ML20205L232
| ML20205L232 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 10/28/1988 |
| From: | Counsil W TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| CP-86-07, CP-86-7, TXX-88757, NUDOCS 8811010530 | |
| Download: ML20205L232 (2) | |
Text
- _.. _ _ _ _
c..
s I
<h FE Log # IXX-887E7 Fi1e 8 10110
=
M# ELECTRIC October 28, 1988
% Nuese G. Ceemeu l
nm,. n, n,m 1
U. S. Nuclear Regulatory Commission l
Attn Document Control Desk Washington, D. C.
20555 St%1ECT: COMANCHE PEAK STEAM ELECTRIL STATION (CPSES)
DOCKET NOS. 50-445 AND 50-446 STATION SERVICE WATER SYSTEM LEAKAGE l
SDAR: CP-86-07 (SUPPLEMENTAL REPORT) j Gentle.wn:
t On Ap'il 11, 1986, wie notified you by our letter logged TXX-4762 of a deficiency involving weld failure and coating degradation in the Station
~
Serv \\ce Water (SSW) System. Our last report, logged TXX-88476, was submitted on Ju.se 22, 1988.
The purpose of thit, report is to update the status of the corrective actions implemented to date.
In TXX-88476, we listed several Unit I corrective actions which we anticipated would be completed by October 28, 1988.
The following corrective actions have been completed. The documents associated with this work are in the process of I
administrative review and will be completed by Dece+ber 1, 1988, 1.
The plasite 7122 has been removed from the safety related carbon steel piping in the SSW System.
l 2.
The section of pipe in the Unit 1 Train "B" dist.harge piping between the reducing orifice and the flow orifice has been replaced.
l 3.
The installation of flange insulation kits or the replacement of carbon steel bolts with stainless steel bolts at all himetallic connections has been ccmpleted, p
i r
i es1101053o esto2s
[
gDR ADOCK0500g5 i
M North Obw 5s art LB 8I Denes Texas 13Ml
.N
TXX-88757 October 28, 1988 Page 2 of 2 The following is the status of the remaining corrective actions being implemented to resolve this deficiency:
1 The revised estimated completion date for development of the corrosion monitoring plan to monitor SSW System corrosion rates is December 1, 1988.
2.
Draft operating procedures (as described in item 5 of the corrective actions contained in TXX-88476) are in review.
The estimated approval date for issuance of these procedures has been revised to December 1, 1988.
3.
As previously stated in TXX-88476, the replacement of water absorbing gaskets with non-water absorbing gaskets is being done on a case-by-case basis as the flanges are opened for maintenance or other reasons.
Additionally, it was previously comitted in TXX-4762 to eliminate a flow induced vibration problem at 1-SW-026 via use of a longer pipe nipple.
This problem was actually eliminated by utilizing a shorter, thicker pipe nipple.
Our next rcoort, which will be submitted no later than July 29, 1989, will detail our corrective actions for Unit 2 installations.
Very truly yours, W2
/.
i%)L
/d W. G. Counsil MCP/gj c - Mr. R. D. Martin, Region IV Resident inspectors, CPSE! (3)
-