ML20168A455

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Final ASP Analysis - Davis-Besse (LER 346-77-110)
ML20168A455
Person / Time
Site: Davis Besse 
Issue date: 06/16/2020
From: Christopher Hunter
NRC/RES/DRA/PRB
To:
Littlejohn J (301) 415-0428
References
LER 1977-110-00
Download: ML20168A455 (4)


Text

PRECURSOR DESCRIPTION AND DATA NSIC Accession Number:

133706 Date:

December 11, 1977

Title:

Co ntrol of Both Auxiliary Feed Pump Turbines Lost at Davis-Besse 1 The failure sequence was:

1. During testing, control over both auxiliary feedwater pump turbines was lost, rendering the pumps inoperable.
2. Control of the turbine for pump 1-1 was lost due to mechanical binding in the governor.
3.

Control of the turbine for pump 1-2 was lost due to blown control power supply fuses for the speed changer motor.

Corrective action;

1. On pump 1-1, the roll pin which was binding was repositioned, cleaned, and lubricated.
2. On pump 1-2, the blown fuses were replaced, as were two relays suspected of sticking and causing the blown fuses.

Design purpose of failed system or component:

1. The auxiliary feedwater pumps provide RCS heat removal when the main feed system is unavailable.

Unavailability of system per WASH 1400:

  • Auxiliary feedwater:

3.3 x 10-5 /1)

Unavailability of component per WASH 1400:

  • Pumps, failure to start 1 x 10-3 /D Unavailabilities are in units of per demand D-1.

Failure rates are in units of per hour HR 1 '.

Reactor in hot Auxiliary feedwater Auxiliary feedwater Auxiliary feedwater standby during pump 1-1 operable pump 1-2 operable pump required "Reactor/Turbine Trip Test" Potential Severe Core Damage No No No No Yes No NSIC 133706 -

Actual Occurrence for Control of Both Auxiliary Feed Pump Turbines'Lost at Davis-Besse 1

Potential Severe Core Damage Sequence No.

No 1

2 3

4 5

6 7

8 9

10 11 12 13 at Davis-Besse 1 NSIC 133706 -

Sequence of Interest for Control of Both Auxiliary Feed Pump Turbines Lost

  • not included in mitigation procedures

CATEGORIZATION OF ACCIDENT SEQUENCE PRECURSORS NSIC ACCESSION NUMBER:

133706 DATE OF LER:

January 3, 1978 DATE OF EVENT:

December 11, 1977 SYSTEM INVOLVED: Auxiliary feedwater COMPONENT INVOLVED:

Auxiliary feedwater pump turbines CAUSE:

Mechanical binding, blown fuses SEQUENCE OF INTEREST:

Loss of feedwater ACTUAL OCCURRENCE:

Auxiliary feedwater pumps inoperable during testing.

REACTOR NAME:

Davis-Besse 1 DOCKET NUMBER:

50-346.

REACTOR TYPE:

PWR DESIGN ELECTRICAL RATING:

906 MWe REACTOR AGE:

0.6 yr VENDOR:

Babcock & Wilcox ARCHITECT-ENGINEERS:

Bechtel OPERATORS:

Toledo Edison LOCATION:

21. iWles east 6E.Toledo, Ohio DURATION:

360(a) hours PLANT OPERATING CONDITION:

hot standby SAFETY FEATURE TYPE OF FAILURE:

(a) inadequate performance; (b) failed to start; Qin%

ade inoperable; (d) __________

DISCOVERY METHOD:

During testing COMMENT:

-