ML20149D582

From kanterella
Jump to navigation Jump to search
Forwards Insp Rept 50-285/97-09 on 970423-0610.Violations Noted But Not Cited & Being Considered for Escalated Enforcement Action.No Response Re Violation Required at This Time
ML20149D582
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 06/17/1997
From: Howell A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Gambhir S
OMAHA PUBLIC POWER DISTRICT
Shared Package
ML20149D586 List:
References
50-285-97-09, 50-285-97-9, FACA, NUDOCS 9707170185
Download: ML20149D582 (4)


See also: IR 05000285/1997009

Text

r

o

,

yp%

L

/

,

l-

l

' June 17,1997

!

EA 97-280

!

.

~

l

y'

S. K. Gambhir, Division Manager'-

!

_

_ . Production Engineering

'

'

Omaha Public Power District

Fort Calhoun Station FC-2-4 Adm.

. P.Oi Box 399

~ Hwy. 75 - North of Fort Calhoun

Fort Calhoun, Nebraska 68023-0399

,

,

i

? SUBJECT: NRC INSPECTION REPORT 50 285/97-09

1

,

i

Dear Mr. Gambhir:-

'

' An NRC inspection was conducted April 23 through June.10,1997, at your Fort Calhoun

.

Station reactor facility. The enclosed report presents the scope and results of that.

'i

inspection.

s

!

,

The inspection focused on the causes, circumstances, and corrective actions associated

with the April 21,1997, extraction steamline rupture at Fort Calhoun Station.- The

'

inspection results indicated that you did not have in place an effective program for

monitoring the condition'of certain plant piping systems within the scope of 10 CFR 50.65.- Consequently, a catastrophic rupture of a large radius elbow in the extraction

steam piping occurred, which resulted in a plant transient and significant challenge to the -

operators'. ' Additionally, this event posed a significant personnel hazard and resulted in a

L

. reduction in the station fire protection capabilities. The NRC views this as a significant

event. We are particularly concerned because it is our belief that ample industry-wide

' operating experience was available to nuclear licensees such that the occurrences of

,

l

. events such as this are avoidable ; However, the overall operator respanse to this event

~

was identified as a strength.

b

Based on.the results of this inspection, one apparent violation was identified and is being

considered for escalated enforcement action in accordance with the " General Statement of

.

Policy and Procedure for NRC Enfcrcement Actions" (Enforcement Policy), NUREG 1600.

L

Accordingly, no Notice of Violatiore is presently being issued for this inspection finding.

(

In addition, please be advised that the number and characterization of apparent violations

E

. described in the enclosed inspection raport may change as a result of further NRC review.

' Members of our staff have been in coretact with you, in order, to schedule a predecisional'

'

Jenforcement conference to discuss this apparent violation. The decision to hold a

j

.predecisional enforcement conference 'does not mean that the NRC has determined that a

violation has occurred or that enforcement action will be taken.' This conference is being

.

held to obtain information to enable the NRC to make an enforcement decision, such as a

'

'

common understanding of the facts, root causes, missed opportunities to identify the

,

! apparent. violation sooner, corrective actions, significance of the issues and the need for -

i,

"

~ lasting and effective corrective' action. In addition, this is an opportunity for you to point

.out any. errors in our inspection report and for you to provide any information concerning

! \\

,

l.

. .-9707170185 970617 '

w

1

( ',

l

gDR

ADOCK 05000295

m'

lL

PDR

k

m

4

  1. S..

-

r

._ . .

. ..

- ~ . . - -,

. .. . - . ._~

_,-

- . _ _ ..

. - - -

. . - - - . . .

.

-..

!'

I

.t

.

!

!

your perspectives on 1) the severity of the violation, 2) the application of the factors that

the NRC considers when it determines the amount of a civil penalty that may be assessed

in accordance with Section VI.B.2 of the Enforcement Policy, and 3) any other application

'of the Enforcement Policy to this case, including the exercise of discretion in accordance

.

. with Section Vll. .in particular, for this case, your views on the programmatic nature of the

'

erosion / corrosion deficiencies and the extent to which the event complicated recovery

- from the transient, would be important. This conference will be open to public observation

l

!:

in accordance with a recent change to the enforcement policy (61 FR 65088).

-

You will be advised by separate correspondence of the results of our deliberations on this

l

'

matter. No response regarding the apparent violation is required at this time.

'

.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter

- and its enclosure will be placed in the NRC Public Document Room (PDR).

'

Should you have any questions concerning this inspection, we will be pleased to discuss

them with you.

Sincerely,

l

l

J

DDC for

Arthur T. Howell lil, Director

Division of Reactor Safety

Docket No.: 50-285

License No.: DPR-40 -

R

Enclosures:

l-

NRC Inspection Report

50-285/97-09

cc w/ enclosures:

James W. Tiils, Manager

)

Nuclear Licensing

l

l'

Omaha Public Power District

l

Fort Calhoun Station FC-2-4 Adm.

l

P.O. Box 399

[

Hwy. 75~- North of Fort Calhoun

"

Fort Calhoun, Nebraska 68023-0399

i

i

'

. James W. Chese, Manager

' Fort Calhoun Station -

u

'

P.O. Box 399

Fort Calhoun, Nebraska 68023

i-

j-

Perry D. Robinson, Esq.

l

Winston & Strawn

i

- 1400 L. Street, N.W.

..

--

- - . .

_

_ . -

_-

. - -

.

.

.

.

- . . . . _ ...

.~.

-

.

. -

. - . _ .

_ . - -.

..

.

P.

l

.-

,

Washington, D.C. 20005-3502

. Chairman

,

L

Washington County Board of Supervisors

!

Blair, Nebraska 68008.

Cheryl Rogers, LLRW Program Manager

Environmental Protection Section

Nebraska Department of Health

i

301 Centennial Mall, South

P.O. Box 95007

Lincoln, Nebraska 68509-5007

.

.

T

D

&

>

>

l

.

__

_

..

..

.

,

i

I

J

E-Mail report to T. Boyce (THB)

E-Mail report to NRR Event Tracking System (IPAS)

E-Mail report to Document Control Desk (DOCDESK)

E-Mail report to Richard Correia (RPC)

E-Mail report to Frank Talbot (FXT)

E-Mail report to Phil Qualls (PMQ)

'

bec to DCD (IE01)

bec distrib. by RIV:

Regional Administrator

DRS-PSB

. DRP Director

MIS System

Branch Chief (DRP/B)-

RI V File

Project Engineer (DRP/B)

Branch Chief (DRP/TSS)

Resident inspector

G. F. Sanborn, EO

W. L. Brown, RC

J. Lieberman, OE, MS: 7-H5

OE:EA File, MS: 7-H5

P. A. Boehnert, ACRS

DOCUMENT NAME: R:\\_FCS\\FC709RP.JS

To receive copy of document irulicate in box: "C" = Copy without enclosures "E" = Copy with enclosures "N" = No copy

RIV:SRA

E

RI:MB

E

RAE:FPES

SRl:PBB

C:MB

E

NRR

JLShackelford/imb

CAClark

PMQualls

WWalker

DAPowers

06/16/97

06/13/97

06/16/97

06/16/97

06/16/97

EO

D:DRP

D:DRS

GSanborn

TPGwynn

ATHowell ill

06/16/97

06/17/97

06/17/97

OFFICIAL RECORD COPY