ML20168A714

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Final ASP Analysis - Point Beach 1 (LER 266-74-LTR)
ML20168A714
Person / Time
Site: Point Beach 
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1974-LTR
Download: ML20168A714 (4)


Text

PRECURSOR DESCRIPTION AND DATA NSIC Accession Number:

90421 Date:

April 17, 1974

Title:

Auxiliary Feed Pump Suction Strainers Clogged at Point Beach I The failure sequence was:

1. With Unit 1 in a cooldown, the "A" motor-driven AFW pump did not-*provide adequate flow.
2. An in-line suction strainer, of which the operators were unaware, was found to be 95% plugged.
3. A similar strainer, similarly plugged, was found in the suction line of the "B" motor-driven AFW pump.
4. A partially plugged strainer was found in the suction lines of both units turbine-driven pumps.

Corrective action;

1. All the strainers were removed.
2. Other piping systems were examined-to determine if other unidentified strainers existed.

Design purpose of failed system or component:

1. The auxiliary feedwater pumps provide water to the steam generators for reactor cooling in the event the main feedwater system is not operable.

Unavailability of system per WASH 140G:

  • auxiliary feedwater:

2.5 X 10-4 (start + 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />)

Unavailability of component per WASH 1400:

  • strainers, not included 1-pumps, failure to run:

3 X1

/hr.

kUnava ilabilitie~ are in units of per demand D-1.

Failure rates are in units of per hour HR-T.

Unit 1 in cooldowTI Motor-driven AFW Motor-driven AFW Turbine-driven AFW Unit 2 status pump A fails to PUMP B suction pump suction unknown deliver adequate strainer clogged strainer partially flow to Unit 1 clogged (applicable due to clogged to both unit turbine-suction strainer driven pumps)

Potential Severe Core Damage No -

offsite power for main feed pumps available No No No NSIC 90421 -

Actual Occurrence for Auxiliary Feed Pump Suction Strainers Clogged at Point Beach 1 & 2

Potential Severe Core Damage Sequence No.

Nn 1

No Yes 2

3 Yes 4

No 5

4.

- I~A No Yes 6

7 I14 (.')

,Yes 8

No 9

No Yes 10 11

~(F)

Yes 12 Yes 13 NSIC 90421 -

Sequence of Interest for Auxiliary Feed Pump Suction Strainers Clogged at Point Beach I & 2

  • Use of HPI following AFW failure not included in mitigation procedures.

CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUIMBER:

90421 DATE OF LER:

April 17, 1974 DATE OF EVENT:

April 7, 1974 SYSTEM INVOLVED:

Auxiliary feedwater COMPONENT INVOLVED:

AFW pump strainers CAUSE:

Strainers plugged SEQUENCE OF INTEREST:

Loss of feedwater ACTUAL OCCURRENCE:

Inoperable AFW pumps during plant cooldown.

REACTOR NAME:

Point Beach 1 DOCKET NUMBER:

50-266 REACTOR TYPE:

PWR DESIGN ELECTRICAL RATING:

497 MWe REACTOR AGE:

3.5 yr VENDOR:

Westinghouse ARCHITECT-ENGINEERS:

Bechtel OPERATORS:

Wisconsin Electric Power Co.

LOCATION:.15 miles northiof Manitowoc, Wisc.

DURATION:

360(a) hours PLANlT OPERATING CONDITION:

Unit 1 in cooldown SAFETY FEATURE TYPE OF FAILURE:

(a) inadequate performance; (b,) failed to start; (2)made inoperable; (d)__________

DISCOVERY METHOD:

during operation

COMMENT, The affected AFW pumps provide auxiliary feedwater for both units.

Monthly tests failed to reveal strainers because test was run at shutoff head -

the only flow was through a I" ID bypass line & this low flow masked the plugged strainer.