ML20211K036

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Forwards Revised Response to IE Bulletin 85-003, Motor- Operated Valve Common Mode Failure During Plant Transients Due to Improper Switch Settings. Supplemental Info Added Re torque-switch Bypassing During Valve Travel
ML20211K036
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 11/03/1986
From: Kemper J
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20211K039 List:
References
IEB-85-003, IEB-85-3, NUDOCS 8611140243
Download: ML20211K036 (2)


Text

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PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET P.O. BOX 8699 PHILADELPHIA PA.19101 1215)841 4502 V 6C E-PR ESID E N T Noyember 3, 1986 i

Dr. Thomas E. Murley Docket Nos.

50-277 Regional Administrator, Region I 50-278 U. S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19046

Subject:

Peach Bottom Atomic Power Station Units 2 & 3 I.E.Bulletin 85-03, " Motor-0perated Valve Common L

Mode Failure During Plant Transients Due to Improper Switch Settings"

Reference:

Letter, J. S. Kemper (PECo) to T. E. Murley (NRC),

dated October 2, 1986 (Revised Copy Attached)

Dear Mr. Murley:

By this letter, Philadelphia Electric Company (PECo) submits a revised response to I.E.Bulletin 85-03 which corrects our previous submittal for the Peach Bottom Atomic Power Station.

In our response to Item (a) of the Bulletin, it was incorrectly stated that all differential pressures developed in accordance with the BWROG methodology were found to be less than the originally specified values. This statement is correct except for the HIJI and RCIC torus suction valves (M0-23-57 & 58 and M0-13-39 & 41).

For these valves, the originally specified differential pressure is 65 psid whereas the maximum differential pressure calculated using the BWROG methodology is 93 psid (in the open direction only).

This condition does not affect the adequacy of the valves in question. As part of our IEB 85-03 program, we have confirmed with valve and motor-operator vendors that the valve assemblies have the design capability to operate under the higher differential pressure conditions.

In addition to the above, we have provided the following minor revisions:

1)

Supplemental information has been added regarding torque-switch bypassing during valve travel in the open direction which is a current PBAPS design feature.

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The table has been revised to reflect the correct normal position of valve M0-13-20.

3)

Typographical errors have been corrected.

In summary, PECo still adopts the BWROG-based maximum operating differential pressures as previously submitted for the purposes of the IEB 85-03 program (i.e., verification testing of the MOVs will be based on the BWROG developed values).

Please disregard the referenced submittal and consider the attached version as the Philadelphia Electric Company response to I.E.

Bulletin 85-03 for the Peach Bottom Atomic Power Station Units 2 & 3.

PECo apologizes for any inconvenience that these changes may cause your office in processing our submittal.

Sincerely, TSN/pd10168606 Copy to:

T. P. Johnson, Resident Site Inspector USNRC, Document Control Desk

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