ML20138M285

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Monthly Operating Repts for Nov 1985
ML20138M285
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 11/30/1985
From: Alden W, Logue R
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
NUDOCS 8512200346
Download: ML20138M285 (13)


Text

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 - 277 l

LMIT PEACH BOTTOM UNIT 2 DATE DECEMBER 13.1985 COMPANY PHILADELPHIA ELECTRIC CONPANY W.M.ALDEN EHGINEER-IN-CHARGE LICENSING SECTION HUCLEAR GENERATION DIVISION TELEPHONE (215) 841-5022 MONTH NOVEteER 1985 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (HWE-HET)

(HWE-NET) 1 1035 17 1045 2

1040 18 1044 3

1036 19 1045 4

1039 20 1043 4

5 1038 21 1044 6

1035 22 1047 7

1035 23 1038 8

1037 24 1042 9

1037 25 1042 10 938 26 1043 11 1018 27 1040 12 1032 28 1041 13 1037 29 36 7 14 1037 30 0

15 1045,

16 1047

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c AVECAGE DAILY UNIT POWER LEVEL DOCKET HO. 50 - 278 UNIT PEACH BOTTOM UNIT 3 1

DATE DECEMBER 13.1985 COMPANY PHILADELPHIA ELECTRIC COMPANY W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION NUCLEAR GENERATION DIVISION TELEPHONE (215) 841-5022 MONTH NOVEMBER 1985 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL

( PSIE-NET 1 (ISIE-HET 1 1

0 17 0

2 0

18 0

3 0

19 0

4 0

20 0

5 0

21 0

6 0

22 0

7 0

23 0

1 8

0 24 0

9 0

25 0

10 0

26 0

11 0

27 0

12 0

28 0

13 0

29 0

14 0

30 0

15 0,

16 0

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s OPERATING DATA REPORT 9

o DOCKET NO. 50 - 277 DATE DECEMBER 13.1985 CottPLETED BY PHILADELPHIA ELECTRIC COMPANY W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION NUCLEAR GENERATION DIVISION TELEPHONE (215) 841-5022 I

OPERATING STATUS I

1. UNIT NAMEt PEACH BOTTOM UNIT 2

'l NOTESt UNIT 2 EXPERIENCED ONE l

l l

2. REPORTING PERIC08 NOVEteER, 1985 l

SCHEDULED LOAD REDUCTION, l

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30 LICENSED THERMAL POWER (t94T)*

3293 l

ADO ONE AUTO-SCRAM.

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0. NAMEPLATE RATING (GROSS 754Elt 1152 l

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5. DESIGN ELECTRICAL RATING (NET tedt):

1065 l

1 1

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0. MAXIMLM DEPEleABLE CAPACITY (GROSS IS4Els 1098 l

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7. MAXIMUtl DEPE) CABLE CAPACITY (HET F54E) 1051 l

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8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS IMSER 3 THROUGH 7) SINCE LAST REPORTe GIVE REASONSI
9. POWER LEVEL TO letICH RESTRICTED, IF ANY (HET tedEls
10. REASONS FOR RESTRICTIONS. IF ANY:

THIS tt0NTN YR-TO-DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD 720 8.016 100.008
12. PA#eER OF HOURS REACTOR WAS CRITICAL 684.0 2.824.0 65,107.6
13. PEACTOR RESERVE SHUTDOlet HOURS 0.0 0.0 0.0
14. Il0GIS GENERATOR OH-LINE 684.0 2.543.2 63.099.8
15. LMIT RESERVE SHUTD0684 HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (Plat) 2,229,0 %

7.774,848 186.194.849

17. GROSS ELECTRICAL ENERGY GENERATED (t94fl 729,220 2 481,570 61.200.230

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18. NET ELECTRICAL ENERGT GENERATED (PS8fl 704,599 2.324.701 58.587.039.

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19. LD(IT SERVICE FACTOR 95.0 31.7 63.1 n

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l te. UNIT AVAILABILITY FACTOR 95.0 31.7 63.1

21. UNIT CAPACITY FACTOR (USING tec HET) 93.1 27.6 55.7
22. UNIT CAPACITY FACTOR (USING DER HET) 91.9 27.2 55.0
23. LHIT FORCED OUTAGE RATE 0.0 20.9 12.9

'th SHUTD0lNS SCHEDULED OVER NEXT 6 MONTHS (TYPEe DATE. AND DURATION OF EACH18

25. IF SHUTDOIN AT Ele OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: 12/18/85 -
26. UNITS IN TEST STATUS (PRIOR TO CDPt1ERCIAL OPERATIOHit FORECAST ACHIEVED INITIAL CRITICALITY 09/.16/73 INITIAL ELECTRICITY

... 02.b.18 74 C0tttERCIAL OPERATICH

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1 OPERATING DATA REPORT l

l DOCKET NO. 50 - 278 DATE DECEMER 13,1985 l

COMPLETED BT PHILADELPHIA ELECTRIC CONPANY W.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION NUCLEAR GENERATION DIVISION TELEPHONE (215) 841-5022 OPERATING STATUS

1. UNIT NAMEt PEACH BOTTOM UNIT 3 i NOTES UNIT 3 CONTI WED ITS SIXTH I

l l

2. REPORTING PERIOD 8 NOVEMER, 1985 l

REFUELING AM MAINTENANCE I

1 I

3. LICENSED THERMAL PONER(t94T):

3293 l

OUTAGE.

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4. NAMEPLATE RATING (GROSS tt4E):

1152 l

l I.

1 I

5. DESIGN ELECTRICAL RATING (HET PG4E) 1965 l

l l

l

6. MAXIMUM DEPENDA8LE CAPACITY (GROSS tt4E)* 1098 l

l l

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7. MAXIt0JM DEPEM3ABLE CAPACITY (HET t#4E):

1035 l

I

8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS HUteER 3 THROUGH 7) SINCE LAST REPORT. GIVE REASONSI
9. PONER LEVEL TD letICH RESTRICTED IF ANY (HET PteE):
10. REASONS FOR RESTRICTIONSe IF ANY:

THIS MONTH YR-TD-DATE Cur 0JLATIVE

11. HOURS IN REPORTING PERIOD 720 8.016 95.904
12. NLMBER OF HOLAIS REACTOR WAS CRITICAL 0

4.055.7 68.613.E

13. REACTOR RESERVE SHUTD064f HOURS 0.0 0.0 0.0
14. HOURS GENERATOR OH-LINE O.0 3.989.3 66e854.4
15. (MIT RESERVE SHUTD0144 H0(5tS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (ftet1 0

10e796e856-194e996e664 17.' GROSS ELECTRICAL ENERGY GENERATED (Ptef) 0 3.486,130 63,993.670

18. NET ELECTRICAL ENERGY GENERATED (ISOf)

-5e932 3:290.416 61,399.718

19. LDf1T SERVICE FACTOR 0.0 49.8 69.7

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20. LA4IT AVAILABILITY FACTOR 6.0 49.8 69.7
21. UNIT CAPACITY FACTOR (USING PSC NET) 0.0 39.7 61.9
22. UNIT CAPACITY FACTOR (USING DER HETI 0.0 38.5 60.1
23. UNIT FORCED OUTAGE RATE 0.0 0.8 7.1
23. SHUTD01445 SCHEDULED OVER HEXT 6 MONTHS (TYPEe DATE. Ale DURATION OF EACH):

SCHEDULED SHUTD0644 FOR REFUELING AM MAINTENANCE OUTAGEe STARTED 7/14/85

25. IF SHUTDolet AT EM OF REPORT PERIODe ESTIMATED DATE OF STARTUp: 01/04/86
26. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATIDHis FORECAST ACHIEVED INITIAL CRITICALITY 08/07/J4 INITIAL ELECTRICITY 99).Qll]4 CorMERCIAL OPERATION 12/23/74 2

O - HESATIVE VALUE REPORTED FOR CONSISTENC'l MITH FEDERAL ENERGY RESULATORY CorMISSIGH REPORTS.

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UNIT SHUTD0bt45 Am POWER REDUCTIONS DOCKET NO. 50 - 277 LR4IT HAME PEACH BOTTOM L24IT 2 DATE DECEMER 13.1965 REPORT MONTH NOVEleER, 1965 COMPLETED BY PHILADELPHIA ELECTRIC COMPANY N.M.ALDEN ENGINEER-IN-CHARGE LICENSING SECTION NUCLEAR GENERATION DIVISION TELEPHONE I215) 441-50Et l

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l l METHOD OF l LICEhSEE lSYSTEMICOMPCHENTI CAUSE Am CORRECTIVE l

l TYPE!OURATIONlREASONISHUTTING D0604l EVENT l CODE i CODE I ACTION TO NO.! DATE I (1H IHOURS)I (23-l REACTOR (3) l REPORT 8 l (4) l (5) l PREVENT RECLatRENCE

..... _ _... ~ _. -.. _ -

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I 23 1 851110 l F l 900.0 l F l 4

l N/A l XX l 200000( l LOAD REDUCTION TO 77919dE DUE TO CABLE TRAT I

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l l FIREe IN RAD NASTE AREA.

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l t-45-25 l XX l 200000( l letEN THE LB4IT NAS AT 31X poler DLMING THE I

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l l OF THE MAIN TURSINE STOP VALVES CAUSED AH I

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l l AUTOMATIC SCRAM. 1NE St TURSINE STOP VALVE I

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I I FAILEO TO CLOSE DURING SURVELENCE TESTINS.

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I tesILE ATTEMPTING TO CLDSE THE St TURSINE STOP 1

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(2)

(3)

(4)

F. FORCED REASON METHOD E30tIBIT S. INSTRUCTIONS S - SCHEDULED A - EQUIPMENT FAILURE IEXPLAIN) 1 - MADEAAL FOR PREPARATION OF DATA B. MAINTENANCE OR TEST 2 - MADRIAL SCRAM.

ENTRY SHEETS FCII LICENSEE

'C. REFUELING 3 - AUTOMATIC SCRAlf.

EVENT REPORT ILER)

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D - RESULATORY RESTRICTION 4 - OTHER (EXPLAIN)

FILE flAstES-9161)

E - OPERATOR TPLINING + LICENSE EXAMINATION F. ADMINISTRATIVE IS)

S. OPERATICD4AL ERROR (EXPLAINI N. OTHERIEXPLAIN)

EMNIBIT I. M SOLRCE Y

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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET HO. 50 - 278 UNIT HAME PEACH BOTTOM UNIT 3 DATE DECEMBER 13.1985 REPORT N0HTH NOVENBER, 1985 CONPLETED BY PHILADELPHIA ELECTRIC COMPANY

___.=====

W.H.ALDEN ENGINEER-IN-CHARGE LICENSING SECTICH HUCLEAR GENERATION DIVISIDH TELEPHONE (215) 841-5022 1

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l l NETH00 0F l LICENSEE ISYSTENICOMPONENTl CAUSE AfD CORRECTIVE l

iTYPEl0URATICHIREASOHISHUTTING DOWHI EVENT l CODE l CODE l ACTION TO N0.1 DATE I (1)I (HOURS)l (2) l REACTOR (3) l REPORT 3 l (4) l (5) l PREVENT RECURRENCE I

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13 1 851101 l S I 720.0 i C l 4

l H/A I RC l FUELXX l SHUTDORI FOR SIXTH REFUELING /NAINTEliANCE OUTAGI l

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l 720.0 I l

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(1)

(2)

(3)

(4)

F - FORCED REASON METHOD EXHIBIT G - INSTRUCTIONS S - SCHEDULED A - EQUIPMENT FAILURE (EXPLAIH) 1 - MAPUAL FOR PREPARATION OF DATA B - MADITD4AHCE OR TEST 2 - HANUAL SCRAM.

ENTRY SHEETS FOR LICDISEE C - REFUELING 3 - AUTOHATIC SCRAM.

EVENT REPORT (LER)

D - REGULATORY RESTRICTI0tl 4 - OTHER (EXPLAIH)

FILE (HUREG-0161)

E - OPERATOR TRAINING + LICENSE EXAMINATIDH F - ADHINISTRATIVE (5)

G - OPERATIONAL ERROR (EXPLAIN)

H - OTHER(EXPLAIH)

EXHIBIT I - SANE SOURCE l

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Dockot Nos. 50-277/50-278 Attachment to Monthly Operating Report fo r November, 1985 Peach Bottom Atomic Power Station Narrative Summary of Operating Experiences November, 1985 UNIT 2 Unit 2 began the report period operating at full power and maintained full power operation until November 10.

On November 10, a fire occurred in a cable tray in the radwaste building.

An electrical transient (caused by the fire) caused a recirculation pump runback and a turbine electrohydraulic control system (EHC) runback, resulting in a load reduction to 770 MWe.

On November 11, the unit returned to full power and maintained full power operation until November 29.

Repairs to damaged cables were completed within a week.

Investigation into the cause of the cable tray fire continues.

On November 29, the unit was removed from service for a modification and maintenance outage to complete environmental qualification (EO) work in accordance with NRC regulations and to perform pipe support snubber inspections.

During the manual shutdown for EO work on November 29, th e reactor scrammed due to the closure of the 1, 3 and 4, turbine stop valves while attempting to close th e 2 turbine stop valve.

The 2 turbine stop valve had f ailed to close earlier the same day while being tested and was being investigated at the time of the scram.

UNIT 3 Unit 3 continued its sixth refuel outage Ebroughout the report pe riod.

On November 2, the 3C Residual Heat Removal (RHR) pump motor failed due to a fire in the lower motor guide bearing reservoir.

Guide bearing failure was caused by a pump impeller wear ring failure.

A new pump and a motor have been installed, tested, and i

placed into service.

An investigation concludes that IGSCC of the pump impeller wear ring was the cause of failure.

Weld overlay of the RHR and Recirculation System welds was completed on November 12.

On November 16, the 3A residual heat removal (RHR) pump was disassembled to replace the pump flange gasket.

During disassembly, a cracked impeller wear ring was also observed.

As j

a' result, the motor lower guide bearing was inspected, revealing signs of some damage.

The pump impeller was replaced and the motor lower gaide bearing was repaired.

The 3A motor and pump were returned to service on November 26.

Because of the problems

Attachmant to Monthly Operating Raport for November, 1985 Page 2 4

with the 3A and 3C RHR pumps, the 3B and 3D were also inspected and showed significant impeller wear ring damage.

The 3B and 3D pumps are being re naired.

On November 23, during installation of the steam separator, four of the 48 hold-down bolts broke.

Analysis of the bolt concludes IGSCC to be the cause of failure.

During removal, one of the bolts was dropped into the annulus region of the vessel, resulting in damage to a jet pump pressure sensing line inside the vessel.

Resolution of this problem is being investigated.

LLM V

4

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i Docket No. 50-277-Attachment to l

Monthly Operating Report for November, 1985 REFUELING INFORMATION 1.

Name of facility:

Peach Bottom Unit 2 2.

Scheduled date for next refueling shutdown:

i Ja~nuary 31, 1987 3.

Scheduled date for restart following refueling:

T l

May 1, 1987 l

4.

Will refueling or resumption of operation thereaf ter require a j

technical specification change or other license amendment 7 Yes If answer is yes, what, in general, will these be7 Technical Specifications to accommodate reload fuel.

l Modifications to reactor core operating limits.

5.

Scheduled date(s) for submitting proposed licensing action and supporting information:

Reload 7 license amendment to be submitted December 12, 1986.

6.

Important licensing considerations associated with refueling, e.g., new or dif ferent fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel 3

j design, new operating procedures:

None expected.

7.

The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pools (a)

Core - 764 Fuel Assemblies (b)

Fuel Pool - 1462 Fuel Assemblies, 58 Fuel Rods i

8.

The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.

A request for approval of replacement j

higher density fuel racks was submitted to the NRC on June l

13, 1985 which will increase the fuel pool capacity to a total of 3819 fuel bundles in each. fuel pool.

9.

The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.

March, 1991 (Septembe r, 1986, with reserve full core discharge) t

Docket No. 5 0-278 Attachment to Monthly Operating Report for November, 1985 REFUELING INFORMATION

1. - Name of facility:

Peach Bottom Unit 3 2.

Scheduled date for next refueling shutdown:

July 14, 1985 3.

Scheduled date for restart following refueling:

January 4, 1986 4.

Will refueling or resumption of operation thereaf ter require a technical specification change or other license amendment?

Yes.

- If answer is yes, what, in general, will these be?

Technical Specifications to accommodate reload fuel.

Modifications to reactor core operating limits.

5.

Scheduled date(s) for submitting proposed licensing action and supporting information:

MAPLHGR Limits Submitted January 7, 1985 Additional Gore Limit Information - April 11, 1985 6.

Important licensing considerations associated with refueling, e.g., new or dif ferent fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:

None expectad.

7.

The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool:

(a)

Core - 764 Fuel Assemblies (b)

Fuel Pool - 1212 Fuel Assemblies, 6 Fuel Rods 8.

The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

The spent fuel pool storage capacity has been relicensed for 2816 fuel assemblies.

A request for approval. of replacement higher density fuel racks was submitted to the NRC on June 13, 1985 which will increase the fuel pool capacity to a total of 3819 fuel bundles in each fuel pool.

i 9.

The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present-licensed capacity.

Marct, 1992 (March, 1987 with reserve for.

full core discharge)

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1 PHILADELPHIA ELECTRIC COMPANY

' l 2301 MARKET STREET P.O. BOX 8699 PHILADELPHIA. PA.19101 (215)841-4000 December 13, 1985 Docket Nos. 50-277 50-278 Director Office of Inspection & Enfo rceme nt US Nuclear Regulatory Commission Washington, DC 20555 Attention:

Document Control Desk

SUBJECT:

Peach Bottom Atomic Power Station Monthly Operating Report Gentlemen:

Attached are twelve copies of the monthly operating report for Peach Bottom Units 2 and 3 for the month of November, 1985 fo rwarded pursuant to Technical Specification 6.9.1.d under the guidance of Regulatory Guide 10.1, Revision 4.

Very truly

ours, R.

H. Logue Supe rintende nt Nuclear Services At tachme nt cc:

Dr. T.

E. Murley, NRC Mr. T.

P. Johnson, Resident Inspector Mr. Stan P. Mangi, Dept. of Envir. Resources Mr. P. A.

Ross, NRC (2 copies)

Mr. Thomas Magette, Maryland Power Plant Siting INPO Records Center

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