ML20199H516
| ML20199H516 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 01/28/1998 |
| From: | Ruland W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20199H465 | List: |
| References | |
| 50-333-97-11, NUDOCS 9802050070 | |
| Download: ML20199H516 (9) | |
See also: IR 05000333/1997011
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U.S. NUCLEAR REGl.lLATORY COMMISSION
REGION I
Docket No:
50 333
License No:
DPR 59
Report No:
50 333/97 11
Licensee:
New York Power Authority
Facility:
James A. FitzPatrick Nuclear Power Plant
Location:
Post Office Box 41
Scriba, New York 13093
Dates:
December 1519,1997 and January 7,1998
Inspector:
Leonard Cheung, Senior Reactor Engineer
Gordon Hunegs, Sr. Resident inspector
Approved by:
William Rutand, Chief
Electrical Engineering Branch
Division of Reactor Safety
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EXECUTIVE SUMMARY
James A. FitzPatrick Nuclear Power Plant
NRC Inspection Report No. 50 333/97-11
This inspection v.as conducted to review the issue associated with the upgrade
(replacement) of the original General Electric traversing incore probe (TIP) with a Siemens
digital system. This report covered the result of a one week onsite inspection by one
region based inspector and one resident inspector.
Enoineerino
The licensee's replacement in 1991 of the original GE TIP system with a Selmens
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digital TIP system involved an USQ and was in violation of 10 CFR 50.59 (a) (1)
and (2). (E8.1)
The three primary containment isolation ball valves in the TIP system were
inoperable from 1991 to 1996 in that these valves could be opened (by an
unintended design function) when containment isolation was required. This was not
in ecmpliance with FitzPatrick Technical Specifications Section 3.7.D.1. (E8.1)
The licensee's disposition of a Deviation / Event Report for replacement of a
nonsafety-related 24 Vdc power supply in the TIP system was weak. (E8.1)
One unresolved item is closed. (E8.1)
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Ooeratigna
Operators showed a weakness in recognizing a pl6nt condition that required
technical specification actions to be taken in response to the TIP ball valves failing
opan. (04.1)
Plant was placed in cold shutdown in accordance with technical specification
requirements. (04.1)
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Reoort Details
Summary of Plant Status
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This was a special engineering inspection to review the upgrade (replacementl of the
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original General Electric traversing incore probe (TIP) with a Siemens digital system. During
the inspection, FitzPatrick was restarting from a forced outage to repair the safety relief
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valves, and was at fu't power at the end of the inspection.
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E8
Miscellaneous Engineering issue (92903)
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E8.1
(Closed) Unresolved item (96 06 04): Traversina incore Probe (TIP) Svstem Ball
Valve Control Failure
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a.
Insoection Scoos
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On September 16,1996, a human error caused a momentary loss of power to the
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TIP control system and the activation cf the containment isolation signal. When the
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power was restored, the licensee found that the three primary containment isolation
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ball valves in the TIP system opened with a valid Group 2 containment isolation
- signal present. ' At that time, the TIPS were not beir.g inserted or withdrawn. The
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licensee attributed the cause of the valve opening to a power supply failure in the
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torque control unit of the TIP systen, The inspector reviewed pertinent licensee
documents to determine licensee's compliance with safety and regulatory .
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requirements.
b.
Observations and Findinas
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Backaround
in February 1991, the licensee replaced the originti General Flectric (GE) TIP system'
with a Siemens digital system (Modification F188-253). The licensee stated that-
the Siemens system wa.; the only one installed in the United States, therefore, there
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would be no generic concern for this issue.
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1The original GE TIP system consisted of three subsystems; each consisted of motor
= control and drive mechanism, and a guide tube that penetrated the primary
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containment, and an indexer that was inside the primary containment. _ Each guide
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tube (3/8" outside diameter) had two primary containment isolation valves (one ball
valve'and one shear valve) located outside the containment wall. The indexer vos
inside the primary containment. The GE design criteria for the containment isolation
as indicated in Section 5.3.2 of GE document NEDC-22253, "BWR Owners' Group
Evaluation of Cuntainment Isolation Concerns," dated October 1982 states that:
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"Under normal verating conditions, the TIP system guide tubes do not
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communicate with the containment atmosphere because purge air supplied
to the box surrounding the indexing mechanism eff sctively precludes such
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communication. However, following a LOCA (loss of coolant accident) or
containment pressurizing event, a check valve on the box will open, resulting
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In direct communication between the containment atmosphere and the TIP
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guide tubes. Consequently, GDC (General Design Criterion) 56 is the
- applicabie NRC requirement for TlP system isolation design."
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The Siemens system Iso coniisted of three subsystems similar to the GE system,
except that the guide tube size was 10 mm instead of 3/8". The Siemens system
also contained three new indexers. As documented in Section 6.2 of a HtzPatrick
report (JAF RPT NMS 01511, Revision 1, dated December 6,1996), the provision
for t..e indexer design was as follows:
"Under normal operating conditions, the TIP system guide tubes do not
communicate with the containment atmosphere because the indexing
mechanism is sealed against containment atmosphere and effectively
precludes such communication. However, following a LOCA (loss of coolant
accident) or a guide tube break inside containment, direct communication
between the containment atmosphere and the TIP guide tubes is established.
Consequently, GDC 56 is the applicable NRC requirement for TIP system
isolation design."
The Siemens system used four programmable logic controllers (PLC); one in the
central control bait in the main control room, and one in each subsystem. This
system also used a common torque control unit, which had a 24 Vdc power supply
(115 Vac input).
Following the September 16,1996, event, the licensee found that the power supply
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for the torque control unit had failed. The licensee's evaluation dt.termined that this
power supply f ailure had caused the TIP position indication to go to zero.
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Subsequently, the computer software (as designed) opened all three primary
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containment isolation ball valves on a TIP position indication of ze o, in spite of a
valid Group 2 containment isolation signal. The licensee also determined that all
PLCs functioned as designed. The inspector found that this design function had not
been analyzed by the licensee during the 1991 design change (TIP system
replacement) process.
The licensee had issued a Nuclear Safety Evaluation (JAF 8E-89146, Traversing
Incora Probe Upgrade, dated September 12,1990) to sup#t the 1991 TIP system
design change. The inspector reviewed this safety evaluation and found that it did
not nalyze the failure mode of the system components (nonsafety related) that
could cause a malfunction in the safety related containment isolation valves. The
safety evaluation also did not discuss tha hardware or the software (or firmware) of
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the four PLCs, nor the verification and validation of the software.
Desian Basis and Technical Soecifications Reauiremants
The inspector reviewed FitzPatrick Final Safety Analysis Report (FSAR), and found
that the design basis for the three primary containment isolation ball valves
(0*/SOV-104A,B, Clin the TIP system was specified in the FSAR as follows:
1) Notes 16 to FSAR Table 7.3-1 for these three primary containment isolation
valves states, "During normal power operation the TIP ball valves are closed except
during LPRM (local power range monitor) calibration operations when the TIP is
inserted or withdrawn to measure reactor power at various locations within the
reactor core"; and 2) FSAR section 7.5.9.2 (Revirion 4, dated July 1993) states
that (for each TIP subsystem) a guide tube (pr! mary containment isolation) ball valve
opens only when the TIP is being inserted.
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10 CFR 50.59(a)(1) states that a licensee may make changes in the facility as
described in the safety analys:s report, without prior NRC approval, unlesp the
proposed change involves an unreviewed safety question (USO). 10 CFR 50.59(a)(2) states that a proposed change is deemed to involve a USO if a
possibility for a malfunction of a ddlerent type than any evaluated previously in the
safety arialysis report may be created.
However, in 1991, the licensee made a change to the TIP system that in folved a
USO without prior NRC approval. Specifically, the licensee's replacement in 1991
of the original General Electric TIP syste.n with a Siemens digital TIP system
involved a USO in that the Siemens digital system contained an unintended function
which caused, on September 16,1996, a malfunction of a different type for the
three primary containment isolation ball valves in the TIP system. The three ball
valves opened in the presence of a valid Group 2 containment isolation signal and
the TIPS were not being inserted or withdrawn. The ball valves could not be closed
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until the next day when a 24 Vdc power source was temporary connected to the
torque control unit of the TIP system. This incident occurred when the power
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supply to the TIP system was lost and subsequently restored. The unintended
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function in the Siemens digital system was not previously evaluated in the FSAR nor
in the safety evaluation (JAF SE 89146, dated September 12,1990) e ssociated
with TIP system replacement. This is a violac (eel 50 333/97-11-01)
The inspector reviewed Licensoe Event Report (LER) 96-010-01 and found that the
inadvertent opening of the three primary containment isolation ball valves with a
valid containment isolation signal present was discussed briefly in this LER.
However, the condition that FitzPatrick potentially operated the three ball valves
outside the design basis was not reported.
The inspector's review of FitzPatrick Technical Specifications (TS) indicated that
section 3.7.A.2 requires that primary containment integrity shall be maintained at all
times when the reactor is critical or the reactor water temperature is above 212'F,
and fuel is in the reactor vessel, except while performing low power physics tests at
atmospheric prescure at power levels not to exceed 5 MWt. TS section 3.7.D.1
requires that whenever primary containment integrity is required, containment
isolation valves shall be operable. TS section 4.7.D identified the containment
isolation valves as those listed in FSAR section 7.3, which included the three
primary containment isolation ball valves (07SOV 104A,B,C)ln the TIP system.
However, from 1991 to September 1996, when primary containment integrity was
required to be maintained, the three primary containment isolation ball valves in the
TIP system were inoperable, in that these valves could be opened by an unintenced
design function in the TIP system in the presence of a valid containment isolation
signal. The inspector determined that the 1991 replacement of the TIP system also
violated FitzPatrick TS as discussed above. (eel 50-333/97 11-02)
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Licensee's Corrective Actions :
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Following the September 16,1996, event, the licensee made a change to the
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control of the three ball valves in the TIP system. The hcensee placed the circuit
breakers that control power to these valves into normally "open" position (except
during TIP operation). The licensee also completed a revised version of Nuclear
Safety Evaluation JAF SE-89146 on December 6,1996, and revised the affected -
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surveillance procedures to reflect the change. Implementing the above change'
would preclude the ball valves from being opened by errant digital signals. The
inspector's review of these documents found them generally acceptable. However,
the revised safety evaluation still did not discuss the " validation and verification" of
- the PLC software, and did not recognize that the 1991 TIP system replacement
involved an USO.
The licensee also completed an evaluation (Report No. JAF RPT-NMS 02511,
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Assessment of the TIP System Containment Isoletion Design, Revision 1) on
December 6,1996. Thic document referred to a FitzPatrick report (JAF RPT-NMS-
02511, Revision 1, dated December 5,1996), which again refer.to another
FitzPatrick document, JAF CALC RAD-00057, entitled " Potential Radiological
Consequences of the TIP System Failure to isolate Under Normal and Accident
Conditions." The results of these analyses Indicated that the maximum bounding
radiological release was within the 10 CFR 100 limit.-
The other three associated containment isolation valves (explosive operated shear
valves) are normally open and do not automatically clo:e when containment
isolation signal is initiated. They are to be manually closed by the operators.
During this inspection, thh licen'see still had not yet determined the cause of the
power supply failure in the torque control unit. Following the September 16,-1996,
event, the licensee ordered two power supplies (all nensafety related); one for
replacement of the failed unit and one for spare, from the vendor. The licensee
re<:eived the first unit about four days later, and_without understanding the
installation instructions, which was in German, the licensee promptly installed the
unit. The licensee failed 4 ) recognize that this power supply was a dual input
voltage (115/230 Vac) mt and that the shipped unit was configured for 230 Vac
installation. On December 4,1996,the licensee measured the output voltage of the
spare power supply and found that the maximum output voltage that could be
adjusted was 20.16 Vde, much lower than the specified output of 24 Vdc. The
.. licenses stated that the TIP system was still operable even though the torque
. control unit power supply was configured incorrectly.1The inspector's review of
Siemens specifications confirmed the licensee's statement, indicating the acceptable
input voltage to the torque control unit ranged from 13 - 33 Vdc.
During a November 14,1997, telephone call, to the vendor, the licensee was
informed that for 115 Vac input voltage, jumper.BR.1 must be installed on the
output of the full wave bridge in the power supply unit, as indicated in the Germen
installation instruction. Subsequently, the licensee issued a Deviation / Event Report
(DER Nc. 97-1558)to address this issue. The inspector eviewed this DER, which
was closed on November 26,1997, and found the disposition to be week, even for
a nonsafety-related item, whose failure had already caused an inadverte- opening
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of the containment isolation valves. For the corrective actions, the resolution was:
WR 96 06511-05had been initiated to replace existing power supply with a
correctly configured power supply. There were no actions taken to ensure that
personnel performing installation must read and understand installation instructions
before starting installation. During the December 19,1997, exit meeting, the
licensee management stated that additional follow up was needed for this DER,
c.
Conclusion
The inspector concluded that the licensee's replacement in 1991 of the original GE
TIP system with a Selmens digital TIP system involved an USQ and was in violation
of 10 CFR 50.59(a)(1) and (2). The inspector also concluded that the three primary
containment isolation ball valves in the TIP system were inoperable from 1991 to
1996 in that these valves could be opened (by an unintended design function) when
containment isolation was required. This constituted a vlotation of FitzPatrick
Technical Specifications Section 3.7 D.1.
The licensee's disposition of DER 971658 for replacement of a nonsafety related
24 Vdc pwoer supply in the TIP system was weak.
The original unresolved item is closed.
04
Operator Knowledge and Performance
04.1 Operator Actions Associated With Spurious Opening of Traverse incore Probe (TIP)
System Valves During September 16,1996 Event
a.
Insoection Scone
The inspector reviewed post trip logs, operator logs, work requests and deficiency
and event reports associated with the TIP system. Additionally, discussions were
held with operation department staff members,
b.
Observations and Finoinas
The following describes the sequence of events associated with the TIP ball valves:
On September 16,1996, at 1:04 p.m. the TIP ball valves received a group 11
Isolation signal due to low reactor pressure vessel water level and initia!!y closed.
Operators verified and logged that all Group ll containment isclation valves were
closed. At 1:35 p.m., the TIP ball valves inadvertently opened following
energization of a electrical bus. At approximately 2:00 p.m., operators recognized
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that the TIP ball valves were open. Operations shift management discussed the
need to isolate the TIP penetrations using the shear valven and decided that the
action was not necessary. Plant design provides for a shear valve that can cut
through the TIP cable and isolate the penetration if the ball valves are unable to
close because of a TIP cable fouling the valves. The decision to not close the shear
valve was based, in part, on plant conditions, which showed that the conditions in
containment did not indicate a need for isolation, and that the _TIP system had not
been in use prior to the event. However, the TIP ball valves were not declared
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inoperable, nor was a limiting condition for operation (LCO) of Technical
Specificatinns Section 3.7.D.2, Primary Containment Isolation Valves, entered at
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that time. Shift management requested assistance to get the TIP ball valves shut.
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Reactor engineering was unable to shut the valves and at approximately 9:00 p.m.
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the operations support center dispatched en emergency repair team which identified
a power sJpply problem in the TIP controllogic system. On September 17, at
6:00 a.m., the reactor was in cold shutdown. Subsequently, the TIP ball valves
were closed af ter a 24 Vdc power source was temporary connected to the torque
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control unit of the TIP system. At 6:00 p.m., the TIP ball valves were declared
inoperable and the LCO was entered.
Technical Specifications Section 3.7.D.2 requires that, with one or more of the
containment isolation valves inoperable, actions be taken within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to restore
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the valvo, or isolate the oenetration, if this can not be met, the reactor shall be in
cold shutd wn within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Since the shear valves were not closed witnin 4
hours then the plant was required to proceed to cold shutdown.
c.
Conclusions
Operators showed weakness in recognizing a plant condition that required technical
cpecification actions be taken in response to the TIP ball valves fai'ing open. The
reactor was placed in cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> while operators made
attempts to shut the TIP ball valves. Although operators did not declare the valves
inoperable upon discovering they were open and could not be shut, nor did they use
the shear valves to isolate the penetration, the plant was placed in cold shutdown in
accordance with technical specification requirements.
E9
FSAR Reviews
A recent discovery of a licensee operating their facility in a manner contrary to the
updated final safety analysis (UFSAR) description highlighted the need for a special,
focused review that compares plant practices, procedures and/or parameters to the
UFSAR descriptions.
While performing the inspections discum:.a in thic report, the inspectors reviewed
the applicable portions of the UFSAR that related to the areas inspected, including
FSAR Table 7.3-1 and Section 7.5.9.2, that pertained to the design besis for the
three primary containment isolation ball valves in the TIP system. The inspector
verified that other reviewed sections of the FSAR wording were consistent with the
observed p' ant practices, procedures and/or parameters.
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XI
Exit Meeting
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The inspector met with the licensee personnel at the conclusion of the site inspection on
December 19,1997, and summarized the scope of the inspection and the inspection
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results. No proprietary information was knowingly included in this report from those
documents. The licensee acknowledged the inspection find!ngs at that meeting.
The inspector amended the exit meeting in a January 7,1998, telephone call to
Messrs. A. Zarenba and M. Abramski of the New York Power Authority. The inspector
stated that the unintended function in the Siemens digital system had also caused the three
primary containment isolation ball valves in the TIP system inoperable from February 1991
to 1996 as discussed in Section E8.1.b of this report.
PARTIAL LIST OF PERSONS CONTACTED
M. Abramski, Licensing
W. Bennett, Design Engineer
W. Berzins, Manager of Communicatlan
M. Burnstein, l&C Lead Engineer
M. Colomb, Site Executive Officer
R. Converse, Technical Assessment Coordinator
S. Kohr, Supervisor, Mechanicol Design Engineering
D. Lindsey, Administration
D. Ruddy, Director, Design Engineering
R. Steingerwalt, Licensing Engineer
D. Toplay, Administration
D. Vandermark, Quality Assurance Manager
A. Zarenba, Licensing Manager
NaC
G. Hunegs, Senior Resident inspector
ITEMS OPENED AND CLOSED
Ooened
50-333/97 11-01
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USO for TIP system replacement
50 333/97 11-02
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TIP system containment isolation valves inoperable
Closed
50 333/96-06 04
TIP system ball valve control failure
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