ML20205L232

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Supplemental Deficiency Rept CP-86-07 Re Weld Failure & Coating Degradation in Station Svc Water Sys.Initially Reported on 860411.Plasite 7122 Removed from safety-related Carbon Steel Piping in Svc Water Sys.Next Rept by 890729
ML20205L232
Person / Time
Site: Comanche Peak  
Issue date: 10/28/1988
From: Counsil W
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
CP-86-07, CP-86-7, TXX-88757, NUDOCS 8811010530
Download: ML20205L232 (2)


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<h FE Log # IXX-887E7 Fi1e 8 10110

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909.2 Ref. # 10CFR50.SS(e)

M# ELECTRIC October 28, 1988

% Nuese G. Ceemeu l

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U. S. Nuclear Regulatory Commission l

Attn Document Control Desk Washington, D. C.

20555 St%1ECT: COMANCHE PEAK STEAM ELECTRIL STATION (CPSES)

DOCKET NOS. 50-445 AND 50-446 STATION SERVICE WATER SYSTEM LEAKAGE l

SDAR: CP-86-07 (SUPPLEMENTAL REPORT) j Gentle.wn:

t On Ap'il 11, 1986, wie notified you by our letter logged TXX-4762 of a deficiency involving weld failure and coating degradation in the Station

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Serv \\ce Water (SSW) System. Our last report, logged TXX-88476, was submitted on Ju.se 22, 1988.

The purpose of thit, report is to update the status of the corrective actions implemented to date.

In TXX-88476, we listed several Unit I corrective actions which we anticipated would be completed by October 28, 1988.

The following corrective actions have been completed. The documents associated with this work are in the process of I

administrative review and will be completed by Dece+ber 1, 1988, 1.

The plasite 7122 has been removed from the safety related carbon steel piping in the SSW System.

l 2.

The section of pipe in the Unit 1 Train "B" dist.harge piping between the reducing orifice and the flow orifice has been replaced.

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The installation of flange insulation kits or the replacement of carbon steel bolts with stainless steel bolts at all himetallic connections has been ccmpleted, p

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TXX-88757 October 28, 1988 Page 2 of 2 The following is the status of the remaining corrective actions being implemented to resolve this deficiency:

1 The revised estimated completion date for development of the corrosion monitoring plan to monitor SSW System corrosion rates is December 1, 1988.

2.

Draft operating procedures (as described in item 5 of the corrective actions contained in TXX-88476) are in review.

The estimated approval date for issuance of these procedures has been revised to December 1, 1988.

3.

As previously stated in TXX-88476, the replacement of water absorbing gaskets with non-water absorbing gaskets is being done on a case-by-case basis as the flanges are opened for maintenance or other reasons.

Additionally, it was previously comitted in TXX-4762 to eliminate a flow induced vibration problem at 1-SW-026 via use of a longer pipe nipple.

This problem was actually eliminated by utilizing a shorter, thicker pipe nipple.

Our next rcoort, which will be submitted no later than July 29, 1989, will detail our corrective actions for Unit 2 installations.

Very truly yours, W2

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/d W. G. Counsil MCP/gj c - Mr. R. D. Martin, Region IV Resident inspectors, CPSE! (3)

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