reviewed for the need of additional controls. As a
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result of this review hydrometers were added to the M&TE calibration
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progran.
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Electric shop and I&C personnel were instructed on the new controls
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for M&TE.
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Acceptance criteria and sign offs for megger serial number and re-
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calibration due dates were incorporated into 12 Electric Shop
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procedures.
The Quality Assurance Manual and supporting Administrative Pro-
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cedure, A-1201, were revised.
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The inspector verified the above actions and had no further concerns.
This item is closed.
(Closed) Violation (50-244/86-02-09) The circuit schedule which
specified cable conductor terminations for circuits G-1234, G-1235,
G-1237 and G-12344 in safety related Engineering Work Request No. 4067
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was prepared and reviewed by the same individual.
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In response to this violation the licensee instructed electrical
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engineers that circuit schedules are to be prepared and reviewed by
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different individuals.
The electrical engineering manager now reviews
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circuit schedules to ensure they are prepared and reviewed by different
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individuals.
Procedure QA-303 has been revised to provide instructions
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for preparation and review of circuit schedules.
The inspector verified that the above actions were completed.
This item
is closed.
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3.0 Licensee's Corrective Action / Quality Control Program
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3.1 P ro g r_a_m_
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The result of two previous region-based NRC inspections and two
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resident inspections (85-04, 86-02, 86-16, and 86-18) indicate that
the licensee's program for controlling quality ha& degraded somewhat.
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As a result of these inspections the licensee initiated corrective
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actions to upgrade their quality assurance program.
The following
three programs appear to be the most effective:
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A "Back to Basics" program is being given to middle and lower
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level management personnel which stresses the " whys" and
" rationale for" a quality program as mandated by 10 CFR 50
Appendix B requirements.
A severity level program, has been established for monitoring,
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controlling and escalating corrective action requests and
nonconformance reports.
If a satisfactory response to a finding
is not received within 30 days the finding is escalated to the
next higher level.
The station superintendent gets a monthly
report on the status of all findings.
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A QA/QC subccmmittee has been permanently established which
reports to the off-site safety review committee.
This sub-
committee meets monthly to review quality related concerns.
Each month the committee receives a copy of the monthly status
report on quality related findings and a special listing of the
top ten findings.
They also initiate programs to promote
quality.
In addition, the licensee has recently completed having an
independent survey performed of a large . ample of staff at all levels
to determine their attitude towards quality and management.
Results
of this survey are now in the process of being evaluated by the
licensee.
3.2 Findings
Improvements were noted in the prioritizing of corrective actions for
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licensee identified nonconformances.
Effective use of plant staff
and committee meetings was discussed with the licensee's senior
management who acknowledged the comments and stated that this area
would be reviewed for possible improvements.
No violations or
unresolved items were identified.
4.0 Plant Tours
During this inspection period the inspector toured the control room, the
turbine building and administrative offices.
It was noted that
scaffolding was erected throughout the control room for the purpose of
changing the lighting system.
(Subsequent to this inspection this
scaffolding has been removed).
No violations were identified.
5.0 Exit Meeting
An exit meeting was held on December 19, 1986, to discuss the inspection
scope and findings, as detailed in this report.
(See Paragraph 1.0 for
attendees).
At no time was written material given to the licensee.
The inspector
determined that no proprietary information was utilized during this
inspection.
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