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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20234F2361987-06-26026 June 1987 Special Rept:Cardox Sys Inoperable for 26 Days Due to Failed Relay in Cable Vault Zone Discovered on 870519.Fire Watch Established.Replacement Relay Installed & Tested on 870611. Cardox Sys Functionally Tested on 870613 ML20214V7971986-09-0808 September 1986 Ro:On 860810,plant Tripped Due to Low Steam Generator Level Following Loss of Static Inverter.On 860811,dose Equivalent I-131 Activity Exceeded 1.0 Uci/G.Dose Equivalent Iodine Activity & Plant Operating Characteristics Encl ML20212C6381986-07-15015 July 1986 Ro:On 860612,plant Tripped When Excess Flow Check Valve Inadvertently Closed.Dose Equivalent Iodine (Dei) Activity Also Exceeded 1 Uci/G.Dei Activity & Plant Operating Characteristics Presented in Tables 1 & 2,respectively ML20198R3051986-05-20020 May 1986 Ro:On 860416,dose Equivalent I-131 Activity Exceeded 1.0 Uci/G & Remained Above Level All Day.Letdown Flow Increased Upon Reactor Shut Down in Order to Increase Coolant Cleanup & Reduce I-131 Level ML20210U8781986-05-14014 May 1986 Ro:On 860429,Mensor High Precision Quartz Manometer,Which Provides Containment Pressure Info to Plant Computer,Failed. Mensor Repaired & Returned to Svc.Alternate Calculations Will Continue ML20155A8591986-03-24024 March 1986 Ro:On 860222,dose Equivalent Iodine (I-131) Levels Exceeded 1 Uci/G for 7.5 H After Unit Shutdown on 860221 to Repair Hydrogen Leak in turbine-generator Unit.Peak Activity Spike 1.96 Was Uci/G.Cause Not Stated ML20126L7811981-06-0303 June 1981 Ro:On 810603,at Completion of Fuel Handling Activities & W/ Greater than 23 Ft of Water in Reactor Cavity,Svc Water Cooling to Secondary Component Coolers Interrupted for Approx 30 Minutes.No Significant Increase in Temp ML20126B4341980-01-30030 January 1980 RO 80-001/01T:during Review of Steam Line Break Analysis, Incorrect Assumption Utilized in Zero or Low Power Steam Line Break Analysis Discovered.Cause Unstated.Necessary Mods to Be Implemented Prior to Startup 1987-06-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20211M4841999-08-31031 August 1999 Replacement Pages 2-48,2-49 & 2-50 to Rev 14 of Defueled Sar ML20211D7111999-08-0909 August 1999 Rev 17 to Maine Yankee Defueled Safety Analysis Rept (Dsar) ML20196K4821999-07-0606 July 1999 Safety Evaluation Concluding That Because of Permanently Shutdown & Defueled Status of Myaps Facility,Confirmatory Orders No Longer Necessary for Safe Operation or Maint of Plant ML20206H1611999-05-0505 May 1999 Safety Evaluation Supporting Amend 164 to License DPR-36 ML20206G5731999-05-0303 May 1999 Safety Evaluation Supporting Amend 163 to License DPR-36 ML20205D5261999-03-26026 March 1999 SER Accepting Util Rev 1 to CFH Training & Retraining Program for Maine Yankee.Rev 1 to CFH Training & Retraining Program Consistent with Current Licensing Practice for Facilities Undergoing Decommissioning ML20204C4631999-03-16016 March 1999 Safety Evaluation Supporting Amend 162 to License DPR-36 ML20206D7491998-12-31031 December 1998 Co Annual Financial Rept for 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Yankee.W/ ML20141G6511997-05-19019 May 1997 Safety Evaluation Supporting Amend 158 to License DPR-36 ML20138G3541997-05-0202 May 1997 Safety Evaluation Supporting Amend 157 to License DPR-36 ML20141G2871997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Maine Yankee ML20137Z1971997-04-14014 April 1997 Forwards to Commission Results of Staff Evaluation of Performance of Licensees W/Ownership Structure Similar to Plant ML20137N7541997-03-31031 March 1997 Rev 11 to Operational Quality Assurance Program ML20138B1491997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Maine Yankee 1999-08-09
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MAIRE HARHEE ATOMIOPOWER00MPARUe ,vaugr,y,?n", o",lg6 (207) 623-3521 May 14, 1986 O MN-86-63 GDH-86-113 Region I United States Nuclear Regulatory Commission Office of Inspection and Enforcement 631 Park Avenue King of Prussia, Pennsylvania 19406 Attention: Dr. Thomas E. Murley, Regional Administrator
References:
(a) License No. DPR-36 (Docket No. 50-309)
(b) Maine Yankee Final Safety Analysis Report, Section 5.2.4
Subject:
Containment Height of Air Monitoring System Gentlemen:
Maine Yankee Atomic Power Company hereby submits the following report in accordance with Technical Specification 3.11.G.I.
At 0704 hours0.00815 days <br />0.196 hours <br />0.00116 weeks <br />2.67872e-4 months <br /> on Tuesday, April 29, 1986, the plant's Mensor high precision quartz manometer, which provides containment pressure information to ,
the plant computer, failed. The pressure input is utilized to calculate the l weight of air within the sealed containment, and the calculated value is j trended for an added measure of assurance of leak-tightness of the l containment. The containment's integrity is primarily assured by the I automatic isolation features and administrative controls in place generally . l for U.S. plants of this type. l Since discovery of the Mensor quartz manometer failure on April 30th, Operations Department personnel have been performing hand calculations of containment weight of air once per shift with pressure values obtained from a locally read barometer. Additionally, the wide range containment pressure i sensor has been substituted for the Mensor quartz manometer in the computer calculation. The results of the hand calculation and the revised computer calculation are both being used for trending in accordance with Technical Specification 3.11 in the same way the Mensor calculation is normally used.
The alternative calculations are not quite as accurate, however, giving day-to-day fluctuations in calculated air weight about two and one-half times the Mensor based daily fluctuations.
7573L-SEN < )_
8606100001 860514 . I PDR ADOCK 05000309 i g S PDR l l
j MAINE YANKEE ATOMIC POWER COMPANY United States Nuclear Regulatory Commission Page Two Attention: Dr. Thomas E. Murley, Regional Administrator MN-86-63 The necessary parts to repair the Mensor quartz manometer were received on May 7, 1986. The Mensor has been repaired, calibrated, and returned to service. Alternative calculations will continue, however, for ten days to ensure the Mensor is fully operational.
He trust this information is satisfactory. Please contact us should you have any questions regarding this matter.
Very truly yours, MAINE YANKEE ATOMIC POWER COMPANY
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G. D. Whittier, Manager Nuclear Engineering and Licensing GCH/bjp cc: Mr. Ashok C. Thadani Mr. Pat Sears Mr. Cornelius F. Holden We 7573L-SEN