ML20204D388

From kanterella
Jump to navigation Jump to search
Initial Notification of Reportable Occurrence 50-298-78-35 on 781124.Recirculation MG Set B Was Tripped,Then a Fuse Was Pulled for Exam,Allowing MG Set B to Ramp Up in Speed, Causing Fast Pwr Increase.Due to Personnel Error
ML20204D388
Person / Time
Site: Cooper Entergy icon.png
Issue date: 11/29/1978
From: Lessor L
NEBRASKA PUBLIC POWER DISTRICT
To: Seyfrit K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
NUDOCS 7812200259
Download: ML20204D388 (2)


Text

_. _ _ _ _ _ _ _ _ _ _ _. _ _

.~

~

COoPFR NUCLEAR STATION P.O. DoX 98. DRoWNVILLE, NEBR ASKA 68321 Nebraska Public Power Distn. t m EPsoNE m m.3m c

= no

=

November 29, 1978 Mr. Karl V. Seyfrit, Director l

U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region IV 611 Ryan Plaza Suite 1000 Arlington, Texas 76011

Subject:

Reportable Occurrence Initial Notification

Dear Sir:

At the time of the following occurrence on November 24, 1978, we did not consider the event to be reportable. After further review on November 27, 1978, we concluded that the occurrence may be reportable under Technical Specirications 6.7.2.A.4.

I contacted Mr. Eric Johnson on November 27, 1978 and explained to him what we thought had occurred and that we were evaluating the cause and reportability. After interviewing personnel involved and after review of Station Safety Analysis Data in the FSAR, we now have concluded that tha event should be reported under 6,7.2.A.4 of the Technical Specifications.

Therefore, we are submitting this initial report to you.

A more detailed report will follow.

Report No.:

50-298-78-35 Report Date:

November 29, 1978 Occurrence Date: November 24, 1978 Facility:

Cooper Nuclear Station Btownville, Nebraska 68321 Identification of Occurrence:

A condition which probably resulted in a short term reactivity increase that corresponded to a reactor period of less than 5 seconds.

Conditions Prior to Occurrence:

Reactor was at a low power level of approximately 27% of rated thermal power.

Description of Occurrence:

The reactor power was at a reduced level so that surveillance testing of the turbine stop valves and a scheduled rod swap could be accomplished. While at this reduced power level, various pres-sure settings on Recirculation MG Set "B" 011 Lubrication System I

cP 47 0 t

781220025*t 3

I

Mr. K. V. Seyfrit November 29, 1978 Page 2.

were being calibrated and reset if necessary. While performing this work on the lubrication system, Recirculation MG Set "P".was inadvertently tripped due to personnel errer. After Recirculation Pump "B" was brought on line, it was discovered that MG Set "B" would not respond to en increase in speed demand.

Troubleshc7 ting this problem led to the possibility of a fuse being blown in ths.

control circuitry.

The fuse was pulled for examination and im-mediately thereafter MG 6et "B" began ramping up in speed causing a rapid power increase.

The exact time frame of this power increase cannot be determined though it is believed the duration was less than or equal to 10 seconds. The fuse waa put back in as soon as reaction time permitted and also MG Set "B" was tripped by an operator very shortly thereafter; either one or both of these

)

sctions tenainated the transient. The maximum thermal power ob-served during the transient was approximately 75% of rated pover.

Designation of Apparent Cause of Occurrence:

Personnel error (pulling the fuse without a clear understanding of what would result).

Analysis of Occurrence:

The analysis for this event i.' presented in Section XIV.5.6 of the Cooper Final Safety Analysis Report. An examination of the off gas recorders after the event did not show a permanent increase in off gas activity; therefore, it is not believed any fuel damage resulted.

Corrective Action:

The fuse was reinserted as rapidly as possible and the personnel

)

nvolved reviewed the events to prevent a recurrence.

]

l Sincerely, j

i f/

L. C. Lessor Station Superintendent i

Cooper Nuclear Station LCL:cg