ML20168A589

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Final ASP Analysis - Palisades (LER 255-72-086)
ML20168A589
Person / Time
Site: Palisades 
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1972-086-00
Download: ML20168A589 (4)


Text

PRECURSOR DESCRIPTION AND DATA NSIC Accession Number:

71694 Date:

May 26, 1972

Title:

Loss of Offsite Power at Palisades The failure sequence was:

1. With the plant in a hot standby condition, the left channel safety injection system test button was pushed to initiate a quarterly test.
2. This resulted in a loss of offsite power due to the spurious operation of a differential relay on the 1-2 startup transformer.

The actuation of the relay was due to unbalanced sensing 6urrents from a current transformer -

a result of the incompatibility of the installed current transformer with the 345 KV -

2.4 Ky step-down situation.

Corrective action:

The differential relays were removed from startup transformers 1-1 and 1-2.

High-side overcurrent and instantaneous overcurrent relays were installed.

Design purpose of failed system or component:

The differential relays provided overcurrent protection for the startup transformer.

Unavailability of system per WASH 1400:

Offsite power:

2 x 10-5 /hr Unavailability of component per WASH 1400:-

Unavailabilities are In units of per demand D-1.

Failure rates are in units of per hour HR-1.

Plant in Left Channel Loss of Offsite Diesel Gener-Diesel Generator Hot Standby Safety Injec-Power Due to ator Start Manually Syn-tion System Spurious Opera-chronized to Test Button tion of a Dif-Safeguard Buses Pushed to ferential Relay IC and ID (Due to Initiate on the 1-2 Test Button Quarterly Startup Trans-Depression)

Test former Potential Severe Core Damage No Yes Yes No NSIC 71694 -

Actual Occurrence for Loss of Offsite Power at Palisades

Loss of Turbine Emer-Auxiliary PORV PORV or High Long Offaite Generator gency Feedwater and Demanded PORV Isola-Pressure Term Power Runs Back Power Secondary tion Valve Injection Core and Assumes Heat Removal Closure Cooling House Loads Potential Severe Core Damage Sequence No.

_______________________________No No No Yes Yes No No Yes 2

3 4

5 6

7 8

9 10 11 12 13 Yes No Yes

-V..

NSIC 71694 -

Sequence of Interest for Loss of Offsite Power at Palisades

  • Not included in operating procedures

CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUMBER:

71694 DATE OF LER:

May 26, 1972 DATE OF EVENT:

may 17, 1972 SYSTEM INVOLVED:

Offsite power COMPONENT INVOLVED:

Startup transformer CAUSE:

Improperly chosen differential relay SEQUENCE OF INTEREST:

Loss of offsite power ACTUAL OCCURRENCE:

Loss of off site power during testing REACTOR NAME:

Palisades DOCKET NUMBER-255 REACTOR TYPE:

PWR DESIGN ELECTRICAL RATING:

805 MWe REACTOR AGE:

1.0 yr VENDOR: CE ARCHITECT-ENGINEERS: Bechtel OPERATORS:

Consumers Power Corp.

LOCATION: 5 miles south of South Haven, Michigan DURATION:

N/A PLANT OPERATING CONDITION: Hot standby SAFETY FEATURE TYPE OF FAILURE:

inadequate performance; (b) failed to start; (c)made inoperable; (d)

DISCOVERY METHOD:

During testing COMMENT:

The incompatible current transformer had been installed prior to criticality