ML20151W444

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Forwards Corrected Pages to Insp Repts 50-348/88-19 & 50-364/88-19 on 880511-0610.Due to Administrative Oversight, Pages 8 Through 12 Contained Several Grammatical Errors & Incorrect Paragraphs.Record Copy
ML20151W444
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 08/17/1988
From: Verrelli D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Hairston W
ALABAMA POWER CO.
References
NUDOCS 8808240252
Download: ML20151W444 (2)


See also: IR 05000348/1988019

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AUG 171988

Docket-Nos. 50-348, 50-364

License Nos. NPF-2 and NPF-8

(

Alabama Power Company

'ATIN:

Mr. W.. G. Hairston,.III

.

Senior Vice President-Nuclear

Operations

P. O. uox 2641

Birmingham, AL 35291-0400

Gentlemen:

SUBJECT: NRC INSPECTION REPORT NOS. 50-348/88-19 AND 50-364/88-19

This refers to the Nuclear Regulatory Commission inspection conducted by

W. H. Bradford on May 11 - June 10,is inspection was sent to you by letter

1988, of activities at your Farley

facility.

The report documenting th

dated July 7,1988.-

~'~- Due to an administrative oversight, pages 8 through 12 contained a number of

grammatical errors and incorrect paragraphs.

Corrected pages are enclosed for

insertion into the original report.

Please replace the original incorrect

pages 8 through 12 with the corrected pages.

We regret any inconveniences this

may have CuJsed.

Should you have any questions concerning this letter, we will be glad to

discuss then with you.

Sincerely,

David M. Verre111, Chief

ReactorProjectsBranch1

DivisionofReactorProjects

Enclosure:

Report pages 8-12a (Corrected)

cc w/ enc 1:

(S

. Guthrie, Executive Vice President

G

0. Woodard, Vice President -

. Nuclear Generation

(D'. N. Morey, General Manager -

JuclearGeneration

T. W. McGowan, Manager-Safety Audit

and Engineering Review

I Fulmer, Supervisor-Safety

Atdit and Engineering Review

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AUC 171988

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IR 50-248,264/88-19

Corrected 8/11/88

a.

FNP-0-AP-1, Development, Review, and Approval of Plant Procedures,

Section 5, Procedures Safety Evaluation.

Section 5 of this administrative procedure related to safety evalua-

tions required during development, review and approval of plant

procedures and revisions to procedures.

A Nuclear Safety Evaluation

' Check List is prepared during procedure preparation by the individual

responsible for the preparation.

This check list is used to

evaluated whether or not a 10 CFR 50.59 evaluation is required.

Also, the check list is used to determine whether or not PORC review

and NRC approval is required prior to procedure implementation.

Paragraph 5.2 states when a written description safety evaluation is

needed.

Included within the description are the following:

Background, References, Bases and Conclusion.

However, there is no

amplifying information in paragraph 5.2

other than the listing of

these items.

As noted during the exit Interview, the listing should

contain additional guidance, especially for sub-paragraph 5.2.3,

"Bases."

Such guidance might include statements relating to why the

change does not constitute an unreviewed safety question.

The check

list Part 8, "Safety Evaluation," paragraph 4.1 throuch 4.7, lists

only the specific criteria.

Therefore, the support ng safety

evaluation should state clearly and concisely why the question 'yes

or no" can be answered.

The licensee management stated that the comments would be considered,

b.

FNP-0-AP-8, Design Modification Control Section 5, Production Change

Requests, Section 6.3, Safety Evaluation

Section 6.3 of this administrative procedure requires that all design

changes shall have a safety evaluation check list completed to

determine the 10 CFR a]plicability.

The check list is very similar

to the check list in F4P-0-AP-1 used for procedures.

The check list

is used for design change (PCNs) or minor departures.

Paragraph 6.3.2 requires safety evaluation check lists and safety

evaluations to be provided by the design organization responsible for

design development.

However, no instruction are included on the

detail necessary to show a clear basis of the determination that an

unreviewed safety question exists.

The procedure needs to be brought

u) to the standards used in FNP-0-AP-1, and improved as described

a>ove for FNP-0-AP-1.

Licensee management stated that the comments would be considered,

c.

PCN 84-2609, Upgrade of Primary Meteorological Tower Instrumentation

A discussion of the PCN was conducted with the Plant Technical

Manager and the Supervisor of Environmental and Emergency Planning

and an Evaluation Engineer of the Plant Modifications Group.

The

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AUG 171988

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9

IR 50-248,264/88-19

Corrected 8/11/88

modification is to improve the reliability of the existing

meteorological data system as described in the FSAR Section 2.3.3.

An older system of instrumentation is replaced with Het One

instruments.

In addition, backup wind speed and direction

instruments are added to the 150 foot level.

Replacement instruments

are to meet the requirements of Regulatory Guide 1.23 as well as the

accuracy requirements of FSAR, Table 2.3-10.

Revision 1 to PCN

84-2609, safety evaluation noted that addition of the backup

instruments is to provide backup data for temperature differential

between the 35 foot and 200 foot elevation.

The safety evaluation

check list notes that FSAR, Table 2.3-10 will require a change.

PORC minutes for the 1522nd meeting held on May 13, 1986, were

reviewed.

The PORC reviewed the design changes and safety

evaluations associated with this change.

The PORC determined that no

unreviewed safety questions were involved and recommended approval.

The licensee noted that the FSAR will be updated in the annual

updated scheduled for July 1988.

As noted in the Revision 0 to PCN

84-2609, safety evaluation, instrumentation is intended to3revent the

a Technical Specification change would be

required if the additional

plant from entering an LCO upon failure of the one-channe'

windspeed

and direction at the 150 foot elevation.

At the exit interview, the

licensee was advised that Technical Specification Table 3.3-8 appears

to need updating for consistency with the Air Temperature Difference

Instrument.

The licensee agreed to consider the need for these changes.

d.

PCN 86-32496, Erection of Solidification and Dewatering Facility

An interview was conducted with the Plant Technical Manager, the

Health Physics Manager, and Engineer of the Plant Modification Group.

performed by Southern Company Services, Inc.The modifications are

study

The study,

Criteria for Solidification / Dewatering Building for Farley Nuclear

Plant," dated October 31, 1985, was reviewed.

In addition, PORC

meeting minutes of August 8,1986, and March 10, 1987, for design

change Revisions 0 and 21 were reviewed.

In each set of minutes, the

PORC determined that no unreviewed safety question was involved.

Prior to this modification, the solidification and dewatering

process was performed in an open ared between the refueling water

storage tanks.

Temporary connections were made each time the

processes were performed.

The new permanent structure (with all

connections to reactor plant systems) allows the processes to be

performed more safely, more efficiently, and with improved radio-

active protection measures.

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IR 50-248,264/88-19

Corrected 8/11/88

The building (49' wide, 82' lor.g, 40' high) also provides storage

during

refueling

(including studbolt storage), waste and

decontamination equipment storage, solidification equipment storage,

contaminated oil, paint, and scaffold storage.

Four spent resin

liner pits with remote operating controls and view ports, and

supercompaction equipment for dry active waste are housed in the new

facility.

Airborne radioactivity is processed and monitored in the

Unit 1 Auxiliary Building HVAC System.

The facility was designed

against collapse due to wind, tornado and seismic loads combinations

per Regulatory Guide 1.29, Revision 1, and the FSAR.

Piping and

valves were designed, fabricated, inspected, and tested per

ANSI B31.1 as required by Regulatory Guide 1 ?43, Revision 1.

The "Safety Evaluation for Solidification / Dewatering Facility for

Farley Nuclear Plant (PCN 86-0-3496) Revision 3 dated August 1986,

paragraphtitled"Sup)1ementaryNRCGuidanceRev}ew",statedthatthe

facility was reviewec against NRC guidance of IE Circular 80-18 and

Generic Letter No. 81-38.

Subparagraph C, "10 CFR Part 50" notes

that the design and operation of the facility is in compliance with

10 CFR 50.59 and no unreviewed safety questions nave been identified.

Evaluation of potential exposures from direct radiation sources and

potential radioactivity releases was given in subsequent paragraphs.

The evaluation included discussions of potential liquid and gaseous

events and concluded that:

(1) Consequences of a liquid spill are expected to be significantly

less than the open air process previously used.

(2) Consequence of dropping the resin filled liner with a subsequent

airborne release will be less that the open-air configuration

previously used.

(3) There is no significant potential for gaseous release due to

fire or following a liquid spill.

(4) Potential for a gaseous release will be less while filling the

liner and will be minimized by use of the pressure blower

taking suction from the closed pit and exhausting to the Unit 1

Auxiliary Building radwaste vent system.

The evaluation goes on to state that in view of this evaluation, the

facility is not a potential release pathway per the GDC-64 criteria.

The audit indicates that the licensee personnel who were interviewed,

as well as the procedures and safety evaluations performed, followed

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licensee guidance and were in conformance with the intent of 10 CFR

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50.59.

No items of concern were noted.

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IR 50-248,264/88-19

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e.

PCN 887-0-4384, Replacement of Existing Commercial Grade Agastat

Relay with Seismically Qualified Relay

An interview was conducted with the Plant Technical Manager and

Electrical Maintenance Department Group Supervisor.

The General

Office production change request PCR 87-0-4384, the Nuclear Safety

Evaluation Checklists (Revisions 1 to 4) and the minutes for PORC

Meeting No. 1711 dated August 4, 1987 were audited.

The initial PCN related to replacement of Agastat Model 7012 PA

(commercial grade) in Unit 2 600V load center 2E, a safety related

load center.

Also, Agastat Model 7022 (commercial grade) relays

throughout the plant were evaluated for replacement.

The Naclear

Safety Evaluation Checklist, Revision 1, indicates that a ciange to

the plant as described in the FSAR is "yes."

For this reason, a

safety ) evaluation was performed.FSAR Figure 8.3-10 and 8.3-13

(Unit 1

required changing.

A figure will be added to the FSAR for

Unit 2 specifying the correct relay model.

The safety evaluation concludes that the new relay is qualified to

a higher acceleration and when installed will not affect the load

center's original seismic qualification.

One of the actual relays

replaced was examined.

Licensee personnel advised that the relays

(commercial or seismically qualified) are identical to all intents

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and purposes.

The Nuclear Safety Evaluation Checklist for Revision 4

to the PCN was reviewed for the replacement of other relays at 600V

Emergency Load Center 1A, 10, 2A, and 20.

Similar safety conclusions

were made.

No items of concern were noted requiring licensee action,

f.

Procedure FNP-0-AP-76, Revision 4, Authorize Use of Morpholine /Buric

Acid in Secondary Water Chemistry Control System

An interview was conducted with the Plant Technical Manager and the

Chemistry and Environmental Group Supervisor relating to secondary

water chemistry control changes of Revision 4, "Conduct of Opera-

tions - Chemistry and Environmental Group."

The aaplicable safety

evaluation check list indicated "yes" to the question; "A change to

the plant as described in the FSAR?" PORC meeting minutes No. 1760

dated November 3,1987, and the associated safety evaluation were

reviewed.

Licensed Condition 2.C(3)(g) requires the licensee to implement a

secondary water chemistry monitoring program.

The program had been

inspected most recently on August 17-21, 1987, as described in NRC

Inspection Report No. 87-21, dated September 10, 1987.

The inspector

concluded at the time, that the licensee was aware of concerns

relating to maintaining the integrity of the primary coolant pressure

boundary as well as the remainder of the secondary cooling system.

AUS 171988

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IR 50-248,264/88-19

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FSAR Section 10.3.5, Water Chemistry, contains a brief description of

the secondary system water chemistry controls previously used to

minimize corrosion of the steam generator (SG) internals.

This FSAR

section will require revision to describe the use of morphpoline/

boric acid chemistry control.

The previous all volatile treatment

(AVT) used ammonium hydroxide for pH control and hydrazine for oxygen

scavenging as recommended by the SG Owner's Group.

More recently,

the NSSS vendor had recommended the use of boric acid injection for

control of SG tube denting.

Boric acid was used on Unit 1 since

1983, and on Unit 2 since 1986.

FNP-0-AP-76, Revision 4, reflects changes in details of the proce-

dures.

AVT, AVT/ morpholine, and AVT/ morpholine / boric chemistry

specifications were added.

It provided for a formal documentation

memorandum of the selected secondary chemistry program.

The 10 CFR 50.59 safety evaluation Bases section discusses the safety risks in

handling morpholine, the environmental impact (Alabama Department of

Environmental Management a) proved), corrosive effects of morpholine

on 31 ant components, contribution to the total organic carbon, effect

on )1owdown demineralizers, effect on laboratory analysis for silica,

and effect on in-line instruments.

The conclusion is that implemen-

tation of morpholine / boric acid treatment dose not constitute an

unreviewed safety question as defined by 10 CFR 50.59.

However, the safety evaluation dose not specifically address the

three criteria for a determination whether of not NRC approval must

be obtained before implementing the change.

The safety evaluation of

the licensee clenly determined that the use of morpholine was safe.

A Westinghouse Nuclear Safety Evaluation Check List SECL-87-501, in

the audit material clearly concludes that "the previously analyzed

consequences of excessive corrosion (e.g. , tube rupture, feedline

break, and turbine missiles) have act been increased nor has the

probability of such postulated events been previously analyzed.

The

safety factors used in design evaluations of the components including

the pressure boundary stress analysis rione in accordance with the

ASME Boiler and Pressure Vessel Code remain valid.

Therefore, the

margin of safety has not been reduced."

During subsequent conversations with the licensee, use of evaluations

for safety and separate evaluations for 10 CFR 50.59 determinations

were discussed.

A review against the criteria in 10 CFR 50.59 does

not determine that a change is safe, but that the change does or does

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not require NRC approval prior to implementation.

Both reviews and

evaluations important and necessary.

Training in this area for

personnel examining the 10 CFR 50.59 determinations does not exist

today at Farley site.

Consideration for such training was

recommended.

AUG 17 gggg

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10.

Unit 1 Startup from Refueling (71711)

The inspectors verified that adequate administrative procedures were

available to assure that systems disturbed or tested during the refueling

outage were returned to operable status before plant startup.

Accessible

portions of the auxiliary feedwater system and chemical and volume control

system were inspected to vsrify:

valves were in correct alignment;

hangers and supports were made up properly; major components were properly

labeled, lubricated, cooled and no visible leakage exits; breakers were

properly aligned; instrumentation calibration dates were current; support

systems essential

to system perfermance were operational; and,

housekeeping and cleanliness were adequately maintained.

Portions of

these systems had been disturbed during the outage, but based on this

inspection these systems appeared to have been returned to service in

accordance with the applicable procedures.

Refer to

information on auxiliary feedwater pump lubrication. paragraph 4.b for

No discrepancies

were identified.

Portions of the unit startup operations were witnessed by the resident

inspectors and a regional based inspector.

The ins)ectors verified that

the required core physics tests were performed anc that the startup

activities were conducted in accornance with the TS requirements.

Refer

to NRC report 348,364/88-20 for additional comments on this area.

No violations or deviations were identified.

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