ML20212B670
| ML20212B670 | |
| Person / Time | |
|---|---|
| Site: | South Texas |
| Issue date: | 10/22/1997 |
| From: | Tapia J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Cottle W HOUSTON LIGHTING & POWER CO. |
| References | |
| 30-498-97-05, 30-498-97-5, 30-499-97-05, 30-499-97-5, NUDOCS 9710280167 | |
| Download: ML20212B670 (5) | |
See also: IR 05000498/1997005
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NUCLEAR REGULATORY COMMISSION
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OCT 2 21997
William T. Cottle, Group Vice
President, Nuclear
Houston Lighting & Power Company
P.O. Box 289
Wadsworth, Texas 77483
SUBJECT: NRC INSPECTION REPORT 50 498/97-05;50-499/97 05
Dear Mr. Cottle:
Thank you for your letter of October 16,1997, in response to our letter and Notice
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of Violation dated September 9,1997. We have reviewed your reply and find it responsive
to the concerns raised in our Notice of Violation. We will review the implementation of
your corrective actions during a future inspection to determine that full compliance has
been achieved and will be maintained.
Sincerely
.
Joseph I. Ta
, Chief
Project Branch A
Division of Reactor Projects
Docket Nos.: 50-498
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50-499
License Nos.: NPF-76
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NPF 80
cc:
Lawrence E. Martin, General Manager
Nuclear Assurance & Licensing
Houston Lighting & Power Company
P.O. Box 289
Wadsworth, Texas 77483
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Mr. J.- C. Lanier/Mr. M. B. Lee
City of Austin
Electric Utility Department
--721 Barton Springs Road
- Mr. K. J. Fiedler/Mr. M. T. Hardt
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City Public Service Board
' P.O. Box 1771'
San Antonio, Texas 78296
Jack R. Newman, Esq.
Morgan, Lewis & Bocklus
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1800 M. Street, N.W.
- Washington, D.C. 20036 5869
Mr.' G. E. Vaughn/Mr. C. A. Johnson
Central Power & Light Company
P.O. Box 289
Mail Code: N5012
Wadsworth, Texas 77483
INPO-
- Records Center
700 Galleria Parkway
Atlanta, Georgia 30339 5957
Dr. Bertram Wolfe
15453 Via Vaquero
- Monte Sereno, California 95030
Bureau of Radiation Control
State of Texas
1100 West 49th Street
Mr. Glenn W. Dishong
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Texas Public Utility Commission-
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- John Howard, Director
Environmental and Natural _He1ources Policy
Offics of the Governor
P.O. Box 12428
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Judge, Matagorda. County
Matagorda County Courthouse
1700 Seventh Street
Bay City, Texas 77414-
Licensing Representative
Houston Lighting & Power Company
Suite 610-
Three Metro Center
Bethesda, Maryland : 20814
Rufus S. Scott,- Associate -
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General Counsel -
Houston Lighting & Power Company -
P.O.' Box 61867
Houston, _ Texas 77208
Joseph R._Egan, Esq.
Egan & Associates, P.C.
2300 N Street, N.W.
Washingtou, D.C. -20037
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October 16, 1997
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ST-1IL-AE-5768
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File No.: G02.04.02
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STI-30432655
U. S. Nuclear Regulatory Commission
Attention: Document Control DesL
Washington, DC 20555
South Texas Project
Units 1 and 2
Docket No. STN 50-498 and 499
Rep]y_to Notice of Violation 97005-03
South Texas Project has reviewed Notice of Violation 97005-03, dated September 9,
1997, and submits the attached reply. The events described in the Notice of Violation did not
have an adverse effect on the health and safety of the public.
On October 8,1997, your Mr. Joe Tapia granted an extension until October 21,1997 for
this response.
If there are any questions regarding these replies, please contact Mr. S. M. llead at (512)
972-7136 or me at (512) 972-7800.
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Gary Parkey
Plant Manager, Unit i
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Attachment:
Reply to Notice of Violation 97005-03
99-0I43
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llouston Light,ng & Power Company
ST llL-AI! 5768
South Tesai Project Electric Cencrating station
File No.:
G02.04.02
Page 2
Ellis W. MerschofT
Rufus S. Scott
Regional Administrator, Region IV
Associate General Counsel
U. S. Nuclear Regulatory Commission
Houston Lighting & Powei Company
611 Ryan Plaza Drive, Suite 400
P. O. Ilox 61067
Arlington, TX 76011-8064
llouston, TX 77208
Thomas W. Alexion
Institute of Nuclear Power
Project Manager, Mail Code 13113,
Operations - Records Center
U. S. Nuclear Regulatory Commission
700 Galleria Parkway
Washington, DC 20555-0001
Atlanta, G A 30339-5957
David P. Loveless
Dr. Bertram Wolfe
Sr. Resident inspector
15453 Via Vaquero
e/o U. S. Nuclear Regulatory Comm.
Monte Sereno, CA 95030
P. O. Ilox 910
Bay City, TX 77404-0910
Richard A. RatlilT
llureau of Radiation Control
J. R. Wwman, Esquire
Texas Department ofIlealth
Morgan, Lewis & Hockius
1100 West 49th Street
1800 M Street, N.W.
Austin, TX 78756-3189
Washington, DC 20036-5869
J. R. Egan, Esqt. ire
M. T, Ilardt/W C. Gunst
Egan & Associates, P.C.
City Puhile Service
2300 N Street, N.W.
P. O. Box 1771
Washington, D.C. 20037
San Antonio,TX 78296
J. C. Lanier/M. B. Lee
U. S. Nuclear Regulatory Commission
City of Austin
Attention: Document Cor. trol Desk
Electric Utility Deparunent
Washington, D.C. 20555-0001
721 Barton Springs Road
Austin,TX 78704
Cemral Power and Light Compeny
ATTN: G. E. Vaughn/C. A. Johnson.
P. O. Box 289, Mail Code: N5012
Wadsworth,TX 77483
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Attachment 1
ST.HL AE-5768
Page1of3
1.
Statement of Violation:
' Technical Specification 6.8.1.a requires, in part, that written precedures be established,
implemented, and maintained conceming the applicable procedures recommended in
Appendix A of Regulatory Guide 1.33, Revision 2, Febtaary 1978. Regulatory Guide 1.33, Appendix A, Section 9.c.(l), states that procedures should include information on
the method for obtaining permission and clearance for work. This requirement is
implemented, in part, by Plant General Procedure OPGP03-ZO-EC01, Re.ision 6,
" Equipment Clearance Orders." This procedure requires that equipment clearance orders
shall provide adequate personnel and equipment safety.
Contrary to the above:
On June 24, Equipment Clearance Order 97-2-76518 failed to provide adequate personnel
and equipment safety in that Essential Cooling Water Screen Wash Booster Pump 2A
inadvenently started while the system was drained.
Also, on July 21, Equipment Clearance Order 97-1-71609 failed to provide adequate
personnel and equipment safety in that workers breached an unisolated component -
cooling water system pipe while performing maintenance on Residual Heat Removal
Pump 1B.-
This is a Severity Level IV violation (Supplement 1)(498;499/97005-03).
II.
South Texas Project Position:
South Texas Project concurs that the violation occurred.
III.'
Reason for the Violaticn:
The cause of the June 24, Unit 2 Screen Wash Booster Pump event was the failure of the
. Senior Reactor Operator to identify the additional relay contacts that actuate the Screen Wash
Booster Pump during his review of the Equipment Clearance Order for the Traveling Screen.
. The July 21, Unit 1 Residual Heat Removal event was caused by less than adequate
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communications between the work package planner and the Equipment Clearance Order
preparer. In addition, the Equipment Clearance Order acceptor did not perform an adequate
. walkdown verification.
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Attachment i
ST ill Ali 5768
Page 2 of 3
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IV.
COltitECTIVE ACTIONS:
As a result of the Scicen Wash Ilocster Pump event, the following cornctive actions have been
initiated.
1.
The 2A Screen Wash llooster Pump was tested and verified to be operable.
2,
The Work instructions for the implementation of this DCP on Unit I were revised
to include a precaution that identifies this potential event.
3.
'lhe individuals involved in this event were counseled on the importance of
correct Equipment Clearance Orders.
As a result of the flesidual llcat Removal Pump issue, the following actions have been initiated
1.
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sment Clearance Order 97 1 71609 was revised to isolate Component
t Jnp Water to and from the seal cooler, and work order Ril 347683 was
completed safely.
2.
Manageroent has reinforced expectations on the level of detail that will be
provided to the Ik uipment Clearance Order preparer during meetings with Work
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Conaol phmners. 'lhese activities were completed September 10,1997.
3.
'lhe importance of correct Equipment clearance Order preparation and review
was reinforced to all Equipment Clearance Order preparers and reviewers during
meetiligs with supervision. These activities were completed September 10,1997.
4.
Management's expectations for Equipment Clearance Order acceptance were
reinforced to Maintenance personnel during special meetings. These activities
were completed September 10,1997.
These shon tenn corrective actions will resolve the issues identified in this Notice of Violation.
The actions described in section VI are designed to ensure all other issues that may exist . ire
identified and permanently corrected.
V.
Date of Full Compliance:
Ihe Sch Texas Project is in full compliance.
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Attachment 1
Page 3 of 3
VI.
Additionallnformation
Ilased on this violation and other related issues that we have previously identified
through our corrective action program, the following actions are also planned.
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A Project Manager has been assigned to lead a multi discipline team in a
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comprehensive process review of the STP Nuclear Operating Company
liquipment Clearance Order procedure ( including the use of danger tags, caution
tags and test tags) and the plant configuration progr..m.
2.
The general scope of this review will be to identify industry best practices,
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perform a comparison with the STP Nuclear Operating Company program,
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identify areas for improvement, modify the procedure, and train station personnel.
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These actions will be completed by the end of the second quarter of 1998.
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