ML20147H013

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Monthly Operating Rept for Dec 1987
ML20147H013
Person / Time
Site: Limerick Constellation icon.png
Issue date: 12/31/1987
From: Alden W, Gropp R
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
NUDOCS 8801220218
Download: ML20147H013 (6)


Text

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AVERAGE DAILY UNIT P0HER LEVEL DOCKET NO. 50 - 352 UNIT LIMERICK UNIT 1 DATE JAPAJARY 15, 1988 COMPANY PHILADELPHIA ELECTRIC COMPANY R. H. GROPP TECHNICAL ASSISTANT LICENSING SECTION MJCLEAR SUPPORT DEPARTMENT TELEPHONE I215) 841-5058 MONTH DECEPBER 1987 DAY AVERAGE DAILY PONER LEVEL DAY AVERAGE DAILY PONER LEVEL

( P94E-NET 1 ( P94E-NET )

1 1029 17 1043 2 1019 18 1038 ,

3 1034 19 1038 4 1030 to 1039 5 1035 21 1034 6 1052 22 1044 7 1035 23 1042 8 1034 24 812 9 1030 25 800 i

10 1027 26 809 11 1040 27 937 12 1035 28 1039 l

l 13 1018 29 1061 14 1944 30 1002 15 1034 31 1027 16 1041 "1-} ; p-((/

8801220218 871231

//

PDR ADOCK 05000352 R DCD /

OPERATING DATA REPORT l

l 1

DOCKET No. 50 - 352 )

..........._____............. I DATE JANUARY 15, 1988 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY R. M. GROPP TECHNICAL ASSISTANT l

LICENSING SECTION PAJCLEAR SUPPORT DEPARTMENT TELEPHONE 1215) 841-5058 OPERATING STATUS

1. UNIT HAMEt LIMERICK LNIT 1 l NOTES THE UNIT EXPERIENCED ONE l

...... _________........... ____ _ l l

2. REPORTING PERIODI DECEMBER, 1987 l FORCED LOAD REDUCTION. l

....._____................. l l

3. LICENSED THERMAL PONER(MNT): 3293 l l l l O. NAMEPLATE RATING (GROSS MHEli 1138 l l

...........___. l l

5. DESIGN ELECTRICAL RATING INET HME) 1055 l l l l
6. MAXIMUM DEPENDA8L! CAPACITY (GROSS MHE): 1092 l l l l
7. MAXIMUM DEPENDA8LE CAPACITY (NET HHEli 1D55 l l
8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS NUPSER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONSI
9. P0HER LEVEL TO HHICH RESTRICTED, IF ANY (NET P94Eli
10. REASONS FOR RESTRICTIONS, IF ANY' l

THIS MONTH YR-TO-DATE CUMULATIVE

11. b0URS IN REPORTING PERIOD 744 8,760 16,776 l

l

12. NUMBER OF HOURS REACTOR HAS CRITICAL 744.0 6,151.0 12,868.0
13. REACTOR RESERVE SHUTDOHN HOURS 0.0 0.0 0.0 l

l

14. HOURS GENERATOR OH LINE 744.0 5,926.7 12,562.7
15. UNIT RESERVE SHUTDOHN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MKH) 2,377,260 17,298,219 38,896,381
17. GROSS ELECTRICAL ENERGY GENERATED (MHH) 778,310 5,572,530 12,699.410 l

l 18. NET ELECTRICAL ENERGY GENERATED (MHH) 751,250 5,318,987 12,167,837 1

PAGE 1 0F 2

e $ 6 0PERATING DATA REPORT (CONTIMKD1 DOCKET NO. 50 - 352 l

DATE JANUARY 15, 1988 THIS HONTH YR-TO-DATE CUNULATIVE

19. UNIT SERVICE FACTOR 100.0 67.7 74.9
20. UNIT AVAILABILITY FACTOR 100.0 67.7 74.9
21. UNIT CAPACITY FACTDR (USING HDC NET) 95.7 57.6 68.7
22. UNIT CAPACITY FACTOR (USING DER NET) 95.7 57.6 68.7
23. UNIT FORCED DUTAGE RATE 0.0 4.1 3.8
24. SHUTDO>NS SCHEDULE 0 OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):

REFUELING OUTAGE

25. IF SHUTDODN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUPt
26. UNITS IN TEST STATUS (PRIOR TO Cat 91ERCIAL OPERATION): FORECAST ACHIEVED INITIAL CRITICALITY 12/19/64 12/22/64 INITIAL ELECTRICITY MID APRIL 85 4/13/85 COMMERCIAL OPERATION IST QTR 86 t/01/86 PAGE 2 0F 2

4 . .

IAdIT SHUTD0094S AND P0MER REDUCTIONS DOCKET No. 50 - 352 UNIT NAME LIMERICK UNIT 1 DATE JANUARY 15, 1988 REPORT HONTH DECEPBER, 1987 COMPLETED BY PHILADELPHIA ELECTRIC COMPAM(

R. H. GROPP TECHNICAL ASSISTANT LICENSINO SECTIDH NUCLEAR SUPPORT DEPARTMENT TELEPHCHE I2151 841-5058 .

(... __...........___...__................__............. __.................................................................. <

l l l l l NETH00 0F l LICENSEE l SYSTEM lCOMPCriENTl CAUSE ANJ CORRECTIVE I l TYP E l DURATION I RE ASON I SHUTTING D0604 l EVENT l CODE l CODE l ACTION TO I I I l l l l I l CF l 871224 l F l 000.0 l H l 4 l N/A l RB l DEMINX l RESIN NAS INADVERTENTLY INTRODUCED INTO THE I l l l l l l l l REACTOR VESSEL DUE TO A PROCEDURAL DEFICIENCY /

l l l l l l l l l OPERATIONAL ERRO

R. PROCEDURE

S HAVE BEEN l l l l l l l l l REVISED TO CLARIFY STEPS AND ADD MARNINGS TO l l l l l l l l l PREVENT RECURRENCE.

1 I I ----- l l l l 1 I I I I -

1 I I I I I (1) (2) (3) (4)

REASON METHOD EXHIBIT G - INSTRUCTIONS

[-FORCED

) - SCHEDULED A - EQUIPMENT FAILURE IEXPLAf#) 1 - MAFAJAL FOR AREPARATION OF DATA B - MAINTEMANCE OR TEST 2 - MANUAL SCRAM. ENTRY SHEETS FOR LICENSEE C - REFUELING 3 - AUTOMATIC SCRAM. EVENT REPORT (LER)

D - REGULAWORY RESTRICTION 4 - OTHER IEXPLAINI FILE INUREG-0161)

E - OPERAT"J:R TRAINING + LICENSE EXAMtINATION F - ADMINISTRATIVE (5)

G - OPERATIC *iAL ERROR (EXPLAIN)

H - OTHER(EXF1AIN) EXHIBIT I - SAME SOURCE

m. - - -__ - - _ _ _ -

. t

c. -

Docket No. 50-352 Attachm:nt to Monthly Op3rtting Raport for December 1987 Limerick Generating Station Unit 1 December 1 through December 31, 1987 I. Narrative Summary of Operating Experiences The unit began the report period operating at approximately 100% power.

On December 8, 1987, during the performance of the quarterly HPCI Pump, Valve and Flow Surveillance Test, the auxiliary oil pump began to cycle and the stop valve began to oscillate. An investigation revealed that the mechanical overspeed trip mechanism was malfunctioning. The suspected cause of the malfunction was dirt accumulation in one of the trip mechanism's oil ports. Following flushing of the oil system and exercising the trip mechanism, the surveillance test was completed satisfactorily.

On December 24, 1987, a condensate filter demineralizer resin intrusion occurred while returning a condensate filter demineralizer to service. This resulted in reactor coolant chemistry changes and increased steam line radiation levels necessitating a power reduction to 78% power. On December 27, 1987, following reactor coolant cleanup and subsequent investigation, the reactor was returned to full power operations.

The unit ended the report period operating at approximately 100% power.

II. Challenges to Main Steam Safety Relief valves The:m were no challenges to the Main Steam Safety-Relief va: c.c during the month of December.

s t

PHILADELPHI A ELECTRIC COM PANY 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHI A PA.191o1 (215)841 4000 January 15, 1988 Docket No. 50-352 Director Office of Resource Management U.S. Nuclear Regulatory Commission Washington, DC 20555 Attention: Document Control Desk

SUBJECT:

Limerick Generating Station Monthly Operating Report Gentlemen:

Enclosed is the monthly operating report for Limerick Unit 1 for the month of December 1987, forwarded pursuant to Technical Specification 6.9.1.6.

1 Very truly yours, lh W. M. Alden Director Licensing Section Nuclear Support Division Attachment cc: -Director, Office of. Inspection & Enforcement, USNRC (12 copies) ./

' William T. Russell, Administrator, Region I, USNRC E. M. Kelly, Senior Resident Site Inspector Mr. David E. Ney, PA Dept. of Envir. Resources l

Mr. P. A. Ross, NRC (2 copies)

INPO Records Center l

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