ML20211N876

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Notice of Violation from Insp on 860501-31
ML20211N876
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 07/03/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20211N872 List:
References
50-285-86-14, NUDOCS 8607110063
Download: ML20211N876 (1)


Text

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6 APPENDIX A NOTICE OF VIOLATION Omaha Public Power District Docket: 50-285/86-14 Fort Calhoun Station License: DPR-40 During an NRC inspection conducted on May 1-31, 1986, a violation of the NRC requirements was identified. The violation involved the failure to maintain cable and cable tray installations in accordance with design documentation. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985), the violation is listed below:

4 Criterion V of Appendix B to 10 CFR Part 50, as impl.emented by the OPPD

. Quality Assurance Plan, Section 4.2.1, requires, in part, that activities '

! affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Drawing 11405-E-60, " Reactor Auxiliary Building Tray Conduit Layout Plan," i requires in Note 17 that solid covers be installed on cable trays.

Drawing 11405-E-151, " Cable and Conduit Schedule Notes," .equires in Note 18 that control and instrument cable be tied down in a neat configuration after installation in trays and in Note 20(a) that the 600-volt power cable fill of the trays shall not exceed 40 percent of the

rectangular area of the cable tray.

Contrary to the above, cable and cable tray installations have not been maintained in accordance with design documents in that cable tray covers were not properly installed on trays in Rooms 69 and 57, and in the east and west switchgear rooms; control and instrument cable was not properly tied down in trays EA 5-4 and EB 5-4; 'and the cable tray fill requirement was exceeded in cable tray location 21-S. ,

This is a Severity Level IV violation.

(Supplement I.D) (285/8614-01)

Pursuant to the provisions of 10 CFR Part 2.201, Omaha Public Power District is hereby required to submit to this office within 30 days of the date of the letter transmitting this Notice, a written statement or explanation in reply, including for each violation: (1) the reason for the violations if admitted, (2) the corrective steps which have been taken and the results achieved, (3) the corrective steps which will be taken to avoid further violations, and (4) the date when full compliance will be achieved. Where good cause is shown, consideration'will be given to extending the response time.

Datedcat Arlington, Texas, this pd day of g - 1986.

L g7110063C60703 g ADOCK 05000285 PDR

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