ML20154D513

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Forwards Addl Info Re Reload License Amend Request Provided in 860224 Telcon W/Util,Westinghouse & Nrc.Uprating Amend Request Will Be Submitted During Second Quarter 1987
ML20154D513
Person / Time
Site: Callaway Ameren icon.png
Issue date: 02/28/1986
From: Schukai R
UNION ELECTRIC CO.
To: Harold Denton
Office of Nuclear Reactor Regulation
References
ULNRC-1266, NUDOCS 8603060146
Download: ML20154D513 (6)


Text

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. i UNION BICTRIC COWANY 1901 Grotiot Street, St. Lou 6s Donou F scw February 28, 1986 We President Mr. Harold R. Denton, Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D. C. 20555 '

Dear Mr. Denton:

ULNRC- 1266 DOCKET NUMBER 50-483  ;

CALLAWAY PLANT ,

RELOAD LICENSE AMENDMENT REQUEST ADDITIONAL INFORMATION

References:

1) ULNRC-1207 dated 11/15/85
2) ULNRC-1227 dated 12/13/85
3) ULNRC-1247 dated 1/28/86
4) ULNRC-1258 dated 2/18/86 '
5) ULNRC-1263 dated 2/24/86 The referenced letters transmitted the reload license '

amendment request for Callaway cycin 2 along with additional information to support this request. The attachment to this letter documents additional information provided in a phone call on February 24, 1986, involving NRC, Westinghouse and Union '

Electric.

Item 1 from the attachment was identified as an item which needed to be addressed to support issuance of the Cycle 2 Amendment. It is our understanding the information provided on ,

the phone satisfies the NRC reviewers concern and this letter

  • provides documentation of the response.  ;

Items 2 and 3 of the attachment address initial draft questions raised by the NRC reviewer concerning the eventual  !

request for a power uprating for Callaway. These are documented  !

herein because of the lengthy nature of the responses, but are not considered necessary for close-out prior to issuance of the Cycle 2 Amendment. The Callaway uprating amendment request is  ;

not anticipated to be submitted until the second quarter of 1987. l If there are additional questions, please contact us.

1 Ver truly yours, j

0603060146 060220 (

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,*l Moiling Address: PO Bos 149, $f. Lou 61 MO 63166 fl I

STATF, OF !!ISSOURI )

) SS CITY OF ST. LOUIS )

Robert J. Schukai, of lawful age, being first duly sworn upon oath says that he is General Manager-Engineering (Nuclear) for Union Electric Company; that he has read the foregoing document anel known the content thereof; that he has executed the same for and on behalf of said company with full power and authority to do so; and that the facts therein stated are true and correct to the best of his knowledge, in formation and belie f.

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Dy Ro'bc r J. hukai Gener nager-Engineering Muclear SUDSCRIDED and cworn to before me this Mf ay of /ta/ , 190 h

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MTAfty I'Ut UC, $ FATE Ot latG0Jr4 MY COVtsilCN LAP:FCS APTslL 22. U8A GT. Louis COUNTY l

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o cc Gerald Charnoff, Esq. ,

1 Shaw, Pittman, Potts & Trowbridge 1800 M. Street, N.W.

I Washington, D.C. 20036 j Nicholas A. Petrick j Executive Director SNUPPS 5 Choke Cherry Road Rockville, Maryland 20850 l

l C. W. Itchl i Division of Projects and Resident Programs, Chief, Section lA U.S. Nuclear Regulatory Commission i Region III I 799 Roonovelt Road

! Glen Ellyn, Illinois 60137 i

Bruce Little i Callaway Resident Of fico i U.S. Nuclear Regulatory Commission 1 RR#1 Steedman, Missouri 65077 Paul O'Connor Office of Nuclear Reactor Regulation l U.S. Nuclear Regulatory Commission

Mail Stop 316 7920 Norfolk Avenuo Bothesda, MD 20014

! Managor, Electric Department i Minnouri Public Servico Comminnion  !

! P.O. Dox 360 j Jefferson City, Mo 65102 l

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Attachment to ULNRC- 1266 Additional Information for Cycle 2 l Reload License Amendment Request l

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1. Large break LOCA analyses were performed using the BART

! computer code. The staff SER describing review and approval l of this code is dated December 21, 1983 and is centained in l WCAP-9561-P-A. The staff approval is dependent on selection of proper nodal length and prohibits use of the grid spacer model. Following staf f review of WCAP-10484 use of the grid spacer model was permitted provided that the droplet breakup model was not included. Justify that the DART evaluation {

for Callaway utilized options and assumptions approved by 1 the staff.

Responso In the BART Evaluation Model (DART EM) used to analyze large ,

break LOCAs for Callaway, the proper nodal lengths were utilized as required by the NRC SER. One-half foot spacings were chosen for all nodes in the DART model, except around the peak power location, where the nodes were spaced 1/4 foot apart.  :

i It has been verified and confirmed that the grid spacer l model (grid rewet model) was used and the droplet breakup l model was not utilized, as required by the NRC SER. '

The above confirms that the options and assumptiens utilized i in the DART EM for Callaway were those approved by the NRC.

2. The Commission's Regulation 10CFR50.46 (a) (1) requires that ECCS cooling performance be calculated for loss-of-coolant  ;

accidents of different sizes suf ficient to provide assurance that the entire spectrum of postulated loss-of-coolant accidents are covered. In the reanalysis of loss-of-coolant accidents using DART and NOTRUMP models the peak cladding >

temperature was determined to be 2153*F for a 40% large ,

break sizo and 1299'P for a 3 inch small break size. Dreak ,

sizes smaller than these sizes Woro not examined.

Demonstrate that an adequate break spectrum has been  !

evaluated or perform additional analyses. Include split ,

breaks as well as double ended ruptures. '

Responne The limiting case break identified for Calloway l loss-of-coolant-accidentn is the CD=0.4 DECLG break, at a calculated peak clad temperature (PCT) of 2153*P. In the LOCA analyses the 0.4 discharge coefficient in the lower bound of the cold leg guillotine break spectrum which is l 8

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consistent with the use of the Moody critical flow l correlations required by 10CFR50 Appendix K. This lower '

bound limit was established based on experimental data as i described in Appendix D of WCAP-8340, " Westinghouse l Emergency Core Cooling System, Plant Sensitivity Studies,"

l and has been observed since the institution of 10CFR50 l Appendix K. .

Sensitivity studies using Westinghouse large break LOCA i evaluation models have universally demonstrated that the i limiting (cold leg) guillotine break exhibits a higher  ;

l calculated PCT than the limiting (cold leg) split break.  ;

WCAP-8565-P, " Westinghouse ECCS 4-Loop Plant (17x17)

Sensitivity Studies," provides 4-loop plant results that may be referenced for Callaway which demonstrate this behavior. ,

In the DART Evaluation Model (DART EM), SATAN and WREFLOOD j still provide system and core thermal-hydraulic boundary conditions to the rod heatup PCT computation, just as in  !

previous Westinghouse evaluation models. Note in particular [

that core flooding rates are higher in WCAP-8565-P for split  !

breaks than for the corresponding discharge coefficient guillotine breaks. Since the WREFLOOD model has changed -

very little in the DART EM, this behavior will be retained, providing a relative benefit for the split breaks. In f conclusion, the use of DART does not necessitate that split I breaks be analyzed, so the spectrum provided for Callaway is  !

adequate as in the past.

q WCAP 10,054-P-A, " Westinghouse Small Dreak ECCS Evaluation ,

Model using the NOTRUMP Code," which was provided by '

reference in the submitted text on page 15.6-16, indicaten a ,

2 inch break need not be analyzed. This is based on the fact that a 2 inch break does not lead to core uncovery and .

there is therefore no impact on PCT. Given thin and the l fact that 900* F in PCT , margin exists to the regulatory  :

limit of 2200* F, the small break spectrum provided is )

clearly adequate. i l

3. Discuss how the increase in steam generator tube plugging  !

was considered in the analysis of lons-of-coolant accidents, '

in particular the effect due to increased steam binding l during the reflooding period.  !

nosponse I r

Steam Generator Tube Plugging (SGTP) is a large break LOCA  !

ECCS perforn.ance penalty, because of the flow restriction it  ;

produces within the steam generators. This restriction inhibits maan flow through the coolant loops (i.e.,

increason nteam bending) and hinders the reflooding of the )

reactor core following a large break LOCA. This consequently resultn in higher calculated Peak Clad Temperaturns (PCTO), ao SGTP increases, as noted in WCAP-8986, " Westinghouse Portubation Technique for l Calculating ECCS Cooling Performance." t i

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SGTP levels affect the performance of calculated small break LOCA in three important aspects namely, the reduced heat

transfer area, the increased initial temperature difference between the primary and the secondary side, and countercurrent flow limit (CCFL).

During a small break LOCA only a small portion of the steam generator heat transfer area is required to provide an effective heat sink. Thus the availability of adequate steam generator heat transfer area is unaffected because of tube plugging. In an Appendix K small break LOCA analysis, the increasing temperature difference between the primary and the secondary side will disappear right after the break, '

because the secondary side pressure reaches the steam

' generator safety valve set point immediately after the break. SGTP may affect the CCFL characteristics depending l on the severity of the plugging. At a lower plugging percentage (up to about 20%), the limiting CCFL discussed in Reference 1 is still at the inclined pipe connecting the steam generator inlet plenum and hot leg. Therefore, at low plugging rates (20%), small break LOCA transients would not be affected by the tube plugging and remain non-limiting.

In the LOCA analysis for Callaway, a uniform SGTP level of

' lot was assumed, in order to accommodate a plugging level in any steam generator up to 10%. This was achieved via input

, to the Callaway large break DART EM analysis and the small j

break NOTRUMP EM analysis, including the following

1. The steam generator tube net free volume was reduced by 10%.

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2. All heat transfer areas and flow areas associated with i the steam generator tubes were reduced by 10%.
3. All pressure drops and enthalpy distributions were revised to accommodate 10% SGTP.

l Therefore 10% SGTP was properly implemented in the Calloway LOCA analysis. The calculated LOCA PCT value is valid for i SGTP levels of 10% in any steam generator and conservative

for any tube plugging level below 10%.

l REFERENCE

1. Lee, N., " Limiting Countercurrent Flow Phenomenon in Small  !
Bronk LofA Transients", Proceedings of the Specialists i Meeting on Small Dreak LOCA Analysen in LWRs, Pisa, Italy, June (1985).

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