ML20199H175

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Forwards Rev 1 to Event Rept ER-98-26 Re Safety Limit Exceedance of C-315 Number 1 Normetex Pump High Discharge Pressure Sys
ML20199H175
Person / Time
Site: Paducah Gaseous Diffusion Plant
Issue date: 01/19/1999
From: Pulley H
UNITED STATES ENRICHMENT CORP. (USEC)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GDP-99-1002, NUDOCS 9901250133
Download: ML20199H175 (7)


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DSEC

. A Global Energy Company January 19,1999 GDP 99-1002 i

United States Nuclear Regulatory Commission Attention: Document Control Desk i

Washington, D.C. 20555-0001 Paducah Gaseous Diffusion Plant (PGDP)

Docket No. 70-7001 Event Report ER-98-26, Rev.1 Enclosed is the final voluntary report for the Safety Limit exceedance on the C-315 No.1 Normetex Pump High Discharge Pressure System. This report provides supplemental infom1ation for Event Report ER-98-26, which was issued to the Nuclear Regulatory Commission (NRC) on November 16,1998. The supplemental information is designated by a revision bar in the right margin of the i

report. This report reflects NRC's approval of the deletion of TSR 2.3.2.1 and TSR 2.3.3.1 on the Normetex Pump High Discharge Pressure System and its associated Safety Limit, as documented in Amendment 20 of the Certificate of Compliance. It also provides supplemental information on the direct cause of the event. There are no new commitments in this report.

Any questions regarding this matter should be directed to Larry Jackson at (502) 441-6796.

Sincerely, 1

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(

Pulley General Manager Paducah Gaseous Diffusion Plant

Enclosure:

As Stated cc: NRC Region III Office NRC Resident inspector-PGDP 0) 9901250133 9901191 PDR ADOCK 07007001 C

PDR_

P.O. Box 1410, Paducah, KY 42001 Telephone 502-441-5803 Fax 502-441-5801 http://www.usec.com OfIices in Livermore. CA Paducah, KY Portsmouth,011 Washington, DC

Docket No. 70-7001 GDP 99-1002 Page 1 of 6 EVENT REPORT ER-98-26 Revision 1 DESCRIPTION OF EVENT On October 17, 1998, at approximately 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />, a solenoid valve failed which caused the discharge block valve to close resulting in the unplanned shutdown of the on-stream No.1 Normetex pump in the C-315 Tails Withdrawal Facility. This resulted in an automatic shutdown of the pump motors and a rapid, but brief, discharge pressure increase on the pump before the pump rotation came to a complete stop. A discharge pressure of approximately 50 pounds per square inch absolute (psia) 4 was recorded on the system's monitoring computer. This value exceeds the 45 psia Safety Limit (SL) defined for the Normetex pump discharge bellows pressure, per Technical Safety Requirement (TSR) 2.3.2.1.

The Plant Shift Superintendent (PSS) declared the No.1 Normetex Pump High Discharge Pressure System inoperable at 2105 hours0.0244 days <br />0.585 hours <br />0.00348 weeks <br />8.009525e-4 months <br /> on October 17, 1998. The NRC Senior Resident Inspector was notified of the event. On October 18,1998, at 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br />, a voluntary notification was made to the Nuclear Regulatory Commission (NRC) informing them of the SL exceedance. NRC assigned Worksheet No. 34926 to this event notification.

A previous SL exceedance occurred on August 26,1998, when the C-315 No. 2 Normetex pump tripped due to an unplanned closure of the discharge olock valve. A discharge pressure of approximately 46 psia was recorded. A voluntary 24-hour notification was made to NRC, followed by a voluntary 30-day written report of the event investigation (ER-98-23). The investigation determined that the design of the Normetex Pump High Discharge Pressure System was inadequate I

to preclude transient pressures from exceeding the 45 psia SL. As a result of that event, cempensatory actions were put in place to milimize the risk of exceeding the 45 psia SL. The compensatory measures included stationing an operator at the Normetex pump control panel to monitor and control pump suction and discharge pressures below procedurally implemented limits.

The operator was not expected to take actions to prevent the transient in the event of a discharge valve closure, but to ensure that the steady-state operating pressures would meet the initial conditions necessary to avoid exceeding the SL. Engineering Evaluation EV-C-821-98-018, "Normetex Pump Pressure Limitations," documented the assumptions and calculations for the determination of these pressure limits. Limits for the C-315 No.1 Normetex pump were established at 3.7 psia raaximum suction pressure and 29.5 psia maximum discharge pressure.

4 The operator monitoring the C-315 No. I Normetex pressures on October 17,1998, reported a suction pressure of 3.5 psia and a discharge pressure of 27.5 psia were being maintained, which were below the procedurally defined limits. He heard the general building alarm and determined from the control panel annunciators that the No.1 Normetex pump had shut down and its air-operated suction and discharge valves had closed. The operator then opened the discharge vent valve to evacuate the

Docket No. 70-7001 GDP 99-1002 Page 2 of 6 i

remaining UF in the pump. The operator did not observe a pressure increase prior to the Normetex 6

pump shutdown alarm.

In response to the Normetex pump shutdown alarm, a second operator went to the pump to check for local control panel alarms, which might indicate the cause of the pump shutdown. The pump 4

main drive motors were tripped, but no local control panel alarms were actuated. There was no observable damage to the pump or expansion joint bellows. The operable Process Gas Leak l

j Detection head did not alarm, indicating there was no out-leakage of UF. Operations in the vicinity l

i of the pump were restricted to preserve evidence, with the exception that manual suction and i

discharge block valves were closed to permit long term isolation. When isolated the pumps do not contain significant quantities of UF (less than five pounds). Recognizing that the SL had been 6

exceeded, at 1917 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.294185e-4 months <br /> on October 17,1998, all operating Normetex pumps were placed in standby and the plant was placed on recycle.

On October 18,1998, the United States Enrichment Corporation (USEC) submitted to NRC a Request for Enforcement Discretion related to TSR 2.3.2.1. The enforcement discretion was needed l

to allow cascade operations to return to normal operations, even though the plant could not j

demonstrate that the Normetex Pump High Pressure Discharge System would always function to meet the TSR 2.3.2.1 operability requirements for the Normetex pump discharge bellows pressure.

Thejustification for this request was based on the low safety significance associated with a failure of the discharge expansionjoint. Similarjustification was provided in the Certificate Amendment Request (CAR) which was submitted on September 11,1998, to delete TSR 2.3.2.1, "Normetex l

Pump Discharge Pressure," and TSR 2.3.3.1," Normetex Pump Discharge Pressure System," and l

to revise related sections of the Safety Analysis Report (SAR). (This request was later approved by l

NRC, as documented in Amendment 20 of the Certificate of Compliance, and was implemented by l

the plant on December 23,1998.)

l On October 18,1998, at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, NRC orally issued USEC a Notice of Enforcement Discretion (NOED) which allowed the plant to return to normal operations while NRC processed the above l

TSR changes to remove the SL and the associated TSR. The NOED required the compensatory l

actions defined in the earlier NOED to remain in effect to minimize any pressure transients in the Normetex pump discharge lines. At 0720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> on October 18, 1998, the PSS declared the Normetex Pump High Discharge Pressure Systems operable, in accordance with the NOED. The No.1 Normetex pump remained inoperable, pending determination of cause of the pump shutdown.

NRC issued a written NOED on October 20,1998. The NOED stated the intention to continue to exercise discretion not to enforce compliance with TSR 2.3.2.1 until issuance of the certificate amendment.

Engineering Evaluation EV-C-821-98-026 was prepared, with concurrence by the Plant Operations Review Committee, to ensure all actions required by TSR 1.6.1.2 were met prior to restart of the No.

1 Normetex pump. TSR 1.6.1.2.a and b did not require action because of the nature of the event.

Docket No. 70-7001 GDP 99-1002 Page 3 of 6 TSR 1.6.1.2.c requires a technical evaluation be conducted to determine if any damage has occurred and to evaluate the ability of the system to be restarted. This Engineering Evaluation concluded that there was no damage to the C-315 No. I Normetex pump discharge expansion joint as a result of the momentary SL exceedance.

CAUSES OF EVENT A.

Direct Cause The direct cause of the pump discharge pressure increase was the closure of the discharge block valve on the running pump. The Nomietex pump is basically positive-displacement in nature, and compression of gas into a blocked discharge line results in a rapid pressure rise. The discharge block valve design uses air pressure to actuate a diaphragm that opens the valve. Loss of air pressure closes the valve. Air is supplied to the valve via three solenoid valves arranged in series such that each must be energized to enable air to be supplied to the discharge block valve. If any of the three solenoids de-energizes, or fails closed, air is vented and the discharge block valve closes. In this case, solenoid valve PY-212Cl, the first valve in series from the plant air source, failed.

This failure mode was confirmed during testing associated with the event investigation.

When PY-212C1 was energized, it chattered loudly and vented significant amounts of air out ofits vent pon. If the solenoid valve had been operating properly, this port would have been closed off when the valve was energized. The discharge block valve opened, but one to two minutes later it closed, indicating that PY-212Cl was not maintaining suflicient air pressure to the valve to keep it open. A short time later the test was repeated, but the solenoid valve had degraded to the point that it seized, keeping the block valve closed.

Solenoid valve PY-212Cl is a non-safety-related component of standard commercial quality.

It is estimated that this solenoid had been in service 5-8 years. The safety function of the Normetex pump protective systems involves shutdown and isolation of the pump, thus loss of air to the Discharge Block Valve does not compromise this function. The solenoid valve was removed and disassembled for inspection and evaluation of the failure mode. The interior of the valve was covered with a soot-like deposit. The soot-like material would have interfered with the seating of the valve and is considered the cause of the solenoid valve failure.

A laboratory analysis of the solenoid valve was performed and is documented in detailin KY/L-2039," Failure ofASCO Solenoid Valve in C-315." This analysis determined that the soot-like deposit was mostly silicone and iron. The iron came from wear on the solenoid core, an expected result of chattering. The source of the silicone-based residue was from a l

=

i Docket No. 70-7001 GDP 99-1002 Page 4 of 6 breakdown of the solenoid valve components, rather than from an external source. This was l

based on the lack of any significant quantity of residue found up/ downstream of the solenoid

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valve.

At the time of the event, there was no periodic replacement or internal l

cleaning / inspection preventive maintenance for solenoid valves in this application, since l

t these components were considered to fail safe. However, due to the undesirable pressure j

i transient that is experienced when the discharge block valve closes inadvertently, a l

preventive maintenance schedule for periodic replacement of solenoid valves in this l

application has been established to enhance system reliability.

l As an interim measure, the solenoid valves in this application at each Normetex pump were examined for vent port leakage. One leaking valve was identified and replaced to minimize risk of another inadvertent discharge block valve closure.

B.

Root Cause The cause of the safety limit exceedance on October 17,1998, was that design of the High Pressure Discharge System and the safety-related discharge block valve interlock trip signal was inadequate to prevent the transient pressures from exceeding 45 psia, even with the reduced suction and discharge pressure limits defined by the Engineering Evaluation EV-C-821-98-018. The suction pressure limit bounds the pump flow rate. The discharge pressure limit sets the baseline pressure from which a transient begins. The magnitude of the transient itself was empirically determined based on the August 26,1998, event and an earlier pressure excursion on July 7,1998, which did not exceed the SL. Due to the pumps being similar in design, the analysis assumed that observations of discharge pressure increase could be generically applied to any Normetex pump installation. A weakness exists in this assumption. The analysis assumes that the discharge block valve closes rapidly, thereby allowing the steady-state operating pressure to be used as a transient basis. If the mode of discharge block valve system failure involves partial or slow closure of the block valve, then an incremental pressure increase occurs before the pump trips. This incremental pressure increase must be added to the steady-state operating pressure to get the transient basis.

The post-event tests confirmed that the failure was not complete, since the discharge block valve could be reopened for a time. By nature of the air-operator design (air to open/ spring to close), the application of partial air pressure can mid-position a valve. The interlock trip, assumed to operate in the analysis, requires full closure of the valve to actuate the pump shutdown circuit. Thus, if the solenoid valve vented significant air pressure from the discharge block valve, but not enough to fully close it, the discharge line would be significantly blocked and cause a pressure increase. Based on a reconstructed peak discharge pressure of approximately 50 psia, it is evident that any pressure increase due to partial valve closure was limited to only 5 to 10 psi, which is the amount above the predicted pressure per

1 Docket No. 70-7001 GDP 99-1002 Page 5 of 6 the compensatory action calculations. This pressure increase is estimated to have occurred very rapidly, on the order of a few seconds.

I At some point, either the High Discharge Pressure System, or, if the valve closed fully, the Discharge Block Valve Interlock, would have tripped the pump. The interlock trip was active and likely initiated the pump trip, based on the pressures observed. However, it is indeterminate whether the interlock or the high pressure trip actually tripped the pump.

i CORRECTIVE ACTIONS A.

Corrective Actions Taken 1.

On September 11,1998 USEC submitted a CAR to NRC tojustify the deletion of the TSR 2.3.2.1 SL and the TSR 2.3.3.1 Nonnetex Pump High Discharge Pressure System as TSR requirements.

2.

On October 17,1998, Systems Engineering examined the solenoid valves in the same application at each Normetex pump in the C-315 Tails Withdrawal Facility for vent port i

leakage. One leaking valve on the No. 3 Normetex pump was identified. This valve was replaced on November 6,1998.

3.

On October 19,1998, Maintenance replaced solenoid PY-212-Cl for the discharge valve on the No. I Normetex pump in the C-315 Tails Withdrawal Facility.

4.

On November 10,1998, Systems Engineering examined the solenoid valves in the same application at each Normetex pump in the C-310 Product Withdrawal Facility for vent port leakage. No leaking valves were identified.

5.

On December 23, 1998, Document Control issued Revision 34 to USEC-01-A1, l

" Application for t hated States NRC Certification," which deleted TSR 2.3.2.1 and TSR l

2.3.3.1 on the Nonnetex Pump High Discharge Pressure System and revised related l

sections of the SAR. These changes were based on Amendment 20 of the Certificate of l

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Compliance which was effective the same date.

l 6.

On January 7,1999, Reliability Engineering established a preventive maintenance schedule l

for the periodic replacement of the solenoid valves which control air to the Normetex l

Pump discharge block valve to enhance system reliability.

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a Docket No. 70-7001 GDP 99-1002 Page 6 of 6 B.

Corrective Actions Planned None l

EXTENT OF EXPOSURE OF INDIVIDUALS TO RADIATION OR TO RADIOACTIVE MATERIALS None LESSONS LEARNED Although preventive maintenance guidance for solenoid valves that are in a fail-safe design does not l

specify periodic replacement of solenoid valves, periodic replacement is desirable in this application l

to prevent the pressure transient that is experienced when the discharge block valve closes l

inadvertently from a solenoid failure.

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