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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 ML20235M1941989-02-0808 February 1989 SER Accepting Util Response to NRC Bulletin 88-005 Re Identifying,Locating & Testing Nonconforming Flanges & Fittings Supplied by Piping Supplies,Inc,West Jersey Mfg Co & Chews Landing Mfgs ML20196E5961988-11-30030 November 1988 Safety Evaluation Supporting Amend 10 to License NPF-36 ML20196B6831988-11-30030 November 1988 Safety Evaluation Supporting Amend 9 to License NPF-36 ML20155F3531988-10-0606 October 1988 Safety Evaluation Supporting Util 870414 Request for Authorization to Increase Power to 25% of Full Rated Power W/Listed Conditions.Licensee Evaluation of Operation & Proposal for Inspecting Components Must Be Augmented ML20155F3431988-10-0606 October 1988 Safety Evaluation Supporting Util Request to Operate Facility at 25% Power Re Accident Evaluation ML20155F3381988-10-0606 October 1988 Safety Evaluation Supporting Util Request for Authorization to Operate Facility at 25% Power Re Sys & Procedures for Accident Mitigation ML20154K0101988-09-19019 September 1988 Safety Evaluation Supporting Util 840309,850621 & 860606 Responses to Generic Ltr 83-28, Required Actions Based on Generic Implication of Salem ATWS Events, Items 3.1.1, 3.1.2,3.2.1,3.2.2 & 4.5.1 ML20154F3921988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Sys & Procedures for Accident Mitigation ML20154F3951988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Accident Evaluation ML20154F4031988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Safety of Prolonged Operation at 25% Power ML20154R9391988-05-31031 May 1988 Safety Evaluation Supporting Plant Primary Property Damage Insurance Exemption ML20236F7141987-10-19019 October 1987 Safety Evaluation Supporting Amend 8 to License NPF-36 ML20234B8201987-09-14014 September 1987 SER on Util 830414,851023 & 860227 Responses to Generic Ltr 82-33 Re post-accident Monitoring Instrumentation Meeting Requirements of Reg Guide 1.97 as Applied to Emergency Response Facility ML20237G4701987-08-14014 August 1987 Safety Evaluation Supporting Amend 7 to License NPF-36 ML20214K3961987-05-18018 May 1987 Safety Evaluation Supporting Amend 6 to License NPF-36 ML20215M4181987-05-0404 May 1987 Safety Evaluation Supporting Amend 5 to License NPF-36 ML20211N5921986-12-0909 December 1986 Safety Evaluation Supporting Amend 4 to License NPF-36 ML20213D5001986-11-0303 November 1986 Safety Evaluation Supporting Amend 3 to License NPF-36 ML20205E0601986-08-0101 August 1986 SER of Tdi Owners Group Program to Validate & Upgrade Quality of Tdi Diesel Generators for Nuclear Emergency Standby Svc.Technical Solution Available to Address Problem ML20154L9801986-03-0404 March 1986 Safety Evaluation Supporting Amend 2 to License NPF-36 ML20138N6701985-12-0606 December 1985 Safety Evaluation Supporting Amend 1 to License NPF-36 ML20058E1851982-07-15015 July 1982 Safety Evaluation Supporting Order Extending Const Completion Date to 830331 1993-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20135D8011996-11-26026 November 1996 Part 21 Rept Re Two Safety Related Valves Supplied by Velan Valve Corp Were Not in Compliance W/Originally Supplied QA Documentation.Returned Valves to Velan in May 1996 & on 961120 Velan Advised That Valves Had Been Misplaced ML20080G4691995-01-26026 January 1995 Record of Telcon W/Nrc & Licensees 950126 to Clarify Position Re Dispositioning of Exempt Sources Listed in Section 6.3.3 of Shoreham Termination Survey Final Rept Dtd Oct 1994 ML20069F0001994-01-24024 January 1994 Vols 1-4 to Shoreham Decommissioning Project Termination Survey Final Rept ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20045C8881993-06-0808 June 1993 Vols 1 & 2 to Refueling Jib Crane 1T31-CRN-008A Incident Root Cause Analysis. W/One Oversize Encl ML20044C1181993-02-28028 February 1993 Shoreham Nuclear Power Station Updated Decommissioning Plan. ML20128P6451993-02-28028 February 1993 Snps Decommissioning Project Termination Survey Final Rept for Steam Turbine Sys (N31) ML20128P7431993-02-19019 February 1993 Rev 3 to 93X027, Nuclear QA Surveillance Rept ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20128B9641992-10-31031 October 1992 Rev 0 to Shoreham Decommissioning Project Termination Survey Plan ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20099H5781992-07-31031 July 1992 Rev 4 to Shoreham Defueled Sar ML20114A6311992-07-28028 July 1992 Shoreham Decommissioning Plan ML20101K5791992-06-25025 June 1992 Long Island Power Authority Shoreham Decommissioning Project,Shoreham Nuclear Power Station,Technical Rept on Water Processing & Water Mgt Activities for Reactor Pressure Vessel & Wet Cutting Station ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20082M5081991-08-26026 August 1991 Rev 3 to Shoreham Defueled Sar PM-91-125, Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station1991-07-31031 July 1991 Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station PM-91-112, Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station1991-06-30030 June 1991 Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station PM-91-075, Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station1991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr SNRC-1806, Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 19901991-04-15015 April 1991 Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 1990 PM-91-058, Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station1991-03-31031 March 1991 Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station PM-91-037, Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station1991-02-28028 February 1991 Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station PM-91-016, Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station1991-01-31031 January 1991 Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station SNRC-1797, 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 19901990-12-31031 December 1990 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 1990 SNRC-1794, Shoreham Nuclear Power Station Annual Operating Rept,19901990-12-31031 December 1990 Shoreham Nuclear Power Station Annual Operating Rept,1990 SNRC-1799, Lilco 1990 Annual Rept1990-12-31031 December 1990 Lilco 1990 Annual Rept ML20069Q3901990-12-31031 December 1990 Shoreham Nuclear Power Station Decommissioning Plan. (Filed in Category P) ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 PM-90-097, Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station1990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 PM-90-083, Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station1990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1986-0391990-05-16016 May 1990 LER 86-039-01:on 861006,unplanned Initiation of Reactor Bldg Standby Ventilation Sys Occurred W/All Rods Inserted in Core.Caused by Faulty Design of Retaining Device.Warning Signs Attached to Valve Actuator & Valve Mod Initiated 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 05000322/LER-1987-0221990-05-16016 May 1990 LER 87-022-01:on 870604,HPCI Test Valve to Condensate Storage Tank,Globe Valve & Hpci/Rcic Test Valve to Condensate Storage Tank Failed to Close Against Sys Operating Pressure.Disc of motor-operated Valve 37 Modified 05000322/LER-1989-0051990-05-16016 May 1990 LER 89-005-01:on 890321,results of Local Leak Rate Test of Core Spray Suction Valve a Determined That Leakage,When Combined W/All Type B & C Penetration Leakages,Exceeded Tech Spec Limit.Caused by Normal Valve Degradation 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 1997-05-01
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- UNITED STATES
! g NUCLEAR REGULATORY COMMISSION 5 np WASHINGTON, D C,20555
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SAFETY EVALUATION AMENDNENT kO. 1 TO LICENSE N0. NPF-36 SHOREHAM NUCLEAR POWER STATION
, DOCKET NO. 322 Introduction By letter dated October 21, 1985 (SNRC-1206), the Long Island Lighting Company (LILCo, the licensee) requested that paragraph 2.C.(8) of License No. NPF-36 for the Shoreham Nuclear Power Station (Shoreham, the facility) be revised to allow an extension of time for the completion of the environmental qualification of certain electrical equipment. The licensee had previously requested approval of this extension directly from the Conmission, as required by 10 CFR 50.49, in a letter dated September 26, 1985 (SNRC-1199).
Discussion Condition 2.C(8) of License NPF-36, dated July 3, 1985, states that " Prior to November 30, 1985 the licensee shall environmentally qualify all electrical equipment according to the provisions of 10 CFR 50,49." The licensee requested an extension beyond November 30, 1985 for two items (totaling 13 pieces). The licensee reported that it had successfully qualified 934 out of 1083 items and expected to complete the qualification of the remainder of the equipment (except for the two items in question) by November 30, 1985.
Each of the two Hydrogen Recombiners which comprise the first item consists of a power cabinet and a recombiner skid. They are manufactured by Rockwell International, Inc. The licensee has been working with the vendor to qualify this equipment since May 1980. The vendor was authorized to begin qualification testing in June 1981. However, because of the large number of unqualified components in the power cabinet, the unacceptable results of initial qualifica-tion tests and faults in the test program that were identified in 1982 and 1983, a new test program was established in February 1983. In May 1983, the vendor estimated that all testing would be concluded by mid-1985. The test program proceeded to successfully follow this schedule, until the licensee was informed in August 1985 of the failure of a power cabinet during a seismic test. The seismic test is a normal part of the environmental qualification test sequence.
The vendor has determined that the failure was caused by silicon dust contamina-tion of certain auxiliary electrical contacts. A new cleaning procedure was developed and the power cabinet was retested. The licensee has since informed the staff verbally that,the test was successfully completed in late October, 1985.
In anticipation of the successful completion of the test, the licensee ordered j and has received on site new power cabinets and other components for the recombiner i skid. The new power cabinet and components are being installed now, during a I
maintenance outage. The licensee will have them installed before the reactor
, is restarted. However, because the qualification documentation would not be j complete by November 30, 1985, the licensee requested an extension. The j
staff notes that the justifications for continued operation attached to the licensee's September 26 request are applicable only to the old equipment that
! ! is being replaced.
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The second item for which an extension was requested is an actuator used for
'certain ventilation dampers in the Reactor Building Standby Ventilation System.
, A total of nine dampers are involved. The licensee originally purchased model i MASR-49 actuators for these dampers from Raymond Control Systems, Inc. When the licensee requested vendor assistance in 1981 to demonstrate the qualification of the actuators, it was informed that the model MASR-49 units were obsolete.
The licensee decided to purchase replacement model SURE-49 units and demonstrate their qualification. The test program started in mid-1982 and continued through
- 1985. The staff has been infomed verbally that the final test was completed successfully on October 16, 1985, but, as is the case with the hydrogen
- recombiners, the documentation had not been completed as of November 30, 1985.
., The licensee has-purchased new model SURE-49 actuators which are identical to
, the unit being tested, and will install them during the current outage. The equipment justifications in the licensee's September 26, 1985 letter are applicable only to the old model MSAR-49 actuators which are being replaced.
't
! The licensee has requested an extension until November 30, 1986 for the completion j of qualification of the hydrogen recombiners and an extension until August 31, 1 1986 for the completion of qualification of the damper actuators. Considering that 1) the delay in the qualification of these items was beyona the control of i the licensee, 2) the actual testing is about to be completed, 3) the licensee is in the process of installing the new equipnent which is currently under test, t and 4) the need for an extension beyond November 30, 1985 is based solely on delays in completion of the qualification documentation package, if the tests are successful, the staff finds that the licensee has provided a satisfactory
- basis to demonstrate the exceptional nautre of the case.
- However, the staff does not believe that the length of the extensions requested by the licensee are warranted. An extension until December 31, 1985 should be i
sufficient to allow the licensee to complete the qualification documentation packages. This view was upheld by the Connission, which approved an extension until December 31, 1985 in a letter dated November 19, 1985 to fir. John Leonard
- of LILCo from the Secretary of the Commission.
Evaluation
- Shorehain is currently shutdown to replace the neutron startup sources in the i reactor core and to perform certain maintenance and surveillance items. The plant is scheduled to restart in mid-December,1985. An extension of the
+
- qualification deadline would not affect the safe operation of the plant for
- this limited time period for several reasons:
l j 1. 'The extension'does not modify the design bases or criteria of th'e equip-ment in question. It does not, therefore, increase the probability or consequences of an accident.
- 2. The extension does not vary or affect any plant operating condition or parameter. It does not create the possibility of a new or different kind of accident from any accident previously evaluated.
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- 3. It does not change the qualification parameters or standards, the equipment operability requirements, or the design bases for the equipment in the plant. It would only allow the licensee an extension of time to complete the formal documentation which demonstrates that
' the equipment in question meets the standards and design bases, as already proven by the successful tests.
- 4. During the short time that the plant will operate with this extension (from about mid-December to the end of December,1985), the plant will be limited to operation below 5% of rated thermal power. At these low
- power levels much greater margins of safety exist, with correspendingly i greater time limits before severe consequences may develop during an
't accident. Any reduction in such margins of safety because the qualification documentien for this equipment is not complete are insignificant.
-i Environmental Consideration l This amendment involves facility components located within the restricted area i
defined in 10 CFR Part 20. The staff has determined that the amendment involves l no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in the individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public comment on such findings. Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b)
) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of this amendment. i Conclusion 1
We have concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activities will '
, be conducted in compliance with the Commission's regulations and the issuance of these amendments will not be inimical to the common defense and security or i l to the health and safety of the public. I Dated: DEC 0 6 5ES P
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