ML20205A442

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Interim Deficiency Rept PRD-84/11 Re Potential for Leaking Tantalum Capacitors to Cause Buildup on SA-1 Relay Printed Circuit Board.Initially Reported on 841026.Deferral of Next Rept Requested Until Resumption of Const
ML20205A442
Person / Time
Site: Grand Gulf 
Issue date: 04/12/1985
From: Dale L
MISSISSIPPI POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
AECM-85-2-0008, AECM-85-2-8, NUDOCS 8504250518
Download: ML20205A442 (2)


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MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi EnMMiliddB P. O. B O X 164 0. J A C K S O N, MIS SIS SIP PI 39215-1640 g gnl7 nT : 50 April 12, 1985 NUCLEAR LICENSING & SAFETY DEPARTMENT U. S. Nuclear Regulatory Commission Region II 101 Marietta St., N. W., Suite 2900 Atlanta, Georgia 30323 Attention:

Dr. J. Nelson Grace, Regional Administrator

Dear Dr. Grace:

SUBJECT:

Grand Gulf Nuclear Station Unit 2 Docket No. 50-417 File:

0260/0511/0512 PRD-84/11, Interim Report #1, Westinghouse Type SA-1 Relays AECM-85/2-0008

Reference:

AECM-84/2-0018, October 26, 1984 Per the referenced letter, Mississippi Power & Light Company (MP&L) stated that a final report was expected to be provided by April 12, 1985 for PRD-84/11. The subject potentially reportable deficiency concerned the potential for leaking tantalum capacitors, located internally at the top of the SA-1 relay printed circuit board, to cause corrosion buildup on the circuit board and subsequent relay failure.

MP&L previously determined that this deficiency was not reportable under the provisions of 10CFR21 for GGNS Unit 1.

As indicated in the referenced letter a determination as to whether the deficiency is reportable under 10CFR50.55(e) for Unit 2 can not be made until the Unit 2 relays are energized and monitored for two weeks to determine whether they contain leaking capacitors.

In November 1982 construction activities on Grand Gulf Unit 2 were reduced to a minimum. Being in this reduced activity mode has limited the number of inspections that can be done on Unit 2 equipment to determine if the identified situation was or is applicable.

Bechtel has initiated Quality Action Request (QAR) F-464 to track required action to close our investigation of this PRD.

The QAR will remain open until all action is complete, gar 2iBBR "i89h7 gg4 J0P14AECM85040301 - 1 Member Middle South Utilities System 0 0 i

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AECM-85/2-0008 Page 2 Based on the above explanation, MP&L_ requests that further update on the subject PRD be deferred until after resumption of normal construction activities on Unit 2.

If there are any questions, please advise.

Yours truly, f

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F. Dale Director

-EBS/SHH:rw cc:

Mr. J. B. Richard Mr. O. D. Kingsley, Jr.

Mr. N. S. Reynolds Mr. G. B. Taylor Mr. James M. Taylor, Director Office of Inspection & Enforcement-U. S. Nuclear Regulatory Commission Washington, D. C.

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