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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARSNRC-2134, Proposed Amend 11 to License NPF-82,requesting Deletion of TS & Environ Protection Plan in Entirety1994-01-20020 January 1994 Proposed Amend 11 to License NPF-82,requesting Deletion of TS & Environ Protection Plan in Entirety ML20059K1141993-11-0404 November 1993 License Change Application 2 to License NPF-82,deleting App A,Ts,App B,Environ Protection Plan (non-radiological) & Revising Pol NPF-82,Amend 9 ML20125D4991992-12-14014 December 1992 License Change Application 1 for License NPF-82,changing Defueled TS to Delete Ac Sources & Onsite Power Distribution Sys Requirements & Change Frequency of Radiological Effluent Release Reporting Requirements SNRC-1900, Suppl to 920113 Application for Amend to License NPF-82, Authorizing Long Island Power Authority to Implement Decommissioning Plan.Suppl Consists of Revised NSHC Analysis1992-01-24024 January 1992 Suppl to 920113 Application for Amend to License NPF-82, Authorizing Long Island Power Authority to Implement Decommissioning Plan.Suppl Consists of Revised NSHC Analysis SNRC-1883, Application for Conforming Amend to License NPF-82, Authorizing Implementation of Util Decommissioning Plan Presently Pending Before NRC1992-01-13013 January 1992 Application for Conforming Amend to License NPF-82, Authorizing Implementation of Util Decommissioning Plan Presently Pending Before NRC SNRC-1857, Suppl to 900105 & 0628 Applications for Amend to License NPF-82,authorizing Transfer of OL from Lilco to Long Island Power Authority & Adopting NRC-approved Program to Certify Personnel Currently Licensed Under 10CFR551991-10-31031 October 1991 Suppl to 900105 & 0628 Applications for Amend to License NPF-82,authorizing Transfer of OL from Lilco to Long Island Power Authority & Adopting NRC-approved Program to Certify Personnel Currently Licensed Under 10CFR55 SNRC-1819, Suppl to 900628 Joint Application of Lilco & Long Island Power Authority for Amend to License NPF-82,reflecting Facility Defueled possession-only Status & Modifying Position Descriptions as Listed on Encl1991-06-27027 June 1991 Suppl to 900628 Joint Application of Lilco & Long Island Power Authority for Amend to License NPF-82,reflecting Facility Defueled possession-only Status & Modifying Position Descriptions as Listed on Encl SNRC-1813, Suppl to 900628 Application for Amend to License NPF-82, Authorizing Transfer of Facility from Lilco to Long Island Power Authority (Lipa),Consisting of Agreement Re Coemployment of New York Power Authority & Lipa Employees1991-06-13013 June 1991 Suppl to 900628 Application for Amend to License NPF-82, Authorizing Transfer of Facility from Lilco to Long Island Power Authority (Lipa),Consisting of Agreement Re Coemployment of New York Power Authority & Lipa Employees SNRC-1770, Application for Amend to License NPF-82,replacing Tech Spec Pages 3/4 4-1 & 3/4 4-3 of Proposed Defueled Tech Specs1990-10-30030 October 1990 Application for Amend to License NPF-82,replacing Tech Spec Pages 3/4 4-1 & 3/4 4-3 of Proposed Defueled Tech Specs SNRC-1740, Application for Amend to License NPF-82,revising Tech Specs Re Defueled SAR1990-08-10010 August 1990 Application for Amend to License NPF-82,revising Tech Specs Re Defueled SAR ML20044A3701990-06-28028 June 1990 Joint Application for Amend to License NPF-82,designating Long Island Power Authority as Plant Licensee Upon or After NRC Amending of License to Nonoperating Status ML20006F4701990-02-20020 February 1990 License Change Application 5,amending License NPF-82 by Revising Tech Specs to Incorporate Guidance in Generic Ltr 89-01 Re Implementation of Programmatic Controls for Radiological Effluent Tech Specs ML20005F2461990-01-0505 January 1990 Application for Amend to License NPF-82,creating Defueled Facility OL ML19332G1561989-12-15015 December 1989 Application for Amend to License NPF-82,ceasing Offsite Emergency Preparedness Activities & Implementing Emergency Preparedness Plan for Facility ML20246N9651989-07-14014 July 1989 Application for Amend to License NPF-82,consisting of Change Application 1,revising Tech Specs to Remove Inconsistency in Plant Procedural Change Approval Process ML20205D2771988-10-19019 October 1988 Application for Amend to License NPF-36,consisting of License Change 16,changing Tech Specs to Allow for Exercising Control Rods to Help Prevent Corrosion of CRD Mechanisms & to Provide for Various Functional Tests ML20151D7071988-07-15015 July 1988 Application for Amend to License NPF-36,reducing Test Frequency of Emergency Diesel Generators Per Recommendations of Generic Ltr 84-15 ML20151D7351988-07-11011 July 1988 Application for Amend to License NPF-36,consisting of License Change Application 13,clarifying Method of Demonstrating Operability of Source Range Monitor Channels ML20154M6231988-05-24024 May 1988 Application for Amend to License NPF-36,consisting of License Change Application 12,revising Tech Specs to Change Method for Determining Setpoint for Main Control Room Vent Radiation Monitors ML20154H1411988-05-19019 May 1988 Application for Amend to License NPF-36,consisting of License Change Application 11,to Provide Clarification of Tech Specs ML20236C4501987-10-14014 October 1987 Application for Amend to License NPF-36,consisting of License Change Application 10,correcting Typos,Tech Spec Internal Inconsistency & Designation of Number of Valves on Table 3.6.3-1 ML20238C3871987-09-0404 September 1987 License Change Application 9 for Amend to License NPF-36, Changing Definition of & Some Footnotes Referring to Core Alteration ML20209D2311987-04-24024 April 1987 Application for Amend to License NPF-36,modifying Certain Emergency Diesel Generator License Conditions to Form Basis for Qualification of Tdi Emergency Diesel Generators Over Entire Life of Plant.Supporting Documentation Encl ML20210C7231987-02-0404 February 1987 Application for Amend to License NPF-36,consisting of License Change Application 7,changing Discharge Pressure in Tech Spec Section 4.1.5c from 1,190 to 1,220 Psig for Standby Liquid Control Sys.W/Certificate of Svc ML20212J4571987-01-21021 January 1987 Application for Amend to License NPF-36,incorporating License Change Application 6 & Revising Tech Specs to Implement Design Change to Lower Reactor Vessel Water Level Setpoint of MSIVs & Steam Line Drain Valves ML20207P9191987-01-12012 January 1987 Application for Amend to License NPF-36,consisting of License Change Application 5,clarifying Location of Meterological Towers & Correcting Inconsistency in Organization Charts ML20206P2611986-06-26026 June 1986 License Change Application 4 to License NPF-36,correcting Error in Listing of Types of Radwaste Shipping Containers & Solidification Agents & Clarifying Review of Operations Committee Responsibilities ML20140A7941986-01-20020 January 1986 License Change Application 3 for Amend to License NPF-36, Eliminating Performance of Sampling Analysis If No Waste Batch Released During Month & Correcting Error in Basis for Location of Milk Control Sample ML20136B4251985-11-16016 November 1985 Application to Amend License NPF-36,consisting of License Change Application 2,increasing & Relocating Fire Detectors & Modifying Reactor Coolant Leakage Surveillance Requirement ML20138C8731985-10-21021 October 1985 Application for Amend to License NPF-36,consisting of Change Request 1,revising Tech Specs Re Conversion of Reactor Bldg Standby Ventilation Sys low-range Noble Gas Radiation Monitor to Vent Stack low-range Gas Radiation Monitor ML20127J2751985-06-19019 June 1985 Application for Amend to License NPF-19,changing Tech Spec 3.10.5 to Allow Suspension of Tech Spec 3.6.6.2 During Performance of Startup Test Program Until Reactor Has Operated 120 EFPD SNRC-1115, Application for Amend 52 to OL Application,Consisting of Rev 34 to FSAR1984-11-29029 November 1984 Application for Amend 52 to OL Application,Consisting of Rev 34 to FSAR SNRC-1085, Amend 51 to License Application,Consisting of Rev 3 to Fsar. One Oversize Figure Encl.Aperture Card Available in PDR1984-09-25025 September 1984 Amend 51 to License Application,Consisting of Rev 3 to Fsar. One Oversize Figure Encl.Aperture Card Available in PDR ML20082P8571983-12-0101 December 1983 Application for Amend 50 to OL Application,Consisting of Rev 32 to Fsar.W/Affidavit ML20024F0891983-09-0101 September 1983 Amend 49 to OL Application,Consisting of Rev 31 to FSAR ML20070N1611982-12-30030 December 1982 Application for Amend 46 to OL Application,Consisting of Rev 28 to Fsar.Affidavit Encl ML20052H7081982-05-10010 May 1982 Application for Amend 44 to CPPR-95,consisting of Revision 26 to Fsar.Affidavit Encl ML20073M1971982-04-12012 April 1982 Amend 47 to Application for OL Consisting of Rev 29 to Fsar. Rev Includes Changes to Correct Discrepancies Identified by Configuration Review Program for Specific Sys,Revised Steam Bypass Analysis & Scram Discharge Vol Mods ML20041B7641982-02-17017 February 1982 Application for Amend 43 to License Application,Consisting of Revision 25 to FSAR & Revision to Chapter 13 to Reflect Current QA Organization ML20010A3221981-08-0606 August 1981 Amend 40 to OL Application,Containing Revision 22 to Fsar.Revision Includes Revised Chapter 7,responses to NUREG-0737 & Minor Corrections/Clarifications.Affidavit Encl.W/O Revision 22 ML19345D4881980-12-0505 December 1980 Amend 38 to Application for Ol,Consisting of Revision 20 to FSAR ML19262C2061980-01-14014 January 1980 Amend 35 to Application for Ol,Updating Info Supplied Per 10CFR50.33 Requirements ML20235D0821969-04-18018 April 1969 Amend 4 to Application for Ol,Increasing Size of Reactor & Changing Estimated Costs for Const ML20235C8951968-06-18018 June 1968 Amend 1 to Application for Ol.Util Requests That Dates 721001 & 730501 Be Considered as Earliest & Latest Dates for Completion of Const of Facility 1994-01-20
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARSNRC-2134, Proposed Amend 11 to License NPF-82,requesting Deletion of TS & Environ Protection Plan in Entirety1994-01-20020 January 1994 Proposed Amend 11 to License NPF-82,requesting Deletion of TS & Environ Protection Plan in Entirety ML20059K1141993-11-0404 November 1993 License Change Application 2 to License NPF-82,deleting App A,Ts,App B,Environ Protection Plan (non-radiological) & Revising Pol NPF-82,Amend 9 ML20056C7171993-07-14014 July 1993 Amend 10 to License NPF-82,revising Defueled TS to Delete Requirement That Radioactive Effluent Release Rept Be Submitted on Semiannual Basis & Eliminating Requirements for Ac Sources & Onsite Power Distribution Sys ML20125D4991992-12-14014 December 1992 License Change Application 1 for License NPF-82,changing Defueled TS to Delete Ac Sources & Onsite Power Distribution Sys Requirements & Change Frequency of Radiological Effluent Release Reporting Requirements SNRC-1900, Suppl to 920113 Application for Amend to License NPF-82, Authorizing Long Island Power Authority to Implement Decommissioning Plan.Suppl Consists of Revised NSHC Analysis1992-01-24024 January 1992 Suppl to 920113 Application for Amend to License NPF-82, Authorizing Long Island Power Authority to Implement Decommissioning Plan.Suppl Consists of Revised NSHC Analysis SNRC-1883, Application for Conforming Amend to License NPF-82, Authorizing Implementation of Util Decommissioning Plan Presently Pending Before NRC1992-01-13013 January 1992 Application for Conforming Amend to License NPF-82, Authorizing Implementation of Util Decommissioning Plan Presently Pending Before NRC SNRC-1857, Suppl to 900105 & 0628 Applications for Amend to License NPF-82,authorizing Transfer of OL from Lilco to Long Island Power Authority & Adopting NRC-approved Program to Certify Personnel Currently Licensed Under 10CFR551991-10-31031 October 1991 Suppl to 900105 & 0628 Applications for Amend to License NPF-82,authorizing Transfer of OL from Lilco to Long Island Power Authority & Adopting NRC-approved Program to Certify Personnel Currently Licensed Under 10CFR55 SNRC-1819, Suppl to 900628 Joint Application of Lilco & Long Island Power Authority for Amend to License NPF-82,reflecting Facility Defueled possession-only Status & Modifying Position Descriptions as Listed on Encl1991-06-27027 June 1991 Suppl to 900628 Joint Application of Lilco & Long Island Power Authority for Amend to License NPF-82,reflecting Facility Defueled possession-only Status & Modifying Position Descriptions as Listed on Encl SNRC-1813, Suppl to 900628 Application for Amend to License NPF-82, Authorizing Transfer of Facility from Lilco to Long Island Power Authority (Lipa),Consisting of Agreement Re Coemployment of New York Power Authority & Lipa Employees1991-06-13013 June 1991 Suppl to 900628 Application for Amend to License NPF-82, Authorizing Transfer of Facility from Lilco to Long Island Power Authority (Lipa),Consisting of Agreement Re Coemployment of New York Power Authority & Lipa Employees SNRC-1770, Application for Amend to License NPF-82,replacing Tech Spec Pages 3/4 4-1 & 3/4 4-3 of Proposed Defueled Tech Specs1990-10-30030 October 1990 Application for Amend to License NPF-82,replacing Tech Spec Pages 3/4 4-1 & 3/4 4-3 of Proposed Defueled Tech Specs SNRC-1740, Application for Amend to License NPF-82,revising Tech Specs Re Defueled SAR1990-08-10010 August 1990 Application for Amend to License NPF-82,revising Tech Specs Re Defueled SAR ML20056A1991990-07-31031 July 1990 Amend 6 to License NPF-82,allowing Licensee to Cease Offsite Emergency Preparedness Activities ML20044A3701990-06-28028 June 1990 Joint Application for Amend to License NPF-82,designating Long Island Power Authority as Plant Licensee Upon or After NRC Amending of License to Nonoperating Status ML20055E3871990-06-25025 June 1990 Amend 5 to License NPF-82,changing Administrative Section of Tech Specs & Moving Procedural Details Re Radioactive Effluent Monitoring Instrumentation,Equipment Requirements & Control of Liquid & Gaseous Effluents to ODCM ML20006F4701990-02-20020 February 1990 License Change Application 5,amending License NPF-82 by Revising Tech Specs to Incorporate Guidance in Generic Ltr 89-01 Re Implementation of Programmatic Controls for Radiological Effluent Tech Specs ML20005F2461990-01-0505 January 1990 Application for Amend to License NPF-82,creating Defueled Facility OL ML19332G1561989-12-15015 December 1989 Application for Amend to License NPF-82,ceasing Offsite Emergency Preparedness Activities & Implementing Emergency Preparedness Plan for Facility ML20246N9651989-07-14014 July 1989 Application for Amend to License NPF-82,consisting of Change Application 1,revising Tech Specs to Remove Inconsistency in Plant Procedural Change Approval Process ML20245B8901989-04-21021 April 1989 License NPF-82,authorizing Operation of Core Levels Not to Exceed 2,436 Mwt ML20196E5781988-11-30030 November 1988 Amend 10 to License NPF-36,changing Definition of Core Alteration in Tech Specs to Include Certain Exceptions & Footnotes in Tech Specs to Be Consistent W/New Definition ML20196B6711988-11-30030 November 1988 Amend 9 to License NPF-36,revising Attachment 3 to Plant License Re Maint & Surveillance Program for Tdi Diesel Generators ML20205D2771988-10-19019 October 1988 Application for Amend to License NPF-36,consisting of License Change 16,changing Tech Specs to Allow for Exercising Control Rods to Help Prevent Corrosion of CRD Mechanisms & to Provide for Various Functional Tests ML20151D7071988-07-15015 July 1988 Application for Amend to License NPF-36,reducing Test Frequency of Emergency Diesel Generators Per Recommendations of Generic Ltr 84-15 ML20151D7351988-07-11011 July 1988 Application for Amend to License NPF-36,consisting of License Change Application 13,clarifying Method of Demonstrating Operability of Source Range Monitor Channels ML20154M6231988-05-24024 May 1988 Application for Amend to License NPF-36,consisting of License Change Application 12,revising Tech Specs to Change Method for Determining Setpoint for Main Control Room Vent Radiation Monitors ML20154H1411988-05-19019 May 1988 Application for Amend to License NPF-36,consisting of License Change Application 11,to Provide Clarification of Tech Specs ML20236F6741987-10-19019 October 1987 Amend 8 to License NPF-36,changing Tech Specs Re Location of Two Meteorological Towers ML20236C4501987-10-14014 October 1987 Application for Amend to License NPF-36,consisting of License Change Application 10,correcting Typos,Tech Spec Internal Inconsistency & Designation of Number of Valves on Table 3.6.3-1 ML20238C3871987-09-0404 September 1987 License Change Application 9 for Amend to License NPF-36, Changing Definition of & Some Footnotes Referring to Core Alteration ML20237L3231987-08-31031 August 1987 Corrected Pages 3/4 3-81,3/4 3-81a,3/4 3-83 & 3/4 3-84 of Amend 7 to License NPF-36 Re Fire Detection Instrumentation Limiting Condition for Operation & Radioactive Liquid Effluent Monitoring Instrumentation ML20237G4601987-08-14014 August 1987 Amend 7 to License NPF-36,changing Footnote of Surveillance Requirement 4.4.3.1.c on RCS Leakage Detection Sys & Tech Spec Section 3.3.7.9 on Fire Detection Instrumentation ML20214K3881987-05-18018 May 1987 Amend 6 to License NPF-36,revising Tech Specs to Reflect Util Plan to Enrich Boron in Standby Liquid Control Sys to 85 Atom Percent B-10 Per 10CFR50.62(c)(4) ML20215M3981987-05-0404 May 1987 Amend 5 to License NPF-36,revising Tech Specs to Change Reactor Vessel Water Level Setpoint for Closure of Main Steam Isolation & Line Drain Valves from Level 2 to Lower Level of Level 1 ML20209D2311987-04-24024 April 1987 Application for Amend to License NPF-36,modifying Certain Emergency Diesel Generator License Conditions to Form Basis for Qualification of Tdi Emergency Diesel Generators Over Entire Life of Plant.Supporting Documentation Encl ML20210C7231987-02-0404 February 1987 Application for Amend to License NPF-36,consisting of License Change Application 7,changing Discharge Pressure in Tech Spec Section 4.1.5c from 1,190 to 1,220 Psig for Standby Liquid Control Sys.W/Certificate of Svc ML20212J4571987-01-21021 January 1987 Application for Amend to License NPF-36,incorporating License Change Application 6 & Revising Tech Specs to Implement Design Change to Lower Reactor Vessel Water Level Setpoint of MSIVs & Steam Line Drain Valves ML20207P9191987-01-12012 January 1987 Application for Amend to License NPF-36,consisting of License Change Application 5,clarifying Location of Meterological Towers & Correcting Inconsistency in Organization Charts ML20211N5831986-12-0909 December 1986 Amend 4 to License NPF-36,revising Tech Specs to Eliminate Need for Performing Monthly Sampling & Analysis for Dissolved & Entrained Gases If No Waste Batch of Liquid Effluents Released During Month ML20213D4971986-11-0303 November 1986 Amend 3 to License NPF-36,correcting Internal Inconsistency in Tech Specs Re Process Control Program for Radwaste Shipping Containers & Solidification Agents ML20206P2611986-06-26026 June 1986 License Change Application 4 to License NPF-36,correcting Error in Listing of Types of Radwaste Shipping Containers & Solidification Agents & Clarifying Review of Operations Committee Responsibilities ML20154L9641986-03-0404 March 1986 Amend 2 to License NPF-36,revising Tech Specs to Reflect Conversion of One of Two Low Range Reactor Bldg Standby Vent Sys Noble Gas Radiation Monitors to Low Range Plant Vent Stack Noble Gas Radiation Monitor ML20140A7941986-01-20020 January 1986 License Change Application 3 for Amend to License NPF-36, Eliminating Performance of Sampling Analysis If No Waste Batch Released During Month & Correcting Error in Basis for Location of Milk Control Sample ML20138N6501985-12-0606 December 1985 Amend 1 to License NPF-36,extending Deadline for Completion of Environ Qualification of Electrical Equipment Until 851231 ML20136B4251985-11-16016 November 1985 Application to Amend License NPF-36,consisting of License Change Application 2,increasing & Relocating Fire Detectors & Modifying Reactor Coolant Leakage Surveillance Requirement ML20138C8731985-10-21021 October 1985 Application for Amend to License NPF-36,consisting of Change Request 1,revising Tech Specs Re Conversion of Reactor Bldg Standby Ventilation Sys low-range Noble Gas Radiation Monitor to Vent Stack low-range Gas Radiation Monitor ML20132G7631985-07-0303 July 1985 License NPF-36 for Facility ML20127J2751985-06-19019 June 1985 Application for Amend to License NPF-19,changing Tech Spec 3.10.5 to Allow Suspension of Tech Spec 3.6.6.2 During Performance of Startup Test Program Until Reactor Has Operated 120 EFPD SNRC-1115, Application for Amend 52 to OL Application,Consisting of Rev 34 to FSAR1984-11-29029 November 1984 Application for Amend 52 to OL Application,Consisting of Rev 34 to FSAR SNRC-1113, Application for Amend to CPPR-95,extending Const Completion Date from 841231 to 850330,due to Litigation on Tdi Emergency Diesel Generator.Decision Expected in Early 19851984-11-26026 November 1984 Application for Amend to CPPR-95,extending Const Completion Date from 841231 to 850330,due to Litigation on Tdi Emergency Diesel Generator.Decision Expected in Early 1985 SNRC-1085, Amend 51 to License Application,Consisting of Rev 3 to Fsar. One Oversize Figure Encl.Aperture Card Available in PDR1984-09-25025 September 1984 Amend 51 to License Application,Consisting of Rev 3 to Fsar. One Oversize Figure Encl.Aperture Card Available in PDR 1994-01-20
[Table view] |
Text
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LONG ISLAND LIGHTING COMPANY Operating License NPF-36 Docket 50-322 License Change Application 7 This License Change Application requests modification to Operating License NPF-36 for the Shoreham Nuclear Power Station to achieve consistency with the anticipated physical condition of the plant. LILCO plans to implement a design change that will equip Shoreham's Standby Liquid Control _ System with slightly more than twice the " equivalent control capacity" required by 10 CFR 50.62 (c) (4) . This will be accomplished by the use of eighty-five (85) atom percent Boron-10 enriched sodium pentaborate, a minimum injection rate of 41.2 gpm, and a proposed concentration range of 9.8 to 12.0 percent.
An in-plant test of the Standby Liquid Control System was performed September 1986 to determine the feasibility of meeting the requirements of the above mentioned rule with two pump operation. Based upon the results of this test and a subsequent calculation, LILCO proposes to change the discharge pressure in Section 4.1.5c from 1190 psig to 1220 psig.
These requests and supporting documentation are contained in the Attachment to this License Change Application.
Long Island Lighting Company By . ( M John' D. Leonard, Jr.
Vice President - Nucle O .erations Subscribed and sworn to before me this ^/db day of February 1987.
4 UtiDA A. CPATTY f-rdOTARY PU UC S f b Ysk Notarp Public of NeW York nam, a s e a may co.vm , tgm ua .31 inf My Commission Expires: fla rck M, l 7 PY 2
NO P
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UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION In the Matter of
)
Long Island Lighting Company ) Docket No. 50-322
)
)
SHOREHAM NUCLEAR POWER STATION - UNIT 1 CERTIFICATE OF SERVICE I hereby certify that copies of License Change Application 7 to the Operating License for Shoreham Nuclear Power Station - Unit 1, dated February # , 1987, have been served on the following by hand delivery or by deposit in the United States mail, first class, this day of February 1987:
Mr. Jay Dunkleberger New York State Energy Office 2 Rockefeller Plaza Albany, New York 12223 L. F. Britt, Manager Nuclear Licensing and Regulatory Affairs Subscribed and sworn to before me this N day of February 1987.
LINDA A. CRATTY fiOT/JiY PU UC S f Nc4 Ye k Quaws m w t -, - _'
ccm e Emueeantr Notary Public. of /New York My Commission Expires Ph nk 30 (17
Attachment To License Change Application 7
1.0 DESCRIPTION
OF CHANGE Shoreham Technical Specification 4.1.5 and Figure 3.1.5-2 will require the proposed changes as identified in Exhibits A through C. Upon implementation, these changes will provide reasonable assurance that Shoreham's Standby Liquid Control System has slightly more than double the equivalent control capacity required by 10 CFR 50.62 (c) (4) .
In addition, Technical Specification bases section 3/4.1.5 requires revision as identified in Exhibit D.
2.0 REASON FOR CHANGE LILCO letter SNRC-1205, dated October 10, 1985, stated that two pump injection was the preferred method of compliance with 10 CFR 50.62 (c) (4) , subject to the results of a test.
The two pump injection test was performed in September 1986 under cold shutdown conditions, and, as subsequently described in this section, the results of the test showed that two pump operation would not be viable for compliance with the rule. Hence, another method of compliance had to be selected. For Shoreham, boron enrichment was chosen.
In order to satisfy the equivalent control capacity require-ments of 10 CFR 50.62, the Shoreham 218 inch (internal diameter) reactor pressure vessel would require a boron-10 sodium pentaborate enrichment of approximately forty (40) atom percent. As part of the effort to find a suitable alternative to two pump operation, a study was performed to determine the effect of greater sodium pentaborate enrich-ments on the magnitude of the ATWS core melt frequency estimate as presented in the Shoreham Probabilistic Risk Assessment which was submitted by letter dated June 24, 1983.
As expected, tne higher enrichments allow additional time for Standby Liquid Control initiation because less time is required for injection of the amount (weight) of sodium pentaborate necessary to achieve a hot shutdown condition.
This results in a decrease in the human error probability estimate for Standby Liquid Control System injection and to a lesser extent, a reduction in the ATWS core melt frequency.
After the Standby Liquid Control System (SLCS) two-pump test yielded higher than anticipated discharge line losses, the derivation of the pump discharge surveillance pressure was reviewed. The actual two-pump test results were analytically manipulated to develop a calculated discharge line pressure drop for one-pump operation (at 43 gpm). The maximum pump discharge pressure (for one-pump operation) is the sum total
i
. 1
- 1
. 1 l
of the discharge line losses plus the maximum vessel injection pressure. These maximum values are assumed to i occur during a postulated full power ATWS with MSIV closure.
The maximum vessel pressure is the sum of the lowest setpoint of Safety Relief Valves (SRVs) (1115 psig) and the pressure due to the head of the water in the reactor vessel. The derivation of the pressure at the SLCS sparger based on the lowest SRV setpoint and a water filled reactor vessel is a conservative calculation. The calculation has recommended a Standby Liquid Control System pump discharge surveillance pressure of 1220 psig.
3.0 BASIS FOR NO SIGNIFICANT HAZARDS FINDING The proposed changes to the Standby Liquid Control System do not involve a significant hazards consideration because operation of the Shoreham Nuclear Power Station Unit 1, in accordance with this change, would not:
(1) involve a significant increase in the probability or consequences of an accident previously evaluated. The probability of an accident previously evaluated in the Shoreham Updated Safety Analysis Report (USAR) will not be increased as the use of 85 atom percent boron-10 enriched sodium pentaborate is chemically the same as natural pentaborate and does not have any effect on these accident initiators. The consequences of any accident previously evaluated in the FSAR will not be increased, based on a review of the Chapter 15 and Chapter 3 analyses. The use of the Standby Liquid Control System as a diverse means to shutdown the reactor is discussed in USAR Section 15.1.27,
" Anticipated Transients Without Scram." This section states that up to 10 minutes are available to initiate SLC system. As discussed in NEDO-10349, the offsite radiological dose consequences calculated for this event are within the 10 CFR 100 dose limits. The analysis assumes the use of natural pentaborate (twenty atom percent B-10).
The use of eighty-five atom percent B-10 enriched sodium pentaborate at the minimum technical specification required flow rate of 41.2 injection rate will reduce the time required to bring the reactor to hot shutdown by approximately a factor of four. This will allow increased time for operator action and result in a higher probability that the SLC system will be initiated in a timely manner. Additionally, the use of enriched pentaborate does not require substantial modification of the SLC system. Pump redundancy will be maintained.
The SLC tank level instrumentation setpoints will be reset to accommodate the smaller liquid poison volume associated with the use of eighty-five percent enriched pentaborate. The new setpoints will account for instru- i ment accuracy to ensure that the required quantity of pentaborate is injected into the vessel.
4 9
Although this request will also result in an increase in the pump discharge surveillance pressure of the system, it is still well below the system design pressure and the relief valve setpoint. The capability of the relief valve to prevent system overpressure and maintain system integrity remains intact. The margin between the relief valve setpoint and the proposed pump discharge surveillance pressure is sufficient to prevent flow diversion through the relief valves, which will be verified during the pump surveillance.
Additionally, the change in system pressure does not change the system classification. The system remains moderate energy due to the limited time the SLC discharge piping is pressurized. Since the moderate energy analysis still remains valid, a significant increase in the probability and consequences of pipe break accidents, as previously evaluated for Shoreham, is precluded. The proposed SLC pump surveillance pressure increase will ensure vessel injection at sufficient flow rates for anticipated ATWS conditions.
Therefore, this change does not compromise the safety of the plant.
(2) create the possibility of an accident that is different than any already evaluated in the USAR. The use of highly enriched pentaborate will not cause core power oscillations even with the assumption of no core flow during SLC injection. Based on the results of tests conducted in the Vallecitos Nuclear Center 1/6 Scale 3D Boron Mixing Test Facility as applied to the specific conditions of Shoreham, General Electric concluded that the dispersion of the boron following the restart of core flow is gradual enough that there is no danger of maldistribution of the boron in the water in the vessel.
The SLC system provides a diverse means of a reactor shutdown. It is an accident mitigator and the change in pump discharge pressure will not cause the SLC system to initiate any type of accident or malfunction not previously evaluated. The higher pressure will not cause any adverse conditions greater than those caused by the ATWS, nor will the surveillance itself cause any adverse conditions since a sufficient relief valve margin is maintained and the piping design pressure is not exceeded.
(3) involve a significant reduction in the margin of safety as defined in the bases to Technical Specification 3/4.1.5. The present bases primarily discusses the
-l technical issues associated with the shutdown require-ment. The enriched pentaborate net tank volume and i concentration ranges have been specified to adhere to the shutdown basis. The use of enriched pentaborate will increase the margin of safety associated with the injection rate. The ATWS Rule requires an injection rate-equivalent in control capacity to 86 gpm of natural pentaborate based on a 251 inch internal diameter vessel. The proposed SNPS Technical Specification will ensure an injection capacity.that is 200% of this requirement based on Shoreham's 218 inch internal diameter reactor pressure vessel.
The increased pump discharge surveillance pressure will still allow sufficient relief valve setpoint margin to ensure a minimum pentaborate injection rate of 41.2 gpm to the reactor under ATWS conditions. Since the relief
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valve setpoint will not be readjusted outside the present range of 1340 + 60 psig, the system design pressure will not be exceeded. The proposed increase in the SLC pump discharge surveillance pressure maintains the margin of safety by requiring a technical specification flow rate verification at a pressure that is more representative of what the system could experience during an ATWS. 1 CONCLUSION The proposed Technical Specification change to allow the use of eighty-five atom percent boron-10 enriched sodium penta-borate in the SLC tank at a concentration range of 9.8-12.0 percent does not increase the probability of an accident, nor does it cause a reduction in any safety margin. The enriched boron option was specified as part of LILCO's ATWS compliance program. A study indicated an ATWS core melt frequency reduction of a factor of 5 was associated with the use of highly enriched sodium pentaborate in comparison to the present SLC system configuration (natural pentaborate). As stated above, the use of highly enriched sodium pentaborate will not result in core power oscillations, even with the i assumption of zero core flow during SLC injection. l The reduction of the concentration range was motivated by a desire to reduce the probability of equipment failures caused by pentaborate crystallization. The revised minimum required solution temperature reflects the lower saturation temper-ature associated with a maximum concentration of 12.0 percent.
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The Commission has provided guidance concerning the appli-cation of standards for determining whether a significant hazards consideration exists by providing certain examples (48 FR 14870) of amendments that are considered not likely to involve significant hazards consideration. Example (ii) relates to a change that constitutes an additional limi-tation, restriction or control not presently included in the technical specifications: for example, a more stringent surveillance requirement. Example (vii) relates to a change to make a license conform to changes in the regulations.
In this case, the proposed changes described above are similar to both Example (ii) and Example (vii). First, the proposed change is needed for compliance with a change in the regulations (i.e., 10 CFR 50.62 (c) (4)) . Second, as stated above, the proposed changes constitute a more stringent surveillance requirement than that required by the rule since compliance with the rule can be accomplished with an enrichment of approximately forty atom percent boron-10 enriched sodium pentaborate.
Therefore, based upon the above considerations and analyses, LILCO has determined that this proposed change does not involve a significant hazards consideration.
4.0 TIMING OF CHANGE Since this proposed technical specification change will require extensive numbers of station procedure changes and operator training, LILCO requests that it become effective upon implementation of modification and operator training.