ML20141F331
| ML20141F331 | |
| Person / Time | |
|---|---|
| Site: | Trojan File:Portland General Electric icon.png |
| Issue date: | 10/31/1985 |
| From: | Orser W, Ulmer F PORTLAND GENERAL ELECTRIC CO. |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| WSO-652-85, NUDOCS 8601090229 | |
| Download: ML20141F331 (6) | |
Text
OPERATING DATA REPORT DOCKET NO. 1Q;-34 4 DATE 11-01-as COMPLETED BY P
.T M1mer TELEPHONE 50Lss6-3713 Ext. 495 OPERATING STATUS Notes Troian Nuclear Plant
- 1. Unit Name:
Octot,er 1985
. 2. Reporting Period:
3411
- 3. Licensed Thermal Power (MWt):
1216
- 4. Nameplate Rating (Gross MWe):
1130
- 5. Design Electrical Rating (Net MWe):
1122
- 6. Maximum Dependable. Capacity (Gross MWe):
1080
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Oc:ur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A
"!^
- 9. Power Level To Which Restricted,If Any (Net MWe):
N/A
- 10. Reasons For Restrictions.If Any:
This Month Yr to.Date Canulative 745.
7,296.
80,352,
- 11. Hours In Reparting Period 740.3 5,340.7 48,086.4~
- 12. Number Of Hours Reactor Was Critical 0.0 0.0 3,887.4
- 13. Reactor Reserve Shutdown Hours 735.2 5,254.7 47,590.2
- 14. Hours Generator on-Line 0.U 0.U 4,249.
- 15. Unit Reserve Shutdown Hours
? 470_R40-17_ss1 792_0 149.962.176.
I
- 16. Gross Thermal Energy Generated (MWH) 804.280 5.643.177.
49.198.957
- 17. Gross Electrical Energy Generated (MWH) u.
767.775.
5.366.665.
46.517.195
- 13. Net Electrical Energy Generated (MWH) 98.7 72.0 59.2
- 19. Unit Service Factor 98.7 72.0 63.3
- 20. Unit Availability Factor 95.4 66.1.
34.6
- 21. Unit Capacity Factor (Using MDC Net) 91.2 65.1 51.2
- 22. Unit Capacity Factor (Using DER Net) 0.0 5.4 16.1 23.' Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Eacht:
Cycle 8/9 Refueling outage scheduled for April 28, 1986.
N/A
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
26._ Units in Test Status (Prior to Commercial Operation):
Forecast Achieved 1
N/A N/A INITIAL CRITICALITY N/A N/A INITIAL ELECTRICITY COMMERCIAL OPERATION N/A N/A
=
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8601090229 B51031 DR ADOCK O 34 (qp7)
AVERAGE DAILY UNIT POWER LEVEL j
+
DOCKET NO. 50-344 TROJAN UNIT DATE 11-01-85 COMPLETED BY F.
J.
Ulmer TELEPHONE 907-996-3713 Ext. 495 OCTOBER 1985 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 312 1058 37 0
g 10s0 18 3
1063 gg 1054 4
1064 1053 20 1065 1058 5
21 1058 1071 6
22 7
1001 1060 g
3 1008 24 1054 1012 1061' 9
25 10 1067 26 1053 33 1065 1096 27 1065 1061 12 3
13 1065 29 1067 1061 1064 g4 30 15 31 1065 1053 16 INSTRUCTIONS On this format, list the average daily unit power levelin MWe Net for each day in the rep irting month. Compute to the nearest whole megawatt.
(9/77) c- --
L.
UNIT SifU1 DOWNS AND POWER REDUCTIONS DOCKET NO.
50-344 UNIT NAME mnn.1AN DATE 11-01-85 COMPLETED liY P
T - If1mnr REIVRT MONTil OCTOBER 1985 TELErilONE 503-556-3713 Ext. 495 E
E
~
,5 E
}
}.Y }
Licensee E t, Cause & Corrective W.
Date g
3g jge Event g7 e.3 Action to yU Prevent Recurrence t-
$E 5
j p, g Report a in U 6
85-07 850924 S
9.8 G*
3 85-12 IIG VALVOP Outage contiued from September.
85-08 851007 F
'O A
4 n/a fill VALVOP Reactor power uas reduced from 100% to 45% due to a diaphragm air leak on #4 feedwater regulat ing valve.
The diaphragm was replact :d and the plant' returned to 100%.
- T 1e rea: ;on for this shutd aun uas J ncorretly reported be equipment
- f. tilure in the Sept ( mber ceport.
The reason for the shutdown shouli l h, 1ve be< sn reported i s' ope cational error.
I 2
3 4
F: Forced Reason:
Method:
Exhibit G. Instructions S: Scheduled A Equipment Failure (Explain)
I-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.
Entry Sheels for Licensee C Refueling 3 Automatic Sc:am.
Event Report (1.ER) File (NUREG.
D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Traiiing A Ucense Examination F Administrative 5
G-Operational Errug (Explain)
Exhibit I Same Source (9/77)
Il Other (Explain)
I s
-~
l e
ammme Portland General Electric Company Trojan Nuclear Plant P.O. Box 439 Rainier, Oregon 97048 (503)556-3713 November 4, 1985 WSO-652-85 Office of Resource Management US Nuclear Regulatory Commission Washington, DC 20555 Gentlemen:
In accordance with the Trojan Nuclear Flant Technical Specifications reporting requirements, the monthly report is submitted for October, 1985.
Sincerely W.
S.
Orser General Manager WSO: pat Attachments h
/'
o
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO:
50-344 DATE:
11-01-85 COMPLETED BY:
F.
J. Ulmer TELEPHONE:
503-556-3713 OPERATIONS:
The plant entered the month in Mode 3 at no-load operating temperature and pressure.
PCV-455B, loop C pressurizer spray valve was secured in the closed position to prevent excessive valve stem leakage.
At 0446 on October 1, 1985, the reactor attained criticality.
At 0948, October 1, the turbine generator unit was synchronized with the grid and remained on-line for the rest of the month.
At 2013 on October 7, plant power was reduced from 100% to 45% due to excessive diaphragm air leakage on #4 feedwater regulating valve
( FWRV ).
The FWRV diaphragm was repaired and the plant returned to 100% power at 0245 on October 8.
At 0935 on October 8, a fire occurred in non-ESF electrical cabinet B45 on the 93-foot level of the auxiliary building.
The fire was caused by contract workers drilling through the cabinet and into a live bus bar while drilling holes for cable mounts.
The fire was immediately extinguished and the two injured workers were sent by ambulance to a hospital for observation and treatment of minor flash burns.
At 0517 on October 9, plant power was reduced to 85% to perform core power distribution testing.
At 1315, the testing was complete and the plant returned to 100% power.
On October 22nd and 24th while excavating north of the fuel building, blasting wire was uncovered.
In both instances, US Army Ordanance Disposal Teams were called out to investigate.
The wiring was deter-mined to be from site excavating during plant construction and no explosive material was found.
Major Safety-Related Maintenance 1.
'A' Train ESF equipment outage 2.
'B' Train ESF equipment outage 3.
Overhaul electric fire pump 4.
Repaired auxiliary feedwater pump suction pressure transmitters Miscellaneous Maintenance 1.
Repaired load center B-45 2.
Repacked
'B' bearing cooling water pump 3.
Overhaul of fish rearing facility pump l
t ZE d YI
l l
Page 2 LLicense Changes:
Amendment 107
~
The amendment revised the Technical Specifications to reduce the fre-quency of diesel generator testing and allowed _the' engine to be warmed up for most tests before increasing speed.
The test-starts from ambient conditions are to be conducted semi-annually instead of monthly.
NRC letter 84-15 identified that cold fast-starts of diesel generator sets contributed to premature diesel engine degradation and excessive diesel generator testing contributes to unnecessary wear.
Miscellaneous Conducted annual' Radiological Emergency Response Plan (RERP) drill with offsite agencies.
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