ML20151C193

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AO 20-75:on 751218,30-inch Ventilation Pipe Contacted by Power Showel During Const Activity.Caused by Inadequate Administrative Controls Re Preparation & Review of Const Activity.Work Activity Stopped.Engineering Review Requested
ML20151C193
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 12/19/1975
From: Sewell R
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
AO-20-75, NUDOCS 8103090153
Download: ML20151C193 (2)


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!~ VU AGCY WHEA 1 -UUA PT-M35.513P i, n

'AS l ROKQUWOLK0 APE 0YYRA353002)PD 12/19/75 1715 LJ u ' ;

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llE 7.CZC O'02 DLY JACKSON t1ICH. 12/19/75 l j 7, I: PXS J G KEPPLER g;{

US'!RC (FORMERLY AEC)

GLEN ELLYN, IL' i

i THIS VILL CONFIRI1. THE TELECON BETUEEt!'D E DE 1100R,' BIG ROCK POIt'T

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PLANT AND..MR D HUNTER, USNRC, THIS MORNINC.

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REPORT.-No'- A0-20-75 DOCKET 50-155 LJ,!

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REPOPT DATE - DECEMDER'19, 1975 (b

OCCt[RMENCE DATE ' DECEMBER-18,-1975 c'I i 28.

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FACILITY - BIG ROCK POINT PLANT "o n IJ D 4.

IDENTIFICAT10t10F OCCURRENCE - INADEQUATE PREPAT;ATION AND REVIEU p

OF CONSTRUCTION ACTIVITY.-

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' CONDITIONS PRIOR TO'0CCURRENCE

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DESCRIPTION OF OCCURRENCE - A' CONSTRUCTION CREV USING A POUER I.i

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SHOVEL'VAS DIGGING IN THE AREA BETVEEN THE TURDINE CUILDINC /!!D l

[if REACTOR CONTAINMENT AND CONTACTED-A 3C-INCH VENTIl.ATION P1FE AT A b

i DEPTH OF ABOUT 2 FEET BELOV THE SUHFACE.

ONLY SUPEHFICIAL DAMAGE TO THE PIPE' OCCURRED. - THE V0P.K ACTIVITY. VAS STOPPED PENDIN3 A KEVIEV h.h j

OF THE PROJECT.

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THIS ' DOCUMENT CONTAINS POOR QUALITY PAGES I

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DESIG'JATION OF APPARENT CAUSE 0F OCCURRENCE - FAILURE OF ADMIT;IS-(t' TRATIVE CONTROLS PER SECTION 7.2.2.1.3 A(1)G OF THE TECH SPECS.

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MhLYSIS OF OCCURRENCE - A WORK PACKAGE COVERING THE EXCAVATIO"

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I, PROJFCT DID NOT EXIST.

THE DRAVINGS USED BY Tile CONTRACTOR DID NOT IDENTIFY ANY INTERFERENCES AND ONLY SHOUED T){E COMPLETED STRUCTURE

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To u.E INSTALLED SUBSEQUENT TO T)(E EXCAVATION.

AN EVALUATION DY Tl!E PLM'T STr.FF HAD NOT BEEN CONDUCTED AND REVIEWED AS REQUIhED BY PLANT

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ADMI'ISi!.ATIVE PT,0CEDURES.

SEVEFtAL SAFETY-RELATED BUNIED SYSTENS

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HWE SUBSEQUE'!TLY BEEN IDENTIFIED 04 PLANT DRAWINGS IN THE EXCAVATIO::

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AREA MJD AN EV ALUATION' 0F THE INTEGRITY OF T}iESE SYSTE!;S VILL BE 1:EE g__

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COPRECTIVE ACTION - UORK ACTIVITY WAS STOPPED AND NEADBY BUT.IED i

LINES UILL DE PF.0TECTED FROM FhEEZIN3.

ENGINEET.ING REVIEU HAS BEEN I

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REQUESTED THROU3H THE CCNT3 ACTOR BEFORE PROCEEDING WITH WORK.

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