ML20211J332

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Insp Rept 50-341/87-06 on 861229-870209.Violations Noted: Failure to Verify Adequacy of Design & Failure to Preoperational Test & Surveillance Test Hydrogen Recombiner Sys.Insp Based on 861226 Event
ML20211J332
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 02/20/1987
From: Greenman E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20211J267 List:
References
50-341-87-06, 50-341-87-6, NUDOCS 8702260417
Download: ML20211J332 (5)


See also: IR 05000341/1987006

Text

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U.S NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-341/87006(DRP)

Docket No. 50-341

Operating License No. NPF-43

Licensee:

Detroit Edison Company

2000 Second Avenue

Detroit, MI 48226

Facility Name:

Fermi 2

Inspection At:

Fermi Site, Newport, Michigan

Inspection Conducted:

December 29, 1986, through February 9, 1987

Inspectors:

W. G. Rogers

M. E. Par er

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Approved By:

E. G. Greenman, Deputy Director

DivisionofReactorProjects

Date

Inspection Summary

Inspection on December 29, 1986, through February 9, 1987 (Report No.

50-341/87006(DRP))

Areas Inspected:

Special unannounced inspection by two resident inspectors

of the events surrounding the discovery on December 26, 1986, of both

(24.409.01) divisions of hydrogen thermal recombiners being ino)erable.

Results:

Three violations were identified (failure to verify tie adequacy

of design, failure to preoperational test and surveillance test the hydrogen

recombiner system utilizing the designed cooling water system, and the plant

entered Operation Condition 2 on eleven occasions with both divisions of the

hydrogen recombiner system inoperable - Paragraph 2).

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DETAILS

1.

Persons Contacted

a.

Detroit Edison Company

+* Frank Agosti, Vice President, Nuclear Operations

S. Becker, Maintenance

B. Catanese, Maintenance Staff

+*S. Catola, Chairman, Nuclear Safety Review Group

+0. K. Earle, Technical Engineer

  • S. Frost, Licensing

S. Heard, Assistant Operations Engineer

+*J. Leman, Superintendent, Maintenance and Modification

+*R. Lenart, Plant Manager, Nuclear Production

+*R. May, Maintenance Engineer

+*G. Ohlemacher, I&C Assistant Maintenance Engineer

+*W. Orser, Vice President, Nuclear Engineering

  • R. Poche, Licensing

+*E. Preston, Operations Engineer

+T. Randazzo, Director, Regulatory Affairs

  • L. Simpkin, Nucleu Engineering Director

+*F. Sondgeroth, Licensing

+*B. R. Sylvia, Group Vice President, Nuclear Operations

+*G. Trahey, Director, Quality Assurance

+*W. Tucker, Acting Superintendent, Operations

b.

U.S. Nuclear Regulatory Commission

+*M. Parker, Resident Inspector

+*W. Rogers, Senior Resident Inspector

+M. Farber, Reg #cnal Inspector

  • Der .es those attending exit meeting on January 15, 1987.

+ Denotes those attending exit meeting on February 3, 1987.

Other personnel were contacted as a matter of routine during

the inspection.

2.

Hydrogen Recombiner System

On December 26,fication required six month functional surveillance 1986, at 1

Technical Speci

(24.409.01) on the Division II hydrogen recombiner system.

The

surveillance was being performed using the Residual Heat Removal

keep-fill (demineralized water) system as a source of cooling water for

the hydrogen recombiner system.

During the surveillance, the licensee

initiated the Residual Heat Removal (RHR) system in the torus cooling

mode in preparation for HPCI testing.

At the same time the RHR system

was started, the air temperature of the hydrogen recombiner began

decreasing.

This prevented successful completion of the hydrogen

recombiner surveillance.

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Technical Specification 4.6.6.1 states, "Each drywell and suppression

chamber hydrogen recombiner system shall be demonstrated OPERABLE at

least once per six months by verifying during a recombiner system

functional tast that the heater outlet gas temperature increases to

greater than or equal to 1150 F within 75 minutes and is maintained

for at least one hour." The licensee was unable to satisfy these

requirements upon initiation of the RHR system and subsequently declared

both divisions of hydrogen recombiners inoperable and took appropriate

action to comply with the applicable Technical Spec'fication action

statements.

The licensee initially determined that the inability to achieve outlet

gas temperature was due to excessive cooling water flow.

The cooling

water flow to the hydrogen recombiners had been provided at about 60 psig

through the RHR keep-fill system. When the RHR system was started, the

cooling water pressure was increase'd to about 220 psig which resulted in

greater flow and thus more coeling.

This resulted in a decrease of the

thermal recombiner temperature.

The licensee subsecuently adjusted the

cooling water flow, repeated the surveillance, and ceclared both divisions

of the thermal recombiners operable on December 27, 1986.

In order to satisfy operability concerns addressed by the resident

inspectors, the licensee repeated the surveillance with the manual

isolation valve full open, simulating the original test conditions.

The

Division I thermal recombiner passed the surveillance on January 8,1987,

but Division II failed on January 9,1987.

After the second surveillance failure on the Division II thermal recombiner

system on January 9,1987, pressure gauges were installed on the cooling

water line.

The RHR pressure to the unit was measured at 190 psig and

the pressure to the blower seal was measured at 140 psig.

Rough flow

measurements determined that approximately three gpm were provided to

the seal with one and one-half gpm at the seal outlet.

The licensee

subsequently determined that the blower seal was leaking internally

at the higher RHR pressures.

Discussions with the seal manufacturer, Durametallic Corporation, concluded

that the springs in the blower seal will compress at 39 psid and could

allow water to enter the blower cavity.

Vendor drawings identified that

the blower seal was designed for a cooling water flow of one gpm at

10 psi 15 psi.

Rockwell International vendor drawing No. N019560002

provided for an RHR system pressure to the hydrogen recombiners of

100 psi minimum, while Rockwell internal letter to H. L. Yobs from

S. A. Itow dated January 13, 1987, indicates 100 psi.

Neither specified

the actual 220 psi to the unit.

The licensee specification 3071-107 dated

April 13, 1972, specifically identified a 250 psig(water source to the341/87006-01(DRP)) o

recombiner units.

This is considered a violation

10 CFR 50, Appendix B, Criterion III, Design Control, for failure to

appropriately verify the adequacy of design.

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A review of the preoperational test program identified that the thermal

T4804.001,"preoperational' test, "T4804 Thermal Recombiner System PRET

recombiner

Revision 2, allowed the use of the RHR system or an alternate

source if needed to supply cooling water.

The PRET identified that the RHR keep-fill system was utilized in the

-preoperational test and that no specific intent was made to utilize the

higher RHR pressures to verify proper system operation.

The system was

operated on nyeral occasions and each time the RHR keep-fill system was

used as a source of cooling water.

Through discussions with personnel

there were several reasons that the RHR was not utilized:

(1) RHR pump

availability; (2) economic factors, and (3) RHR keep-fill availability.

As a result, the hydrogen recombiner system was never tested utilizing the

higher RHR pressures. Additionally, functional surveillance Procedure

No. 24.409.01, " Post LOCA Thermal Recombiner Functional Test," Step

No. 5.3, allowed the RHR keep-fill system to be in service to provide

water to the blower and spray cooler during the test.

A temporary change

to this procedure, effective December 26, 1986, deleted the use of the

RHR kee)-fill system.

This is considered a violation (341/87006-02(DRP))

of 10 CFR 50, Appendix B, Criterion XI, Test Control, for failure to

preoperational test and surveillance test utilizing the designed cooling

water system.

On January 9, 1987, the licensee identified that while utilizing the RHR

systemasasourceofcoolingwater,theDivisionIIhydrogenrecombiner

system only heated up to 761 F within the required 75 minute time period.

Technical Specification 4.6.6.1 requires the outlet gas temperature to

increase to greater than or equal to 1150 F within 75 minutes.

The

inability to obtain the required gas temperature was due to excessive

internal cooling water seal leakage at the higher RHR pressures.

As a

result, the Division II hydrogen recombiner system was inoperable and

unable to satisfy the surveillance requirements of Technical Specification 4.6.6.1 utilizing the designated source of cooling water.

Ever since the last seal replacement on August 29, 1985, the licensee has

noticed external seal leakage with the Division II recombiner.

Therefore,

the Division II hydrogen recombiner system was considered inoperable since

the seal replacement on August 29, 1985.

Technical Specifications 3.6.6.1 states that "Two independent drywell

and suppression chamber hydrogen recombiner systems shall be OPERABLE

in Operational Conditions 1 (power operation) and 2 (startup).

Technical Specification 3.0.4 states in part, " Entry into an OPERATIONAL

CONDITION or other specified condition shall not be made unless the

conditions for the Limiting Condition for Operation are mb:, without

reliance on provisions contained in the ACTION requirements."

During the time period from August 29, 1985, to January 8, 1987, the

plant entered Operational Condition 2 (Startup) on eleven occasions

(October 3, 1985, August 4, 1986, August 11, 1986, August 30, 1986,

September 6, 1986, October 3, 1986, October 7, 1986, October 14, 1986,

October 19, 1986, October 29, 1986, and December 19,1986) with both

divisions of hydrogen recombiner systems inoperable.

This is considered

a violation of Technical Specifications 3.0.4 (341/87006-03(DRP)).

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During the troubleshooting effort to repair the thermal recombiners,

several problems were encountered which caused concern as to the

reliability of the recombiners.

They are as follows:

Division I heater breaker would not close in on several occasions

due to sticky door interlock.

Division I silicon controlled rectifiers (SCRs) failed to fire.

Division I SCRs fired continuously"fied as broken.

Division I pin connector was identi

Division II solenoid contact did not close in allowing closure at

heater breaker motor.

In order to address these concerns, the licensee has embarked upon a

program to ensure reliability of the thermal recombiners.

This program

consists of performing reliability runs in addition to the six-montfi

Technical Specification surveillance requirements.

In these runs the

heaters will be energized to approximately 400 F to ensure reliability of

the heaters, blowers, cooling water, and electrical circuits.

These runs

will be performed:

for one month, and then (3) y other day for one week; (2) once per week

(1) everonce per month for six months.

If these runs

are determined to be successful, the surveillance frequency will be

returned to the six-month Technical Specification required frequency.

3.

Exit Interview (30703)

The inspectors met with licensee representatives (denoted in Paragraph 1)

on January 15, 1987, February 3, 1987, and informally throughout the

activities. period and summarized the scope and findings of the inspection

inspection

The inspectors also discussed the likely informational

content of the inspection report with regard to documents or processes

reviewed by the inspectors during the inspection.

The. licensee did not

identify any such documents / processes as pro

The licensee

acknowledged the findings of the inspection.prietary.

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