ML20168A720

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Final ASP Analysis - Rancho Seco (LER 312-76-015)
ML20168A720
Person / Time
Site: Rancho Seco
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1976-015-00
Download: ML20168A720 (4)


Text

uction Valves to Decay Heat Pumps Fail to Open at Rancho Seco re sequence was:

g testing, neither sumnp isolation valve opened when an open signal pplied.

e action; alves were moved manually and then cycled electrically.. The bypass hes for the valve torque switches-was-adjusted to permit more motor before the bypass switches difopped. out.

rpose of failed system or component:

alves provide for fluid flow from the sump to the low pressure and pressure recirculation systems and the building spray system (while e recirculation mode) following a LOCA.

ility of system per WASH 1400:

  • low pressure recirc: 1.3 x 10-2 /D high pressure recirc: 9 X 10-3/D ility of component per WASH 1400:
  • motor operated valve, failure to operate. 1 x 10-3 /D vailabilitieQ are in units of per demand D-1 . Failure rates are in per hour HR-T

core Damage No No No - No LOCA and unit in shutdown.

NSIC 120995 - Actual Occurrence for Failure of Both Suction Valves to Decay Heat Pumps from Emergency Sump at Rancho Seco

Small Reactor Auxiliary ]High Low Pressure Potential Sequence LOCA Trip Feedwater and Secondary Heat Removal jInjection Pressure, Recirculation and LPR/HPI Cross-Connect Severe Core Damage No.

2 3

4 5

6 7

NSIC 120995 - Sequence of Interest for Both Sump Suction Valves to Decay Heat Pumps Fail to Open at Rancho Seco

CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS CCESSION NUMBER- 120995 LER: November 22, 1976 F EVENT: November 11, '1976 INVOLVED: Decay heat NT INVOLVED: Pumps Switch setting incorrect.

E OF INTEREST: LOCA OCCURRENCE: Valves fail to open for decay heat system.

NAME: Rancho Seco NUMBER: 50-312 TYPE: PWR ELECTRICAL RATING: 918 MWe R AGE: 2.1 yr B&W CT- ENGINEERS: Bechtel RS: Sacramento Municipal Utility District N: .25 mi1les SE..of. Sacramento, CA N: 360(a) hours OPERATING CONDITION: Shut down.

FEATURE TYPE OF FAILURE: (a) inadequate performance; (b) failed to start; QDmade inoperable; (d) ______

ERY METHOD: During test.

T: Bypass switches for torque switches were dropping out before valve disc cleared seat resulting in torque switch stopping valve movement.