ML20137V630

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Monthly Operating Rept for Nov 1985
ML20137V630
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 11/30/1985
From: Gobell J
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML20137V627 List:
References
NUDOCS 8602190644
Download: ML20137V630 (4)


Text

I 9

OPERATING DATA REPORT DOCKET N0:

50-313 DATE:

November, 1985 COMPLETED BY:J. N. GoBell TELEPHONE:

(501)964-3251 OPERATING STATUS 1.

Unit Name:

Arkansas Nuclear One - Unit 1 2.

Reporting Period:

November 1-30, 1985 3.

Licensed Thermal Power (MWt):

2568 4.

Nameplate Rating (Gross MWe):

902.74 5.

Design Electrical Rating (Net MWe):

850 6.

Maximum Dependable Capacity (Gross MWe):

883 7.

Maximum Dependable Capacity (Net MWe): 836 8.

If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

9.

Power Level To Which Restricted.

If Any (Net MWe):

823 MWE (s97%)

10.

Reasons For Restrictions.

If Any:

Apparent high operating level in the "A" steam generator caused by fouling at the tube support plate crevice MONTH YR-TO-DATE CUMULATVE 11.

Hours in Reporting Period....

720.0 8,016.0 95,995.0 12.

Number of Hours Reactor was Critical.....................

720.0 6,261.4 64,919.3 13.

Reactor Reserve Shutdown Hours........................

0.0 0.0 5,044.0 14.

Hours Generator On-Line......

720.0 6,110.6 63,514.1 15.

Unit Reserve Shutdowr. Hours..

0.0 0.0 817.5

16. Gross Thermal Energy Generated (MWH)........................

1,614,180.0 14,482,518.0 150,835,334.0

17. Gross Electrical Energy Generated (MWH)..............

551,420.0 4,873,979.0 49,836,250.0 18.

Net Electrical Energy Generated (MWH)..............

525,369.0 4,618,081.0 47,480,604.0 19.

Unit Service Factor.........

100.0 76.2 66.2 20.

Unit Availability Factor.....

100.0 76.2 67.0

21. Unit Capacity Factor (Using MDC Net)..............

87.3 68.9 59.2 22.

Unit Capacity Factor (Using DER Net)..............

85.8 67.8 58.2 23.

Unit Forced Outage Rate......

0.0 17.6 14.9 24.

Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

25.

If Shut Down At End of Report Period.

Estimated Date of Startup:

26.

Units in Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8602190644 851215

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PDR ADOCK 05000313 R

PM

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO:

50-313 UNIT.

'One DATE:

November, 1985 COMPLETED BY: J. N. GoBell TELEPHONE:

(501)964-3251 MONTH November DAY

' AVERAGE DAILY POWER LEVEL (MWe-Net) 1.............

823 2.............

820 3.............

816 4.............

813 5.............

810.

6.............

807 7.............

806 8.............

804 9.............

529 10............

613 11............

546 12............

787 13............

629 14............

404 15............

802 16............

804 17............

603 18............

800 19............

799 20............

800 21............

798 22............

423 23............

326 24............

777-25............

795 26............

794 l

27............

791 28............

792 29............

791 30............

790 31............

AVGS:

730 INSTRUCTION On this format, list the average daily unit power level in MWe-Net for each day in reporting month.

Compute to the nearest whole megawatt.

NRC MONTHLY OPERATING REPORT OPERATING

SUMMARY

NOVEMBER 1985 UNIT ONE 4

Unit One started the month of November operating at 97% power limited by the high level in the "A" once through steam generator (OTSG).

At 0250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> on the ninth, power was reduced to 40% to conduct maintenance on the "A" main feed pump (MFP), because of pump speed oscillations.

At 0705 hours0.00816 days <br />0.196 hours <br />0.00117 weeks <br />2.682525e-4 months <br /> on the twelfth, the unit was back up to 96% power, limited by the high level in the "A" OTSG.

On the thirteenth at 1535 hours0.0178 days <br />0.426 hours <br />0.00254 weeks <br />5.840675e-4 months <br />, there was a plant runback to 44% power, caused by a spurious control signal being accidentally sent to the integrated control system during maintenance activities on the feedwater controls.

The unit was back up to 95% power, limited by the high level in the "A" 0TSG at 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> on the fifteenth.

i A plant runback to 40% power again occurred at 0504 hours0.00583 days <br />0.14 hours <br />8.333333e-4 weeks <br />1.91772e-4 months <br /> on the twenty-second when the governor shaft in the "B" MFP broke.

The unit was j

back up to 95% power at 0444 hours0.00514 days <br />0.123 hours <br />7.34127e-4 weeks <br />1.68942e-4 months <br /> on the twenty-fourth.

1 I

Unit One finished the month of November operating at 95% power, limited by the high level in the "A" once through steam generator.

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UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT FOR NOVEMBER, 1985 DOCKET NO 50-313 UNIT NAME ANO Unit 1 DATE December 3, 1985 COMPLETED BY J. GoBell TELEPHONE (501)964-3251 Method of Licensee Cause-& Corrective Duration Shutting Event System Component Action to No.

Date Typel

.(Hours)

Reason 2 Down Reactor 3 Report #

Code 4 Code 5 Prevent Recurrence 8513 851109 F

0 A

5 N.A.

SJ P

Power was reduced due to oscillations of the "A main feedwater pump and remained reduced to complete maintenance on the pump.

1 2

3 4

F:

Forced Reason:

Method:

Exhibit G - Instructions S:

Scheduled

-A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C-Refueling 3-Automatic Scram.

Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Continuation 1022)

E-Operator Training &

5-Load Reduction License Examination 9-Other 5

F-Administrative Exhibit I - Same Source G-Operational Error (Explain)

H-Other (Explain) 1 6