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Category:ANNUAL OPERATING REPORT
MONTHYEARML18039A2581997-12-31031 December 1997 Bfnp Annual Operating Rept for 970101-1231. ML18038B6301995-12-31031 December 1995 Annual Operating Rept Jan-Dec 1995. W/960228 Ltr ML18038B1541994-12-31031 December 1994 Annual Operating Rept Jan-Dec 1994. ML18037A7721993-12-31031 December 1993 Annual Operating Rept Jan-Dec 1993. ML18036B1731992-12-31031 December 1992 Annual Operating Rept for 1992. ML20094G9601991-12-31031 December 1991 Annual Operating Rept Browns Ferry Nuclear Plant Jan-Dec 1991 ML18033B6481990-12-31031 December 1990 Annual Operating Rept for Browns Ferry Nuclear Plant for 1990. W/910301 Ltr ML20043A2121989-12-31031 December 1989 Annual Operating Rept for Browns Ferry Nuclear Plant for 1989. W/900314 Ltr ML20247F9281988-12-31031 December 1988 Annual Operating Rept to NRC,1988 ML20151A8371987-12-31031 December 1987 Annual Operating Rept to NRC,870101-1231 ML18032A6871987-12-29029 December 1987 Supplemental Annual Operating Rept for 1986 Re Herbicide Usage.No Herbicides Used on Any Transmission Line right-of- Ways in CY86 ML20235M5331986-12-31031 December 1986 Annual Operating Rept,Browns Ferry Nuclear Plant 860101-1231 ML20210C2351985-12-31031 December 1985 Supplemental Annual Operating Rept,New Procedures & Procedure Changes,Browns Ferry Nuclear Plant,1985 ML20137X9561985-12-31031 December 1985 Annual Operating Rept,Browns Ferry Nuclear Plant,Jan-Dec 1985 ML20077M3901983-02-28028 February 1983 Annual Operating Rept,1982 ML18025B3611981-02-27027 February 1981 Annual Operating Rept,1980. ML20003B6561981-02-19019 February 1981 Supplemental Annual Operating Rept,Browns Ferry Nuclear Plant,1979. Includes Stear Summary ML19296C5691979-12-31031 December 1979 Annual Operating Rept,1979. ML19282A7881979-02-28028 February 1979 Annual Operating Rept for 1978. 1997-12-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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6 W
, ENCLOSURE l SUPPLEMENTAL ANNUAL OPERATINC REPORT NEW PROCEDURES AND PROCEDURE CHANCES
, BROWNS FERRY NUCLEAR PLANT (BFN)
~ JANUARY 1, 1985'- DECEMBER 31, 1985
- During 1985, various procedures as described in the Safety Analysis Report (SAR) were drafted or revised. These changes were reviewed against 10 CFR
- 50.59, and no procedures were initiated that constituted an unreviewed. safety question (USQ). A brief description and safety evaluation summary is~given
~
for the following procedures which affected details of the SAR.
I. -Procedure Change. 0I-32. Control Air
~
A. Description of Activity - Revise OI-32 for units 1 & 2 to change valve position of HCV-32-576C, HCV-32-577C, and HCV-32-2385 from closed ~to open for normal operation. These valves allow bypass flow around FCV-32-29 -28, & -91, respectively.
B. References - TVA Drawings 47W847-6 & 47W847-7, OI-32, FSAR sections 10.14 (Control Air) & 5.3 (Secondary Containment),-technical specification section 4.7.c.
C. Reason for Activity - Malfunctioning of Air-operated Control Air Isolation Valves (FCV-32-29, -28, & -91) causes loss of control air to reactor building. This change will allow for uninterrupted control air supply.
D. Unreviewed Safety Question Determination
- 1. Is the probability of occurrence.or the consequences of an accident or malfunction of equipment import' ant to safety previously evaluated on the Safety Analysis Report increased?
Yes No X Leaving these valves open will not allow for secondary containment isolation in the event of a control air line break.
However, these control air lines are not of sufficient flow area to compromise secondary containment integrity as shown by a I separate analysis.
- 2. Is the possibility for an accident or malfunction of a different
! type than any evaluated previously in the Eafety Analysis Report
! created? I l Yes No X -
8705060122 T7050i PDR R
ADOCK 59 PDR ,
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This change will affect secondary containment only, and this' effect has been analyzed.
l- 3. Is the margin of safety as defined in the basis for any-g Technical Specification reduced?
Yes No X i- ' Standby Gas Treatment' System will still be-capable of.
maintaining the Reactor Building at -1/4 inch water gauge. vacuum' with less than 12,000 cfm total leakage.
II. procedure Chanze SI4.7.B (now 4.7.B.1. 4.7.B.7.'and 4.7.B.10). Standby i . Gas Treatment System ~(SGTS) '
t l- . .-
- 1. 1 1. . Description of Activity ,
4-s- . -
Removal of requirement for SGTS charcoal filter heaters. -
4 B. References i
Nemorandum from N. R. Beasley to G. R. Hall on Standby Gas Treatment System: charcoal filter heaters.
C. Reason for Activity i
Heaters are to be permanently removed from SGTS design. This is a temporary measure until DCR and technical specification change can be processed.
- D. Unreviewed Safety Ouestion Determination a
- 1. Is the probability of an occurrence or the consequences of an 4
accident or malfunction of equipment important to safety previcusly evaluated on the Safety Analysis Report increased?
Yes r- X
-t Co:.sistent with paragraph 3.4.d of Regulatory Guide 1.62 R1-1978 !
- and paragraph 2.2.3 of ERDA 76-2, each train is operated 10 i
hours per month to control moisture buildup on the absorber bed (technical specification 4.7.2.d). This is sufficient to ensure-
- moisture will not accumulate on charcoal filters; and, therefore, there is no increase in probability or consequences j of an accident previously analyzed.
- 2. Is the possibility for an accident or malfunction of a different A
type than any evaluated previously in the Safety Analysis Report created?
Yes No X I
s 4
i
A Since they will effectively no longer exist,~ charcoal filter heaters will not increase the probability of any unanalyzed accident.
- 3. Is the margin of safety as defined in the basis for any Technical specification reduced?
Yes No X This alteration will not affect the operability of any SGTS trains, so that the safety margin will not be reduced. _
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, ~ ,, E TENNESSEE VALLEY: AUTHORITY.. -
CHATTANOOGA. TENNESSEE 374o1 SE 157' Lookout ~ Place MAY 011987 10 CFR 50.59 U.S. Nuclear Regulatory Cosunission ATTN: -Document Control Desk
- Washington, D.C. 20555
. Gentlemen:
In the Matter of ) Docket Nos. 50-259 Tennessee: Valley Authority _) 50-260-50-296 BROWNS FERRY NUCLEAR PLANT - SUPPLEMENTAL ANNUAL OPERATING REPORT -
JANUARY 1.-1985, TO DECEMBER 31, 1985, BROWNS FERRY NUCLEAR PLANT UNITS 1, 2, AND 3 . DOCKETS NOS 50-259, 50-260, 50-296 - OPERATING LICENSES DPR-33, DPR-52, AND DPR-68 Pursuant to 10 CFR 50.59, the enclosed supplement to the annual; operating report for Browns Ferry units 1, 2, and 3 is. submitted.to report changes to procedures as described in the Final Safety Analysis Report.
Very truly yours, TENNESSEE VALLEY AUTHORITY
, I-R.Grdiey,.Dir]ctor Nuclear Safety innd Licensing .
Enclosure cc (Enclosure):
Mr. G. G. Zech, Assistant Director Regional Inspections Division of TVA Projects Office of Special Projects U.S. Nuclear Regulatory Conunission Region II 101 Marietta St., NW, Suite 2900 Atlanta, Georgia 30323 Browns Ferry Resident Inspector Browns Ferry Nuclear Plant P.O. Box 311 Athens, Alabama 35611 fcA1 F *[
sl{
l An Equal Opportunity Employer
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