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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20198K6611998-12-24024 December 1998 Safety Evaluation Supporting Amend 120 to License DPR-6 ML20154E0371998-09-30030 September 1998 Safety Evaluation Accepting Request for Exemption from Certain Portions of 10CFR50.47(b) & App E to 10CFR50 to Allow Brpnp to Discontinue Offsite EP Activities & Reduce Scope of Onsite EP as Result of Permanently Shutdown ML20154E0581998-09-30030 September 1998 Safety Evaluation Accepting Licensee Request from Exemption from Certain Portions of 10CFR50.47(b) ML20198K0091998-09-18018 September 1998 SER Accepting Licensee Request for Exemption from Certain 10CFR50 Requirements for Emergency Planning for Big Rock Nuclear Plant ML20216K0011998-04-16016 April 1998 Safety Evaluation Approving Licensee Request Re Plant Training Program for Certified Fuel Handlers ML20141J8731997-08-14014 August 1997 Safety Evaluation Supporting Amend 119 to License DPR-6 ML20137X0161997-04-18018 April 1997 Safety Evaluation Accepting Changes to Rev 17 of CPC Quality Program Description for Operational NPPs (CPC-2A) ML20137J9381997-04-0202 April 1997 Safety Evaluation Supporting Amend 118 to License DPR-6 ML20058F3441993-11-22022 November 1993 Safety Evaluation Concurring W/Contractor Findings Presented in Technical Evaluation Rept EGG-RTAP-10816, Evaluation of Utility Responses to Suppl 1 to NRC Bulletin 90-01;Big Rock Point ML20058A1601993-11-15015 November 1993 Safety Evaluation Supporting Amend 112 to License DPR-6 ML20057E1981993-10-0505 October 1993 Safety Evaluation Supporting Amend 111 to License DPR-6 ML20056E1661993-08-16016 August 1993 Safety Evaluation Supporting Amend 110 to License DPR-6 ML20128C9621992-11-27027 November 1992 Safety Evaluation Accepting Response to Suppl 1 to GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Usi A-46 ML20059H6051990-09-11011 September 1990 Safety Evaluation Approving Util 891229 Application for Disposal of Discharge Canal Dredging Spoils at Site ML20059F2581990-08-31031 August 1990 Safety Evaluation Approving Licensee Proposal to Dispose of Discharge Canal Dredgings Onsite in Manner Described in Util ML20012E4281990-03-16016 March 1990 Safety Evaluation Supporting Amend 102 to License DPR-6 ML20246D2391989-08-16016 August 1989 Safety Evaluation Supporting Amend 100 to License DPR-6 ML20245G5211989-08-10010 August 1989 SER Accepting Util Response to Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability for All Domestic Operating Reactors ML20245H8421989-07-28028 July 1989 Safety Evaluation Supporting Amend 98 to License DPR-06 ML20248C0621989-05-31031 May 1989 Safety Evaluation Supporting Amend 97 to License DPR-6 ML20246L8251989-05-0202 May 1989 Safety Evaluation Supporting Amend 96 to License DPR-6 ML20245F8391989-04-14014 April 1989 Safety Evaluation Supporting Amend 95 to License DPR-6 ML20235J0251989-02-15015 February 1989 Safety Evaluation Supporting Amend 94 to License DPR-6 ML20205T5911988-11-0404 November 1988 Safety Evaluation Supporting Requested Relief from Inservice Testing Requirements ML20205S1271988-10-14014 October 1988 Safety Evaluation Supporting Amend 93 to License DPR-6 ML20154G1131988-09-14014 September 1988 Safety Evaluation Supporting Amend 92 to License DPR-6 ML20154C1381988-09-0707 September 1988 Revised Safety Evaluation Accepting Continued Use of Hafnium Hybrid Control Blade & Proposed Surveillance Program ML20155F3511988-06-0606 June 1988 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 2.1 (Part 1), Equipment Classification ML20154J1981988-05-17017 May 1988 Safety Evaluation Supporting Amend 91 to License DPR-6 ML20154H5341988-05-17017 May 1988 Safety Evaluation Supporting Amend 90 to License DPR-6 ML20154H4051988-05-17017 May 1988 Safety Evaluation Supporting Continued Use of Present Six Nucom Rods,Insertion of Two Similar Rods for Cycle 23 & Use of Surveillance Program ML20211P1411987-02-19019 February 1987 Safety Evaluation Supporting Issuance of Amend 89 to License DPR-6 ML20211N5401987-02-17017 February 1987 Safety Evaluation Supporting Issuance of Amend 88 to License DPR-6 ML20207S1681987-02-12012 February 1987 Safety Evaluation Concluding That Portions of Util 861205 Application to Amend License DPR-6,revising Tech Spec Section 5.2.1,Tables 1 & 2 Re Defining Operating Limits for New Reload I-2 Fuel Unacceptable ML20209H0651987-01-28028 January 1987 Safety Evaluation Supporting Amend 87 to License DPR-6 ML20212L9441987-01-16016 January 1987 Safety Evaluation Supporting Original Exemption from 10CFR50,App R Requirements Re Oil Collection Sys to Be Installed on Recirculation Pumps ML20198A3911986-05-12012 May 1986 Safety Evaluation Supporting Amend 85 to License DPR-6 ML20210P1761986-05-0606 May 1986 Safety Evaluation Supporting Amend 84 to License DPR-6 ML20155D7161986-04-11011 April 1986 Safety Evaluation Supporting Util 840730 Proposed Amend to License DPR-6,changing Tech Specs to Add Definition for Reportable Event & to Delete Specific Reporting Requirements Included in 10CFR50.72 & 50.73 ML20141N6571986-03-10010 March 1986 Safety Evaluation Supporting Amend 83 to License DPR-6 ML20154A1011986-02-12012 February 1986 Safety Evaluation Supporting Amend 82 to License DPR-6 ML20138K8001985-12-12012 December 1985 Safety Evaluation Supporting Util 850410 Request for Relief from Inservice Testing Requirements for Valves in Feedwater & Reactor Depressurization Nitrogen Backup Sys ML20136D1451985-11-19019 November 1985 Safety Evaluation Re Response to Generic Ltr 83-28,Items 3.1.1-3,3.2.1-3 & 4.5.1 Concerning post-maint & Reactor Trip Sys Functional Testing.Response Acceptable ML20138R2071985-11-15015 November 1985 Safety Evaluation Re Environ Qualification of Electric Equipment Important to Safety.Util Program Complies w/10CFR50.49 & Resolution of 830426 SER & Technical Evaluation Rept Acceptable ML20209J2401985-11-0505 November 1985 Safety Evaluation Supporting Util 831107 & 850816 Responses to Generic Ltr 83-28,Item 1.1, Post-Trip Review Program & Description ML20205F6051985-11-0101 November 1985 Safety Evaluation Supporting Amend 81 to License DPR-6 ML20198A9621985-11-0101 November 1985 Safety Evaluation Supporting Request for Relief from Inservice Insp Requirements ML20205E9721985-10-29029 October 1985 Safety Evaluation Supporting Amend 80 to License DPR-6 ML20133N3931985-10-22022 October 1985 Safety Evaluation Supporting Amend 79 to License DPR-6 ML20137W3231985-10-0202 October 1985 Safety Evaluation Supporting Amend 78 to License DPR-6 1998-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C3031999-09-28028 September 1999 Annual Rept of Facility Changes,Tests & Experiments ML20199A6621999-01-0505 January 1999 Special Rept:On 981230,hi Range Noble Gas Monitor Was Inoperable for Greater than Seven Days.Cause Unknown. Preplanned Alternate Method of Monitoring Appropriate Parameters within 72 H Was Established ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML20198K6611998-12-24024 December 1998 Safety Evaluation Supporting Amend 120 to License DPR-6 ML20154E0371998-09-30030 September 1998 Safety Evaluation Accepting Request for Exemption from Certain Portions of 10CFR50.47(b) & App E to 10CFR50 to Allow Brpnp to Discontinue Offsite EP Activities & Reduce Scope of Onsite EP as Result of Permanently Shutdown ML20154E0581998-09-30030 September 1998 Safety Evaluation Accepting Licensee Request from Exemption from Certain Portions of 10CFR50.47(b) ML20198K0091998-09-18018 September 1998 SER Accepting Licensee Request for Exemption from Certain 10CFR50 Requirements for Emergency Planning for Big Rock Nuclear Plant 05000155/LER-1998-001-01, :on 980714,during Facility Decommissioning, Found Liquid Poision Tank Discharge Pipe Severed.Caused by Corrosion.Staff Reviewed Current Decommissioning Surveillance Testing on safety-related SSCs1998-08-0606 August 1998
- on 980714,during Facility Decommissioning, Found Liquid Poision Tank Discharge Pipe Severed.Caused by Corrosion.Staff Reviewed Current Decommissioning Surveillance Testing on safety-related SSCs
ML20217N2131998-04-24024 April 1998 Brpnp Zircaloy Oxidation Analysis ML20216K0011998-04-16016 April 1998 Safety Evaluation Approving Licensee Request Re Plant Training Program for Certified Fuel Handlers ML20217H4641998-03-26026 March 1998 Rev 2 to Post Shutdown Decommissioning Activities Rept (Psdar) ML20202G1941998-02-12012 February 1998 Rev 7 to Updated Final Hazards Summary Rept for Big Rock Point Plant 05000155/LER-1997-005-01, :on 971009,violation of Facility OL Was Discovered.Cause Cannot Be Determined.All Items Removed Except Cable & Hook Attached to B Rack1997-11-0505 November 1997
- on 971009,violation of Facility OL Was Discovered.Cause Cannot Be Determined.All Items Removed Except Cable & Hook Attached to B Rack
ML20154A7591997-10-0808 October 1997 10CFR50.59 Annual Rept of Facility Changes,Tests & Experiments, Since 971008 ML20216E4731997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Big Rock Point Plant ML20141J8731997-08-14014 August 1997 Safety Evaluation Supporting Amend 119 to License DPR-6 ML20210H5601997-07-31031 July 1997 Monthly Operating Rept for July 1997 for Brpnp ML20148T4901997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Big Rock Point Nuclear Plant ML20148N9251997-06-0606 June 1997 Rev 18 to CPC-2A, Quality Program Description for Operational Nuclear Plants ML20140C8981997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Big Rock Nuclear Power Plant 05000155/LER-1997-004, :on 970410,determined Potential Loss of DC Power for Primary Containment Spray & Liquid Poison Systems. Caused by Inadequate Design Control Program.Removed & Replaced Breaker 72-121997-05-0606 May 1997
- on 970410,determined Potential Loss of DC Power for Primary Containment Spray & Liquid Poison Systems. Caused by Inadequate Design Control Program.Removed & Replaced Breaker 72-12
ML20138J0121997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Big Rock Point ML20137X0161997-04-18018 April 1997 Safety Evaluation Accepting Changes to Rev 17 of CPC Quality Program Description for Operational NPPs (CPC-2A) ML20137J9381997-04-0202 April 1997 Safety Evaluation Supporting Amend 118 to License DPR-6 ML20137P0391997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Big Rock Point Nuclear Plant ML20135F2361997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Big Rock Nuclear Plant 05000155/LER-1997-003, :on 970128,demineralized Water Piping Discovered Susceptible to Overpressurization During Dba. Caused by Design Deficiency.Conducted Evaluation of Surge Protection for Piping & Procedures Revised1997-02-27027 February 1997
- on 970128,demineralized Water Piping Discovered Susceptible to Overpressurization During Dba. Caused by Design Deficiency.Conducted Evaluation of Surge Protection for Piping & Procedures Revised
05000155/LER-1997-002, :on 970115,penetration Insp Was Not Performed IAW Ts.Process for Facility Change 462J,App R Penetration Nozzle Installation,Did Not Provide Adequate Review. Penetrations Were Inspected1997-02-10010 February 1997
- on 970115,penetration Insp Was Not Performed IAW Ts.Process for Facility Change 462J,App R Penetration Nozzle Installation,Did Not Provide Adequate Review. Penetrations Were Inspected
ML20148N9181997-02-0101 February 1997 Rev 17 to CPC-2A, Quality Program Description for Operational Nuclear Plants 05000155/LER-1997-001, :on 970102,containment Sphere Integrated Leakage Rate Test Was Not Performed IAW App J to 10CFR50. Caused Because TV-02 Did Not Provide Adequate Guidance for Control of Test.Blind Flange Was Removed1997-01-31031 January 1997
- on 970102,containment Sphere Integrated Leakage Rate Test Was Not Performed IAW App J to 10CFR50. Caused Because TV-02 Did Not Provide Adequate Guidance for Control of Test.Blind Flange Was Removed
ML20134H3691997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Big Rock Point Nuclear Plant 05000155/LER-1996-013-01, :on 961207,automatic Reactor Scram Initiated by Turbine Trip Occurred.Caused by Failed Resistor within Associated Logic Circuit.Amplidyne Voltage Regulator Resistor Was Replaced1997-01-0202 January 1997
- on 961207,automatic Reactor Scram Initiated by Turbine Trip Occurred.Caused by Failed Resistor within Associated Logic Circuit.Amplidyne Voltage Regulator Resistor Was Replaced
ML20133C5421996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Big Rock Point Nuclear Plant ML20137F2101996-12-31031 December 1996 1996 Annual Financial Rept CMS Energy 05000155/LER-1996-003-01, :on 960118,RDS B Train Were Found Inoperable During Refueling Outage Surveillance Testing.Caused by Mechanical Binding.Disc & Seat Cleaned & Remaining Kerotest Valves Inspected1996-12-0909 December 1996
- on 960118,RDS B Train Were Found Inoperable During Refueling Outage Surveillance Testing.Caused by Mechanical Binding.Disc & Seat Cleaned & Remaining Kerotest Valves Inspected
ML20135E5101996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Big Rock Point Nuclear Plant ML20134H3381996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Big Rock Point Nuclear Plant 05000155/LER-1996-012-01, :on 961004,92 Day TS Surveillance Requirement Inadvertently Surpassed.Caused by Human Error.Three Yr Review of T90-10 Analyses Conducted & All Analyses Found to Be Performed as Scheduled1996-10-31031 October 1996
- on 961004,92 Day TS Surveillance Requirement Inadvertently Surpassed.Caused by Human Error.Three Yr Review of T90-10 Analyses Conducted & All Analyses Found to Be Performed as Scheduled
05000155/LER-1996-011-01, :on 960926,TS Surveillance Requirement Inadvertently Surpassed.Caused by Inadequate Procedure. Start-up Procedure 0-TGS-1, Master Checklist Immediately Revised1996-10-23023 October 1996
- on 960926,TS Surveillance Requirement Inadvertently Surpassed.Caused by Inadequate Procedure. Start-up Procedure 0-TGS-1, Master Checklist Immediately Revised
05000155/LER-1996-010-01, :on 960916,automatic Reactor Scram Occurred During Startup Due to High Reactor Pressure.Fabrication Process Will Be Evaluated & Corrected1996-10-15015 October 1996
- on 960916,automatic Reactor Scram Occurred During Startup Due to High Reactor Pressure.Fabrication Process Will Be Evaluated & Corrected
ML20211N1561996-10-0808 October 1996 Annual Rept of Facility Changes,Tests & Experiments, Consisting of Mods & Miscellaneous Changes Performed Since 961008 ML20128F9821996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Big Rock Point Nuclear Plant 05000155/LER-1994-008-01, :on 941018,one out-of-four Sensors Found out-of-tolerance in Nonconservative Direction.Caused by Setpoint Drift.Reactor Steam Drum Water Level Sensor LS-RE020A Reset within Required Tolerance1994-12-22022 December 1994
- on 941018,one out-of-four Sensors Found out-of-tolerance in Nonconservative Direction.Caused by Setpoint Drift.Reactor Steam Drum Water Level Sensor LS-RE020A Reset within Required Tolerance
ML20059E8321993-12-31031 December 1993 Monthly Operating Rept for Dec 1993 for Big Rock Point Nuclear Plant ML20058K0931993-11-30030 November 1993 Monthly Operating Rept for Nov 1993 for Big Rock Point Nuclear Plant ML20058E8961993-11-29029 November 1993 1993 ISI Rept 3-1 Big Rock Point Plant, for 930626-0905 05000155/LER-1993-011-01, :on 931102,redundant Core Spray Valve Inadvertently Removed from Svc for Approx 12 Minutes, Rendering Redundant Core Spray Sys Inoperable.Caused by Human Error.Corrective Action Being Formulated1993-11-29029 November 1993
- on 931102,redundant Core Spray Valve Inadvertently Removed from Svc for Approx 12 Minutes, Rendering Redundant Core Spray Sys Inoperable.Caused by Human Error.Corrective Action Being Formulated
ML20058F3441993-11-22022 November 1993 Safety Evaluation Concurring W/Contractor Findings Presented in Technical Evaluation Rept EGG-RTAP-10816, Evaluation of Utility Responses to Suppl 1 to NRC Bulletin 90-01;Big Rock Point ML20058G5981993-11-17017 November 1993 Part 21 Rept Re Westronics Recorders,Model 2100C.Signal Input Transition Printed Circuit Board Assembly Redesigned to Improve Recorder Immunity to Electromagnetic Interference.List of Affected Recorders & Locations Encl 05000155/LER-1993-010-01, :on 931021,several Licensed Operators Did Not Receive All Required Requalification Training During 1991-92 Training Cycle.Caused by Human Error.Training Action Plan Developed for Missed 1991-92 Training1993-11-17017 November 1993
- on 931021,several Licensed Operators Did Not Receive All Required Requalification Training During 1991-92 Training Cycle.Caused by Human Error.Training Action Plan Developed for Missed 1991-92 Training
1999-09-28
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UNITED STATES 8"
NUCLEAR REGULATORY COMMISSION o
h WASHING TON, D. C. 20555 y.....)
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO REQUESTED RELIEF FROM INSERVICE TESTING REQUIREMENTS CONSUMERS POWER COMPANY BIG ROCK POINT PLANT DOCKET NO. 50-155
1.0 INTRODUCTION
By letter dated July 5, 1988, Consumers Power Company (the licensee) requested changes, among others to the Technical Specifications (TS) related to the inservice testi..; of cert-in Reactor Depressurization System (RDS) valves for Big Rock Point Plant.
Recognizing that the proposed TS changes deviate from certain ASME Code Section XI requirements, the licensee also submitted two relief requests for NRC review and approval.
- 2. 0 EVALUATION 2.1 Relief Request for RDS Depressurizing Valves Test Frequency The Code of Federal Regulations, 10 CFR 50.55a, requires, in part, that certain safety-related power operated valves (POVs) be tested in accordance with the ASME Code Section XI requirements.
Section XI, in turn, requires that these POVs be full stroke tested every three months, or each cold shutdown if quarterly testing is not practical, and after each repair and maintenance.
Previous TS for Big Rock Point Plant required that the RDS depressurizing valves be tested during each cold shutdown, but in no case these valves need be exercised more often than once every three months.
While the associated pilot valves were being full stroke exercised, the RDS depressurizing valves were only being partial stroke exercised because they discharge directly into containment.
That partial stroke exercise used compressed gas trapped in the spool between the system isolation valve and the depressurizing valve.
Evidence is available to show that the test is not adequate to demonstrate the operability of the RDS depressurizing valves and also that the test is a significant contributor to chronic pilot valve leakage.
Based on the evidence discussed above, the licensea proposed, and NRC approved, a change in RDS surveillance requirement 11.4.1.5.c.1 from a partial stroke test of the RDS depressurizing valves during each cold shutdown, but not required more often than once every 90 days, to a full stroke test each refueling outage.
The four depressurizing valves will be sent off site for full stroke, full pressure tests using live steam.
Justification, as well as relief from the Code requirement, are prerequisites under 10 CFR 50.55a for extending the test interval to refueling outages.
For that approval, based on the licensee's submittals, the staff concluded (1) that a full stroke test using system pressure could not be performed during any mode 8811140297 es1104 PDR ADOCK 0".000155 P
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9 of operation because the RDS valves for Big Rock Point Plant discharge directly to containment, (2) that there is no practical method available to perform the full stroke test on-site, and (3) that, during a regular cold shutdown, it is impractical to remove the valves for off-site testing.
To offset the impact of the longer test interval, the licensee will disassemble and visually inspect one depressurizing valve each refueling outage as a preventive measure.
If results i
of the inspection indicate corrective repairs to the valve are required, the licensee will disassemble and visually inspect additional valves to ensure the concern is not generic.
Based on the above discussion, the staff finds that the relief request to full stroke test the RDS depressurizing valves each refueling outage, in lieu cf quarterly or during cold shutdowns, is acceptable because more frequent testing is impractical and the full stroke testing, although less frequent, is a signif-icantly better alternative than the existing partial stroke testing.
2.2 Relief Request for RDS Depressurizing Valve Pilot Valve Testing Ouring the 1988 refueling outage at Big Rock Point Plant, the RDS depressurizing valve tops were modified and now have removable pilot valve assemblies.
The modifi ation consisted of installation of two isolation valves and a bolting flange between the depressurizing valve top and the pilot valve inlet, and another bolting flange between the depressurizing valve top and the pilot valve 1
outlet.
This modification provides physical separation and isolation of the pilot vaive assembly from the RDS depressurizing valve and therefore allows removal of the pilot valve assembly for repair while the plant is in power
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operation.
Based on the design modification to the RDS depressurizing valves, the licensee proposed, and NRR approved, the addition of surveillance requirement 11.4.1.5.d to Big Rock Point Plant TS as follows:
"Should a pilot valve be isolated from service and removed, the replacement pilot valve shall be functionally tested prior to installation and return to service." Since the pilot valve assembly is a separate entity from the RDS depressurizing main valve, any repair work performed on the pilot valve should not affect the operation and integrity of the main valve.
As such, post-maintenance testing of the pilot valve need only
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be done on the pilot valve and not necessarily on the main valve.
Therefore, the staff finds that relief from Section XI post-maintenance requirement in this instance is not necessary.
However, after installation, (1) the pilot valve solenoid electrical continuity should be rechecked, (2) the isolation valves between the pilot valve and main valve should be verified open, and (3) the pilot valve inlet bolting flange leakage should be checked by using system 2
operating pressure.
t Based on the above discussion, the NRC staff finds that the relief request to test only the pilot valve, rather than the entire RDS depressurizing valve, t
following repairs to only the pilot valve is acceptable, but that relief is unnecessary because a recently completed design modification made the pilot
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valve a separate component from the main RDS depressurizing valve.
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3.0 CONCLUSION
Based on the review summarized herein, we conclude that the relief granted and the alternative examinations imposed through this document provide reasonable assurance that the acceptable level of quality and safety intended by the ASME Code will be satisfied. We have determined that, pursuant to 10 CFR 50.55a(g)
(6)(i), granting relief where the inspection requirements are impractical is authorized by law and will not endanger life or property or the common defense and security and is otherwise in the public interest considering the burden that could result if the requirements were imposed on the facility.
Date:
November
- 4,1988 Principal Contributors:
J. Huang W. Scott