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Results
Other: AECM-83-0146, Forwards Response to Five of Six Items Contained in Re Util Work Addressing Containment Issues.Evaluation of Condensation Oscillation Loads Produced by Discharges from RHR HX Relief Valve Will Be Completed by Late Apr, AECM-84-0443, Forwards Approach to Chugging,Assessment of RHR Steam Discharge Condensation Oscillation in Mark III Containments, Per 830323 Commitment.Ae Evaluation Will Be Completed by mid-Dec 1984, AECM-85-0018, Forwards Evaluation of RHR Relief Valve Condensation Oscillation Loads on Structures & Piping.Info Demonstrates That All Loads Which Could Be Produced by Actuation of RHR HX Relief Valves Acceptable, AECM-85-0046, Provides Basis That Weir Wall Overflow Following Postulated Inadvertent Upper Containment Pool Dump Does Not Involve Significant Safety Problem.Evaluation Plans & Justification Provided, AECM-85-0233, Forwards Weir Wall Overflow Probability Analysis. Because of Very Low Probability of Occurrence & Leak of Safety Significance for Worst Case Postulated Overflow (Ref AECM-85/0046),corrective Actions Not Warranted, AECM-85-0376, Submits Info Re Wier Wall Overflow,Per 851021 Request.Topics Addressed Include Overflow Effect Upon Uninsulated Drywell Piping & Evaluation of Recirculation Piping Relative to Predicted Water Level.Ge Rept Re Containment Issue Encl, AECM-86-0143, Clarifies Planned Resolution of Possible Loads from Chugging Caused by Steam & Gas Venting Into Suppression Pool Through RHR Relief Valve Discharge Line.Rhr HX Vent Line Header Will Have Dedicated Discharge Line to Pool, ML20097F052, ML20137Q230, ML20204J145
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MONTHYEARAECM-83-0146, Forwards Response to Five of Six Items Contained in Re Util Work Addressing Containment Issues.Evaluation of Condensation Oscillation Loads Produced by Discharges from RHR HX Relief Valve Will Be Completed by Late Apr1983-03-23023 March 1983 Forwards Response to Five of Six Items Contained in Re Util Work Addressing Containment Issues.Evaluation of Condensation Oscillation Loads Produced by Discharges from RHR HX Relief Valve Will Be Completed by Late Apr Project stage: Other ML20137Q2301983-07-31031 July 1983 Containment Issue Isolation Transient Project stage: Other ML20097F0521984-03-31031 March 1984 Approach to Chugging,Assessment of RHR Steam Discharge Condensation Oscillation in Mark III Containments Project stage: Other AECM-84-0443, Forwards Approach to Chugging,Assessment of RHR Steam Discharge Condensation Oscillation in Mark III Containments, Per 830323 Commitment.Ae Evaluation Will Be Completed by mid-Dec 19841984-09-0707 September 1984 Forwards Approach to Chugging,Assessment of RHR Steam Discharge Condensation Oscillation in Mark III Containments, Per 830323 Commitment.Ae Evaluation Will Be Completed by mid-Dec 1984 Project stage: Other AECM-85-0018, Forwards Evaluation of RHR Relief Valve Condensation Oscillation Loads on Structures & Piping.Info Demonstrates That All Loads Which Could Be Produced by Actuation of RHR HX Relief Valves Acceptable1985-01-24024 January 1985 Forwards Evaluation of RHR Relief Valve Condensation Oscillation Loads on Structures & Piping.Info Demonstrates That All Loads Which Could Be Produced by Actuation of RHR HX Relief Valves Acceptable Project stage: Other AECM-85-0046, Provides Basis That Weir Wall Overflow Following Postulated Inadvertent Upper Containment Pool Dump Does Not Involve Significant Safety Problem.Evaluation Plans & Justification Provided1985-02-25025 February 1985 Provides Basis That Weir Wall Overflow Following Postulated Inadvertent Upper Containment Pool Dump Does Not Involve Significant Safety Problem.Evaluation Plans & Justification Provided Project stage: Other ML20126J2671985-06-11011 June 1985 Forwards Request for Addl Info Re Steam Condensing Mode of RHR Sys.Info Requested by 850715 Project stage: RAI AECM-85-0287, Responds to NRC 850611 Request for Addl Info Re Steam Condensing Mode.Listed Methods for Predicting Chugging Will Be Evaluated.Evaluation Scheduled for Completion by 8512201985-09-13013 September 1985 Responds to NRC 850611 Request for Addl Info Re Steam Condensing Mode.Listed Methods for Predicting Chugging Will Be Evaluated.Evaluation Scheduled for Completion by 851220 Project stage: Request AECM-85-0233, Forwards Weir Wall Overflow Probability Analysis. Because of Very Low Probability of Occurrence & Leak of Safety Significance for Worst Case Postulated Overflow (Ref AECM-85/0046),corrective Actions Not Warranted1985-10-0404 October 1985 Forwards Weir Wall Overflow Probability Analysis. Because of Very Low Probability of Occurrence & Leak of Safety Significance for Worst Case Postulated Overflow (Ref AECM-85/0046),corrective Actions Not Warranted Project stage: Other AECM-85-0376, Submits Info Re Wier Wall Overflow,Per 851021 Request.Topics Addressed Include Overflow Effect Upon Uninsulated Drywell Piping & Evaluation of Recirculation Piping Relative to Predicted Water Level.Ge Rept Re Containment Issue Encl1985-11-27027 November 1985 Submits Info Re Wier Wall Overflow,Per 851021 Request.Topics Addressed Include Overflow Effect Upon Uninsulated Drywell Piping & Evaluation of Recirculation Piping Relative to Predicted Water Level.Ge Rept Re Containment Issue Encl Project stage: Other AECM-86-0012, Discusses Status of Util Activities in Response to NRC 850611 Request for Addl Info Re Review of Possible Condensation Oscillation Loads from Chugging. Dedicated Lines from RHR HX Noncondensible Vents Preferred Resolution1986-01-28028 January 1986 Discusses Status of Util Activities in Response to NRC 850611 Request for Addl Info Re Review of Possible Condensation Oscillation Loads from Chugging. Dedicated Lines from RHR HX Noncondensible Vents Preferred Resolution Project stage: Request AECM-86-0143, Clarifies Planned Resolution of Possible Loads from Chugging Caused by Steam & Gas Venting Into Suppression Pool Through RHR Relief Valve Discharge Line.Rhr HX Vent Line Header Will Have Dedicated Discharge Line to Pool1986-05-16016 May 1986 Clarifies Planned Resolution of Possible Loads from Chugging Caused by Steam & Gas Venting Into Suppression Pool Through RHR Relief Valve Discharge Line.Rhr HX Vent Line Header Will Have Dedicated Discharge Line to Pool Project stage: Other AECM-86-0175, Corrected Response to 860326 Request for Addl Info Re Listed Humphrey Concerns,Including Addl Submerged Structure Loads & Containment Open Area,Correcting Omission of Page 2 from Attachment 31986-08-14014 August 1986 Corrected Response to 860326 Request for Addl Info Re Listed Humphrey Concerns,Including Addl Submerged Structure Loads & Containment Open Area,Correcting Omission of Page 2 from Attachment 3 Project stage: Request ML20204J1451987-03-23023 March 1987 SER Supporting Licensee Responses to Humphrey Concerns on Safety of Mark III Containment Design Project stage: Other ML20204J1161987-03-23023 March 1987 Forwards SER Re Licensee Responses to Humphrey Concerns on Mark III Containment Design.Humphrey Concerns Satisfactorily Resolved.Licensee Will Continue to Prohibit Use of RHR Steam Condensing Mode Until Design Mods Implemented Project stage: Approval 1985-11-27
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,A MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi RIBAMidd l P. O. B O X 164 0, J A C K S O N, MIS SIS SIP PI 39215-1640 November 27, 1985 NUCLEAR LICEN5ING & $AF ETY DEPARTNtENT U. S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Washington, D. C.
20555 Attention:
Mr. Harold R. Denton, Director
Dear Mr. Denton:
SUBJECT:
Grand Gulf Nuclear Station Units 1 and 2 Docket Nos. 50-416 and 50-417 License No. NPF-29 Weir Wall Overflow AECM-85/0376 Tne following information is submitted in response to a telephone request by Mr. Les Kintner and Al Notafrancesca on October 21, 1985 and subsequent conversations concerning weir wall overflow.
QUESTION 1 - Is there hot, uninsulatad piping in the dry well that would be affected by a weir wall overflow?
RESPONSE - A review of the piping below the predicted water level (EL 101.4' which is 0.65' above the drywell floor) after a weir wall overflow event'shows the only hot piping to be four drain lines leading from the recirculation piping. Two of the drains are 2" nominal pipe size and are insulated for their entire length. The remaining two are 3/4" nominal size and cre insulated for the first 41" away from the recirculation line.
Stress calculations performed on these lines show that they maintain their structural integrity following the overflow. The predicted water level was established by using a conservative approach, (Ref AECM-85/0233 dated October 4, 1985) and is based on:
- 1) the upper containment pool and suppression pool both being near their maximum level,
- 2) an inadvertent upper pool dump,
- 3) and a negative drywell pressure slightly in excess of the vacuum relief set point. A higher level would require all of the above conditions concurrent with multiple vacuum relief failures. The worse case assumption was also made that the drywell is absolutely pressure tight below the vacuum breaker set point.
In a recent pressure test of the drywell at 3 psid, a leak rate of approximately 2600 SCFM was recorded.
QUESTION 2 - What is the elevation of the recirculation piping relative to the predicted water level after a weir wall overflow?
RESPONSE - The center line elevation of the recirculation suction piping is 103' Sk" in the colo condition and 103' 3\\" when hot.
The pipe is 24" nominal diameter and is covered by a metallic nonwicking insulation and removable blanket insulation encapsulated with aluminized cloth / wire mesh where required for inservice inspection and/or interferences.
8512050108 B51127 0
PDR ADOCK 05000416 y%
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PDR Memoer Middle South Utilities System
AECM-85/0376 Page 2 QUESTION 3 - Has a report on fatigue analysis of piping in the drywell after subjection to a weir wall overflow been written? Is it generic?
RESPONSE - A generic report performed by General Electric for the Containment Issues Owners Group concerning fatigue analysis of recirculation piping after a weir wall overflow is attached. Note that this report considered total immersion of pumps, motors and piping.
. QUESTION 4 - General Electric strongly suggests a shutdown and inspection after a weir wall overflow event. What procedures address this action for Grand Gulf?
RESPONSE - In light of the extremely low probability of this event, no specific procedure exists which directly addresses a weir wall overflow.
However, Technical Specifications require the plant to be placed in a hot shutdown condition within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if suppression pool level exceeds the range of 18' 4 "
to 18' 9 3/4" and is not restored within I hour. An inadvertent upper pool dump will cause the suppression pool to exceed its upper limit by almost 5 feet. Technical Specifications also require a plant shutdown as stated above if unidentified leakage exceeds 5 gpm, total leakage exceeds 30 gpm or there is an increase of 2 gpm in unidentified leakage within any 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> period. Any significant weir wall overflow would exceed at least one if not all of these Technical Specifications.
For the case which was previously discussed the result would be thousands of gallons of water on the drywell floor. In addition to a required plant shutdown, the 2 gpm increase in unidentified leakage in a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> period requires that the source of the increase be verified not to be service sensitive type 304 or 316 austenitic stainless steel. The only way to verify this requirement is to make a drywell entry and inspect the components in the overflow area.
The Technical Specification requirements are tracked by procedure 02-S-01-17, Control of Limiting Conditions for Operation. Documentation of the above required actions in accordance with this procedure would be required prior to a plant restart.
Yours truly, L. F. Lale Director TWS/SHH:bms Attachment cc:
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1 AECM-85/0376 Page 3 cc:. Mr. T. H. Cloninger (w/a)
Mr. O. D. Kingsley, Jr. (w/a)
Mr. R. B. McGehee (w/a)
Mr. N. S. Reynolds.(w/a)
Mr. H. L. Thomas (w/o)
. Mr..R.-C. Butcher (w/a)
Mr. James M. Taylor, Director (w/a)
Office of Inspection & Enforcement U. S.. Nuclear Regulatory Commission
- Washington, D. C.
20555 Dr. J.. Nelson Grace, Regional Administrator (w/a)-
U. S. Nuclear Regulatory Commission Region II 101 Marietta St., N. W., Suite 2900 Atlanta, Georgia 30323 s
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