ML20168A720

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Final ASP Analysis - Rancho Seco (LER 312-76-015)
ML20168A720
Person / Time
Site: Rancho Seco
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1976-015-00
Download: ML20168A720 (4)


Text

PRECURSOR DESCRIPTION AND DATA NSIC Accession Number:

120995 Date: November 11, 1976

Title:

Suction Valves to Decay Heat Pumps Fail to Open at Rancho Seco The failure sequence was:

1. During testing, neither sumnp isolation was applied.

valve opened when an open signal

.Corrective action;

1. The valves were moved manually and then cycled electrically.. The bypass switches for the valve torque switches-was-adjusted to permit more motor turns before the bypass switches difopped. out.

Design purpose of failed system or component:

1. The valves provide for fluid flow from the sump to the low pressure and high pressure recirculation systems and the building spray system (while in the recirculation mode) following a LOCA.

Unavailability of system per WASH 1400:

  • low pressure recirc:

1.3 x 10-2 /D high pressure recirc:

9 X 10-3/D Unavailability of component per WASH 1400:

  • motor operated valve, failure to operate.

1 x 10-3/D UnavailabilitieQ are in units of per demand D-1.

Failure rates are in units of per hour HR-T

Potential Severe core Damage No No No -

No LOCA and unit in shutdown.

NSIC 120995 -

Actual Occurrence for Failure of Both Suction Valves to Decay Heat Pumps from Emergency Sump at Rancho Seco

Small Reactor Auxiliary

]High Low Pressure LOCA Trip Feedwater and

Pressure, Recirculation Secondary jInjection and LPR/HPI Heat Removal Cross-Connect Potential Severe Core Damage Sequence No.

2 3

4 5

6 7

NSIC 120995 -

Sequence of Interest for Both Sump Suction Valves to Decay Heat Pumps Fail to Open at Rancho Seco

CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUMBER-120995 DATE OF LER:

November 22, 1976 DATE OF EVENT:

November 11, '1976 SYSTEM INVOLVED:

Decay heat COMPONENT INVOLVED:

Pumps CAUSE:

Switch setting incorrect.

SEQUENCE OF INTEREST:

LOCA ACTUAL OCCURRENCE:

Valves fail to open for decay heat system.

REACTOR NAME: Rancho Seco DOCKET NUMBER:

50-312 REACTOR TYPE:

PWR DESIGN ELECTRICAL RATING:

918 MWe REACTOR AGE:

2.1 yr VENDOR:

B&W ARCHITECT-ENGINEERS:

Bechtel OPERATORS:

Sacramento Municipal Utility District LOCATION:

.25 mi1les SE..of. Sacramento, CA DURATION:

360(a) hours PLANT OPERATING CONDITION:

Shut down.

SAFETY FEATURE TYPE OF FAILURE:

(a) inadequate performance; (b) failed to start; QDmade inoperable; (d)

DISCOVERY METHOD:

During test.

COMMENT:

Bypass switches for torque switches were dropping out before valve disc cleared seat resulting in torque switch stopping valve movement.