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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217H6341999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for Kh Curran,Lm Gerlach,Rc Weber & Bt Rhodes Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC Form 396 Encl.Proprietary Info Withheld ML20217H6251999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for MR Kahn,Aj Mclaughlin,De Montgomery & Kr Murphy Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC from 396 Encl.Proprietary Info Withheld ML20217F4301999-10-14014 October 1999 Responds to 991012 Rai,Based on 991001 Telcon Re Suppl to Request for TS Change to Revise MCPR Safety Limit & Add Approved Siemens Topical Rept for LaSalle County Station, Unit 1 ML20217D3191999-10-12012 October 1999 Submits Request for Addl Info Re Licensee 990707 Proposed License Amend to Revise Min Critical Power Ratio.Listed Questions Were Discussed with Util in 991001 Telcon ML20217C1671999-10-0808 October 1999 Provides Suppl to RAI for Approval of Unreviewed Safety Question Re Assessment of Certain safety-related Concrete Block Walls at LaSalle County Station,Units 1 & 2 ML20217A7601999-10-0606 October 1999 Forwards Insp Repts 50-373/99-15 & 50-374/99-15 on 990729-0916.One Violation of NRC Requirements Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy ML20212M0931999-10-0404 October 1999 Refers to 990922-23 Meeting Conducted by Region II at LaSalle Nuclear Power Station.Purpose of Visit,To Meet with Licensee Risk Mgt Staff to Discuss Util Initiatives in Risk Area & to Establish Dialog Between SRAs & Risk Mgt Staff 05000373/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl1999-10-0404 October 1999 Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20217A6201999-09-30030 September 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC Feedback on Any Planned Insps Which May Conflict with Plant Activities.Plant Issue Matrix & Insp Plan Encl ML20212E7171999-09-22022 September 1999 Forwards RAI Re Requesting Approval of License Amend to Use Different Methodology & Acceptance Criteria for Reassessment of Certain Masonry Walls Subjected to Transient HELB Pressurization Loads 05000374/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl1999-09-20020 September 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl ML20212C0591999-09-17017 September 1999 Informs That NRC Reviewed Licensee Justifications for Deviations from NEDO-31558 & Determined That Justifications acceptable.Post-accident Neutron Flux Monitoring Instrumentation Acceptable Alternative to Reg Guide 1.97 ML20212A3581999-09-13013 September 1999 Confirms That Fuel MCPR Data for LaSalle County Station,Unit 1,Cyle 9,sent by Ltr Meets Condition 2,as Stated in 970509 NRC Ltr ML20211Q9911999-09-10010 September 1999 Informs That License SOP-4048-4,for Wp Sly May Be Terminated Due to Individual Retiring ML20212A1141999-09-10010 September 1999 Forwards RAI Re Licensee 990519 Amend Request,Which Proposed to Relocate Chemistry TSs from TS to licensee-controlled Documents.Response Requested by 990930,so That Amend May Be Issued to Support Upcoming Unit 1 Refueling Outage ML20211P2211999-09-0808 September 1999 Forwards Insp Repts 50-373/99-14 & 50-374/99-14 on 990809- 13.No Violations Noted.Insp Concluded That Emergency Preparedness Program Maintained in Good State of Operational Readiness ML20212A8571999-09-0707 September 1999 Informs That Proprietary Document, Power Uprate SAR for LaSalle County Station,Units 1 & 2, Rev 2,Class III, NEDC-32701P,submitted in ,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20211Q6861999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Plant License Applicants During Wks of 001113 & 20. Validation of Exam Will Occur at Station During Wk of 001023 05000374/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl1999-09-0303 September 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl ML20211M1151999-08-31031 August 1999 Requests That Following Eleven Individuals Take BWR Gfes of Written Operator Licensing Exam to Be Administered on 991006 ML20211G1831999-08-27027 August 1999 Provides Addl Clarification of Proposed Refueling Practices Under Proposed Core Alterations Definition Re 990813 Application for Amend to TS ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8731999-08-25025 August 1999 Forwards Insp Repts 50-373/99-13 & 50-374/99-13 on 990804-06 & 09-11.No Violations Noted.Fire Protection Program Strengths Includes Low Number of Fire Protection Impairments & Excellent Control of Transient Combustibles ML20210U3201999-08-17017 August 1999 Forwards Insp Repts 50-373/99-12 & 50-374/99-12 on 990623-0728.No Violations Noted ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000373/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed1999-07-23023 July 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed ML20210E0501999-07-22022 July 1999 Submits Summary of 990630 Management Meeting Re Licensee Performance Activities Since Start Up of Unit 2.List of Attendees & Matl Used in Presentation Enclosed ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20209H5171999-07-15015 July 1999 Discusses 990701 Telcon Re Arrangements for NRC to Inspect Licensed Operator Requalification Program at LaSalle County Nuclear Generating Station for Weeks of 990913,1018 & 1129 ML20209G4031999-07-14014 July 1999 Forwards Insp Repts 50-373/99-11 & 50-374/99-11 on 990614-18.No Violations Noted ML20209E1211999-07-14014 July 1999 Submits mid-cycle Rev of COLR IAW LaSalle County Tech Spec 6.6.A.6.d.Rev to COLR Was Necessary Due to Implementation of TS Change Approved by Ltr Dtd 990212,which Changed Turbine Stop Valve & Turbine Control Valve Scram ML20209F6931999-07-13013 July 1999 Forwards Insp Repts 50-373/99-04 & 50-374/99-04 on 990513-0622.No Violations Noted.Determined That Multiple Challenges to Main Control Room Operators Occurred During Insp Period Due to Human Performance Weaknesses ML20210C1521999-07-0909 July 1999 Forwards Post-Outage (90 Day) Summary Rept for ISI Examinations & Repair/Replacement Activities Conducted from Beginning of First Insp Period of Second ten-yr Insp Interval Through L2R07 Refueling Outage ML20209G3901999-07-0909 July 1999 Informs NRC of Status of Commitments & Requests NRC Concurrence for Use of ASME Section III App F Acceptance Criteria to Permanently Qualify Units 1 & 2 Penetrations M-49 & M-50 ML20209E0341999-07-0909 July 1999 Provides NRC with Siemens Power Corp (SPC) Fuel & GE Fuel MCPR Data for LaSalle Unit 1 Cycle 9.LaSalle Unit 1 Is Currently Scheduled to Start Cycle 9 in 991101 ML20209E0361999-07-0808 July 1999 Forwards LaSalle County Station Unit 2 Cycle 8 Startup Test Rept Summary,Iaw TS NPF-18,Section 6.6.A.1.Startup Test Program Was Satisfactorily Completed on 990501 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196J4711999-06-30030 June 1999 Discusses Closure of GL 92-01,Rev 1,Suppl 1, Rv Structural Integrity, Issued on 950519 to Plant,Units 1 & 2 ML20212J0311999-06-21021 June 1999 Informs of Actions Taken to Close Remaining Open Items in .Attachment Provides Detailed Justification for Closure of Open Items in Sections 5.2.2 & 5.2.8 ML20196B1951999-06-18018 June 1999 Informs NRC That Do Werts,License OP-30373-2,no Longer Requires Use of NRC License for LaSalle County Station. License May Be Terminated ML20195J7761999-06-15015 June 1999 Submits Request Relief CR-23,requesting Relief from Code Required Selection & Examinations of Noted Integral Attachments & Proposes to Utilize Alternative Selection & Examination Requirements Similar to Code Case N-509 ML20196G8021999-06-15015 June 1999 Requests Renewal of SRO License for Vv Masterson.Current License for Vv Masterson Will Expire Jul 1999.NRC Forms 398 & 396,encl.Without Encls ML20195G7101999-06-11011 June 1999 Informs That Effective 990514,GH Mccallum,License SOP-31412, No Longer Requires Use of NRC License for LaSalle Station. License Should Be Terminated ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207D2821999-05-27027 May 1999 Requests That Implementation Date for Unit 1 Be Changed Prior to Startup for L1C10 to Allow Best Allocation of Resources to Implement Unit 1 Amend Prior to Startup for Either L1C9 or L1C10.Unit 2 Will Implement Mod IAW Request 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217H6251999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for MR Kahn,Aj Mclaughlin,De Montgomery & Kr Murphy Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC from 396 Encl.Proprietary Info Withheld ML20217H6341999-10-15015 October 1999 Requests Renewal of Operator Licenses for Listed Personnel. Current Licenses for Kh Curran,Lm Gerlach,Rc Weber & Bt Rhodes Will Expire in Nov 1999.Proprietary NRC Form 398 & NRC Form 396 Encl.Proprietary Info Withheld ML20217F4301999-10-14014 October 1999 Responds to 991012 Rai,Based on 991001 Telcon Re Suppl to Request for TS Change to Revise MCPR Safety Limit & Add Approved Siemens Topical Rept for LaSalle County Station, Unit 1 ML20217C1671999-10-0808 October 1999 Provides Suppl to RAI for Approval of Unreviewed Safety Question Re Assessment of Certain safety-related Concrete Block Walls at LaSalle County Station,Units 1 & 2 05000373/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl1999-10-0404 October 1999 Forwards LER 99-003-00 IAW 10CFR50.73(a)(2)(iv).Commitments for Submittal Also Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr 05000374/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl1999-09-20020 September 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Encl ML20211Q9911999-09-10010 September 1999 Informs That License SOP-4048-4,for Wp Sly May Be Terminated Due to Individual Retiring 05000374/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl1999-09-0303 September 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Encl ML20211M1151999-08-31031 August 1999 Requests That Following Eleven Individuals Take BWR Gfes of Written Operator Licensing Exam to Be Administered on 991006 ML20211G1831999-08-27027 August 1999 Provides Addl Clarification of Proposed Refueling Practices Under Proposed Core Alterations Definition Re 990813 Application for Amend to TS ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000373/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed1999-07-23023 July 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i).Commitments Made by Util Are Listed ML20209E1211999-07-14014 July 1999 Submits mid-cycle Rev of COLR IAW LaSalle County Tech Spec 6.6.A.6.d.Rev to COLR Was Necessary Due to Implementation of TS Change Approved by Ltr Dtd 990212,which Changed Turbine Stop Valve & Turbine Control Valve Scram ML20210C1521999-07-0909 July 1999 Forwards Post-Outage (90 Day) Summary Rept for ISI Examinations & Repair/Replacement Activities Conducted from Beginning of First Insp Period of Second ten-yr Insp Interval Through L2R07 Refueling Outage ML20209E0341999-07-0909 July 1999 Provides NRC with Siemens Power Corp (SPC) Fuel & GE Fuel MCPR Data for LaSalle Unit 1 Cycle 9.LaSalle Unit 1 Is Currently Scheduled to Start Cycle 9 in 991101 ML20209G3901999-07-0909 July 1999 Informs NRC of Status of Commitments & Requests NRC Concurrence for Use of ASME Section III App F Acceptance Criteria to Permanently Qualify Units 1 & 2 Penetrations M-49 & M-50 ML20209E0361999-07-0808 July 1999 Forwards LaSalle County Station Unit 2 Cycle 8 Startup Test Rept Summary,Iaw TS NPF-18,Section 6.6.A.1.Startup Test Program Was Satisfactorily Completed on 990501 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20212J0311999-06-21021 June 1999 Informs of Actions Taken to Close Remaining Open Items in .Attachment Provides Detailed Justification for Closure of Open Items in Sections 5.2.2 & 5.2.8 ML20196B1951999-06-18018 June 1999 Informs NRC That Do Werts,License OP-30373-2,no Longer Requires Use of NRC License for LaSalle County Station. License May Be Terminated ML20196G8021999-06-15015 June 1999 Requests Renewal of SRO License for Vv Masterson.Current License for Vv Masterson Will Expire Jul 1999.NRC Forms 398 & 396,encl.Without Encls ML20195J7761999-06-15015 June 1999 Submits Request Relief CR-23,requesting Relief from Code Required Selection & Examinations of Noted Integral Attachments & Proposes to Utilize Alternative Selection & Examination Requirements Similar to Code Case N-509 ML20195G7101999-06-11011 June 1999 Informs That Effective 990514,GH Mccallum,License SOP-31412, No Longer Requires Use of NRC License for LaSalle Station. License Should Be Terminated ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207D2821999-05-27027 May 1999 Requests That Implementation Date for Unit 1 Be Changed Prior to Startup for L1C10 to Allow Best Allocation of Resources to Implement Unit 1 Amend Prior to Startup for Either L1C9 or L1C10.Unit 2 Will Implement Mod IAW Request ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206R4561999-05-12012 May 1999 Provides Notification That Ws Jakielski,License SOP-30168-3, Is Being Reassigned & No Longer Requires Use of NRC License, IAW 10CFR50.74 ML20206K7081999-05-0707 May 1999 Forwards 10CFR50.46(a)(3) Rept Re Significant Change in Calculated Pct.Loca Analyses for Both GE Fuel & Siemens Power Corp Fuel Demonstrates Results within All of Acceptance Criteria Set Forth in 10CFR50.46 05000373/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(ii).Attachment a Provides Commitments for Submittal1999-05-0707 May 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(ii).Attachment a Provides Commitments for Submittal ML20206K1861999-04-30030 April 1999 Informs That in Comed Submitted Annual Exposure Rept for Personnel Receiving Greater than 0 Mrem/Yr Rather than 100 Mrem/Yr.Updated Rept Limiting Data to Personnel Receiving Greater than 100 Mrem/Yr,Attached ML20206F0931999-04-30030 April 1999 Forwards LaSalle County Nuclear Power Station,Units 1 & 2 Effluent & Waste Disposal Semi-Annual Rept for 1998. LaSalle County Station Tech Specs Recently Revised to Reduce Periodicity of 10CFR50.36a ML20206R0751999-04-30030 April 1999 Forwards License Renewal Applications & Certification of Medical Examinations for LaSalle County Station Personnel Whose Licenses Expire in Nov.Personnel Listed.Without Encls ML20206D5921999-04-28028 April 1999 Forwards Annual Environ Operating Rept for 1998 for Environ Protection Plan, for LaSalle County Station,Units 1 & 2. Rept Includes Info Required by Listed Subsections of App B to Licenses NPF-11 & NPF-18 ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205L8161999-04-0808 April 1999 Advises NRC of Util Review & Approval of Cycle 8 Reload Under Provisions of 10CFR50.59 & Transmit COLR for Upcoming Cycle Consistent with GL 88-16.Reload Licensing Analyses Performed for Cycle 8 Utilize NRC-approved Methodologies ML20205J9451999-04-0505 April 1999 Submits Petition Per 10CFR2.206 Requesting That LaSalle County Nuclear Plant Be Immediately Shut Down & OL Suspended or Modified Until Such Time That Facility Design & Licensing Bases Are Properly Updated ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207J9841999-03-0505 March 1999 Informs That Effective 990212,KC Dorwick Has Resigned & No Longer Requires Use of NRC License for LaSalle County Station ML20207C7251999-03-0101 March 1999 Forwards Annual Rept for LaSalle County Station, for Period of 980101-981231.App E to Rept Provides Info on All Personnel Receiving Exposures of More than 0 Mrem/Yr Rather than 100 Mrem/Yr Requirement of TS 6.6.A.2 ML20207F9581999-03-0101 March 1999 Requests That Initial License Examination Currently Scheduled for Weeks of May 15 & 22,2000 Be Changed to Weeks of Nov 13 & 20,2000.Class Size Is Projected to Be Twelve RO & SRO Candidates ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207C8401999-02-25025 February 1999 Forwards Rev 60 of Comed LSCS Security Plan,Iaw 10CFR50.4(b) (4).Rev Eliminates Requirement for Annual change-out of Vital & PA Keys & Locks & re-configuration of PA Fence Around North Access Facility.Rev Withheld ML20207A9361999-02-24024 February 1999 Forwards Rev 4 to Restart Plan,To Reflect Review,Oversight & Approval Process Necessary to Restart Unit 2.Review & Affirmation Process Will Focus on Station Capability to Support Safe Dual Unit Operations 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059H5321990-09-11011 September 1990 Requests Withdrawal of Application for Amend to Licenses NPF-11 & NPF-18,per 891215 & s.Amend Would Have Removed Applicability of Tech Spec (TS) 3.0.4 to TS 3.6.5.2, Secondary Containment Automatic Isolation Dampers ML20059H4271990-09-0707 September 1990 Provides Supplemental Response to NRC Bulletin 90-001.Plant Initial Review of Calibr Records Completed on 900831 ML20059G0941990-09-0505 September 1990 Forwards LaSalle County Station Unit 2 Third Refueling Outage,Asme Section XI Summary Rept for Spring 1990 Insp ML20059C6891990-08-30030 August 1990 Forwards LaSalle County Nuclear Power Station Unit 2,Cycle 4 Startup Test Rept & Test Rept Summary ML20056B4061990-08-21021 August 1990 Submits Supplemental Response to Generic Ltr 88-14 Re Design & Verification of Instrument Air Sys.Mfg Purchase Specs & Vendor Manuals Reviewed for Air Quality Requirements ML20059B8961990-08-14014 August 1990 Documents Approval of Schedular Extension & Accepts Human Engineering Discrepancies Discussed ML20059D1731990-08-10010 August 1990 Responds to NRC Re Exercise Weaknesses Noted in Insp Repts 50-373/90-05 & 50-374/90-06.Corrective Actions: LOA-FP-01, Fire Alarm Response Will Be Revised to Alert Control Room Operators to Refer to Emergency Action Levels ML20058N2971990-08-0606 August 1990 Forwards Rev 34 to Security Plan.Rev Details Addl Gate Position for Security Testing & Maint.Rev Withheld (Ref 10CFR73.21) ML20064A5491990-07-27027 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-12 & 50-374/90-13.Corrective Actions:Program Implemented Identifying & Correcting Repetitive Local Leak Rate Failures Through Testing & LER Investigation ML20056A7031990-07-27027 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-13 & 50-374/90-14.Corrective actions:LRP-1250-3 Revised to Include Addl Requirement for Extremity Monitoring ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML20055H7661990-07-24024 July 1990 Forwards Supplemental Response to Generic Ltr 90-04, Status of Licensee Implementation of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions ML20055G2011990-07-13013 July 1990 Forwards Corrected Monthly Operating Rept for June 1990 for LaSalle County Unit 1.Outage/Reduction 16 Corrected ML20055F1831990-07-0909 July 1990 Provides Status Rept on Breaker Replacements in Response to NRC Bulletin 88-010.Breaker Replacements for Plants Scheduled to Be Completed by 901031 ML20044B1751990-07-0909 July 1990 Responds to NRC Request for Addl Info Re Util 890726 Proposed Amend to Tech Specs to Allow Continued Operation for Period of 12 H W/Main Steam Tunnel High Ambient Temp & High Ventilation Sys Differential Trips Bypassed ML17202L2861990-07-0202 July 1990 Forwards Dresden II Upper Vessel Contract Variation Review, La Salle II Upper Vessel Fabrication Summary & Quad-Cities II Upper Vessel Fabrication Summary. ML20055D1921990-06-29029 June 1990 Responds to Generic Ltr 90-04 Re Status of Licensee Implementation of Generic Safety Issues ML20055J2021990-06-26026 June 1990 Responds to NRC Re Violations Noted in Insp Repts 50-373/90-06 & 50-374/90-06.Corrective Actions:Perimeter Zone Repairs Commenced on Schedule & Completely Functional & Out of Compensatory Measures on 900614 ML20044A5071990-06-22022 June 1990 Forwards Revised Response to Station Blackout Rule for Plant.During Blackout Event,Plant Can Utilize RCIC Sys or HPCS to Provide Required Reactor Vessel Inventory Makeup ML20043E8651990-06-0707 June 1990 Forwards Relief Request RV-57 for Emergency Fuel Pool Makeup Crosstive Vent Valve 1(2)E12-F097.Expedious Review of Request Requested Because Valve 1(2)E12-F097 Inoperable & Will Remain So Until NRC Approval Received ML20043D3221990-06-0101 June 1990 Forwards Rev 33 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043C8241990-06-0101 June 1990 Advises of Intentions to Review & Approve Cycle 4 Reload,Per 10CFR50.59 & Forwards Rev 1 to LAP-1200-16, Core Operating Limits Repts for LaSalle County Station Unit 2,Reload 3, Cycle 4, Per Generic Ltr 88-16 ML20043B6581990-05-25025 May 1990 Requests Schedular Extension of Two Human Engineering Deficiencies Re CRT Displays W/Current Ramtek Sys & Approval to Leave Seven Human Engineering Discrepancies Accepted as Is. ML20043B7921990-05-23023 May 1990 Forwards Endorsements 14 to Nelia Policy N-71 & Maelu Policy M-71 & Endorsements 12 to Nelia & Maelu Policies N-83 & M-83,respectively ML20042E8841990-04-30030 April 1990 Responds to Generic Ltr 89-04 Re Weaknesses of Inservice Testing Programs.Plant Has Implemented Rev 2 of Inservice Testing Program Submitted by Util 891002 & 24 Ltrs.No Equipment Mods Required as Result of Generic Ltr ML20042F3591990-04-29029 April 1990 Provides Suppl Response to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Precaution Added to Operating Procedures Which Allows ECCS Pump to Be Secured & Restarted as Necessary to Preclude Running Pumps at Min Flow ML20042F0341990-04-23023 April 1990 Forwards Part 3 to 1989 Operating Rept,Containing Results of Radiological Environ & Meteorological Monitoring Programs. W/O Encl ML20064A6281990-03-30030 March 1990 Submits Supplemental Response to Insp Repts 50-373/86-04 & 50-374/86-04 Re Fire Detection Concerns,Per NRC 900214 Request.Proposed Administrative Controls & Training Will Eliminate Concerns That Assure Protection of Personnel ML20055E1461990-03-29029 March 1990 Provides Supplemental Response to Re Violations Noted in Insp Repts 50-373/89-18 & 50-374/89-18 on 890724- 0825.Corrective Actions:Plant Performs Safety Evaluation for Mods Not Designed by Corporate Nuclear Engineering Dept ML20012C6991990-03-15015 March 1990 Forwards Corrected Tech Spec Page to 881129 Application for Amend to Licenses NPF-11 & NPF-18,removing Specific Load Profiles for Each Dc Battery ML20012B6541990-02-26026 February 1990 Forwards LaSalle County Station Unit 1 Third Refueling Outage ASME Section XI Summary Rept, for Fall 1989 Inservice Insps Performed.Conditions Observed & Corrective Measures Taken Also Contained in Rept ML20006E7421990-02-0909 February 1990 Responds to NRC 900110 Ltr Re Violations Noted in Insp Repts 50-373/89-23 & 50-374/89-22.Corrective Actions:Ltr from Station Manager to All Dept Heads Was Issued on 891218, Discussing Personnel Performance Issues ML20005F5771990-01-0808 January 1990 Documents Guidance Given by P Shemanski Re Typos in Earlier Approved Amend to License NPF-11.Guidance Should Adhere to Wording of Unit 2 Tech Specs.Guidance Given on 900105 & Will Be Followed Until Correction Made at NRR Ofcs ML20011D9661989-12-22022 December 1989 Forwards Core Operating Limits Rept for LaSalle County Station Unit 1,Reload 3 (Cycle 4). Intention to Review & Approve Cycle 4 Reload Under Provisions of 10CFR50.59 Stated ML20005E1661989-12-22022 December 1989 Forwards Rev 32 to Security Plan,Reflecting Administrative Changes in Mgt Structure at Facilities.Rev Withheld (Ref 10CFR73.21) ML19332E4531989-11-29029 November 1989 Responds to Generic Ltr 89-21, Status of Implementation of USI Requirements. Response to USI A-48 Expected by 900319 ML19332C2461989-11-0808 November 1989 Provides Supplemental Response to Insp Repts 50-373/88-05 & 50-374/88-05 on 890302-10.Scheduled Completion Dates for Sample Panel Mods Changed from Third to Fourth Refueling Outages of Each Unit ML19325E5191989-10-31031 October 1989 Forwards Qualification Test Rept QTR87-018, Max Credible Fault Tests CM249-Q2 Carrier Modulator for Fermi 2 SPDS, in Response to NRC 890304 Request for Addl Info Re Facility Validyne Isolator CM-249 ML19325E3601989-10-26026 October 1989 Forwards Addl Info Re Application for Amend to Licenses NPF-11 & NPF-18,revising Tech Specs to Conform W/Diesel Generator Test Schedule Recommendations,Per Generic Ltr 84-15 ML19325E7921989-10-24024 October 1989 Submits Response to SALP 8 Board Repts 50-373/89-01 & 50-374/89-01.Expresses Appreciation for NRC Recognition of High Level of Performance in Area of Plant Operations, Emergency Preparedness & Security ML19325E0941989-10-24024 October 1989 Forwards Clarification to Summary of Changes Made in Rev 2 to Plant Inservice Testing Program ML19353A9051989-10-23023 October 1989 Responds to NRC 890921 Ltr Re Violations Noted in Insp Repts 50-373/89-19 & 50-374/89-19.Corrective Actions:Hose Connection That cross-connected Svc Air Sys W/Clean Condensate Sys Uncoupled & Secured ML17285A8081989-10-18018 October 1989 Responds to Request for Info on Environ Qualification of Taped Electrical Splices.Scotch Tapes Allowed by Electrical Test Guide Included Scotch 33,23 & 70 ML19325D1931989-10-13013 October 1989 Forwards Quarterly Rept on Static-O-Ring Failures Third Quarter 1989,per IE Bulletin 86-002.Stated Switches Replaced ML19327B0431989-10-0505 October 1989 Responds to NRC 890821 Ltr Re Violations Noted in Insp Repts 50-373/89-15 & 50-374/89-15.Corrective actions:post-order for Assembly Revised to Provide Specific Guidance on Use of Siren & Loudspeaker on Mobile Vehicles During Assemblies ML19327A7491989-10-0202 October 1989 Forwards Rev 2 to Combined Units 1 & 2 Inservice Testing Program for Pumps & Valves. Implementation of Program Will Require Procedure Revs Expected to Be Completed by 900228 ML19325D3271989-10-0202 October 1989 Forwards Rept Re Findings & Conclusions of Investigation Re 890826 Scram ML20248D0881989-09-21021 September 1989 Forwards Rev 56 to QA Program Topical Rept CE-1-A ML20247Q6431989-09-21021 September 1989 Documents Relaxation of Commitment Re Disassembling & Insp of Sor Switches ML19327A7681989-09-18018 September 1989 Forwards Response to Allegations Re Potential Employment Discrimination.Encl Withheld (Ref 10CFR2.790(a)(7)) 1990-09-07
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2 -[. q [f Commonwealth Edison y5 l One First National Plaza. Chicage llano 4*
h,9h l Address Reply to Post Office Box 767 l Chicago. Ilhnois 60690 l
November 26, 1985 Mr. James M. Taylor, Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
LaSalle County Station Units 1 and 2 Response to Notice of Violation and Proposed Imposition of Civil Penalty Inspection Report Nos. 50-373/85-023 and 50-374/85-018 (EA 85-95)
Reference:
J. G. Keppler letter to J. J. O'Connor dated September 27, 1985.
Dear dr. Taylor:
This is Commonwealth Edison Company's (Edison) response to the above referenced Nuclear Regulatory Commission's (NRC) Notice of Violation, Proposed Imposition of Civil Penalties and accompanying inspection report.
As we agreed, this response has been submitted within 60 days of the Notice rather than within the 30 days originally provided. We appreciate the opportunity that this extension of time has given us to explain in detail Edison's comprehensive program for addressing the matters at issue here.
Because Edison does not protest the fine, this letter is accompanied by a check as payment in full of the $125,000.00 penalty.
Edison appreciates the significance of the deficiencies identified-in the Notice. Our program to ensure the safe operation of our nuclear facilities depends in part on ensuring the correct implementation of plant modifications. Edison acknowledges that the events which gave rise to these deficiencies were unacceptable. To ensure that similar incidents will not recur. Edison has initiated the extensive corrective action discussed below for boh the Station and the General Office.
The attachment to this letter describes the wide range of measures, both Immediate and long term, which have been instituted by the LaSalle County Nuclear Power Station and General Office management. The immediate measures: (1) ensured that the violations were corrected; (2) determined that no similar violations had gone undetected; and (3) instituted new procedures to prevent a recurrence of similar events. Among the significant longer term measures are the establishment of a committee which, for a trial period, will review post-modification tests for their ability to determine the operability of the modified equipment and the development of a checklist for helping to choose appropriate tests for modified equipment.
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l J. M. Taylor November 26, 1985 l
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These measures demonstrate Edison's continuing commitment to the operational safety of its nuclear stations. Edison believes that such safety i L will be enhanced by the corrective actions described in this letter and its i
attachment and, therefore, that the LaSalle County Nuclear Power Station will continue to operate in a manner that fully ensures public health and safety.
Very truly yours, ,
C,dOk 09a Cordell Reed Vice-President im Attachment cc: J. G. Keppler - Region III ,
LaSalle Resident Inspector SUBSCRIBED AND SWORN to before me this M _ day of9)lNnh to , 1985 sl50h&&w Notary Public i
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i ATTACHMENT RESPONSE TO NOTICE OF VIOLATION 1A. Technical Specification 3.3.3.b requires that with one or more Emergency Core Ccoling System (ECCS) actuation instrumentation channels inoperable take the action required by Table 3.3.3.1.
Table 3.3.3.1 in Action 30 requires that when the number of operable channels is less than the required minimum of two, place the inoperable channel in the tripped condition within one hour or declare the associated system inoperable.
Contrary to the above, from 3:30 a.m. on June 5, 1985 until 12:10 p.m. on June 10, 1985 when the number of operable channels was less than the required minimum of two, the inoperable ECCS actuation instrumentation channel was not placed in the tripped condition within one hour and the associated system was not declared inoperable.
ADMISSION OR DENIAL OF TFE ALLEGED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation resulted from our reliance on post-modification tests which did not accurately determine the cperability of the modified Division 1 Low Reactor Water Level Switches.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED
- 1. Initial Responses As soon as it was discovered that the instruments were inoperable, one of the switches was placed in the tripped condition as required by Action 30 of Table 3.3.3.1 of Technical Specification 3.3.3.b.
l Appropriate Station Personnel and General Office Management were also informed of the event. Shortly thereafter, the errors were corrected and an investigation was initiated into the causes of the events. The results of these investigations provided bases for
! additional actions intended to prevent recurrence of similar events.
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- 2. Further Actions To ensure that no other problems of this type had been missed, several broader actions were taken.
All safety-related modifications made during the Unit 2 outage were reviewed by either the Commonwealth Edison Station Nuclear Engineering Department (SNED) or the architect-engineer. No serious discrepancies requiring further physical changes were discovered. Also, either SNED, the station or the architect-engineer walked down all accessible '
safety-related modifications made during the Unit 2 outage. The architect-engineer also reviewed for completeness the results of our walkdowns. As a result of these walkdowns, only minor discrepancies between the design documents and as-built configurations were discovered. Only one, a labeling deficiency, required correction in the field. For the others, we have corrected the appropriate documents.
Moreover, a Quality Control Inspector independently walked down one hundred twenty-four of tne instruments modified during the outage.
All of the test requirements specified in the safety-related work requests and modifications performed during the outage were reviewed completely. Also, it was verified, prior to restart, that all modified instruments would perform as designed.
- 3. Training All departments involved conducted informal documented training sessions to discuss the event, its causes, and the corrective actions being ta':en to prevent its recurrence. This training was accomplished in two steps. First, prior to startup, appropriate personnel in the instrument maintenance, electrical maintenance, and operating departments were trained. After startup, relevant personnel in construction, maintenance, technical staff, and quality control, as well as contractor personnel were also trained. At each of these sessions the significance of the events and their unacceptability were emphasized.
We believe that these training sessions have strengthened post-modification testing procedures by increasing awareness of the need to ensure that testing accomplishes its intended function.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION
- 1. Revised Modification Procedures Our analysis of these events led us to change significantly the station's procedures governing the types of actions involved here.
These chances in procedure substantially strenothen the orocess for ensuring that post-modification tests are adequate.
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The Station's administrative procedure for plant modifications, LAP 1300-2, has been revised as follows:
- a. The procedure now explicitly requires the preparation of post-modification tests in accordance with the newly established
" Guidelines for Development of Tests for Modifications" LTP 800-9. These guidelines provide methods for developing tests to ensure that system and component operability are adequately demonstrated after modification. Our confidence in these guidelines is based, in part, on the following new approach incorporated in them. Instead of focusing testing on only modified equipment, testing, where warranted, will now be extended to unmodified parts of a system. By varying input signals at those points in the system and observing the corresponding responses in the modified part of the system we will be better able to verify the operability of the modification. In particular, this procedure would have helped to ensure the proper installation of instrument piping to pressure differential DP type instrumentation.
- b. These incidents have also led us to realize the importance of developing in one persun an attitude of responsibility for all aspects of a modification. Accordingly, the procedures now require the cognizant modification engineer to be more involved with the installation and testing of modifications. This greater involvement includes maintaining overall knowledge of a modification's design and status, assuring that design intent is implemented in the modification as installed and monitoring progress on the design, installation and testing of a modification.
- 2. Checklists These incidents have also demonstrated the limited effectiveness of checklists used to determine system operability. Such checklists were developed after April,1985 in response to an incident involving inoperability of a train of the Standby Gas Treatment System. Although it was believed that such checklists would be adequate, there was only a limited period of time in which to assess the adequacy of those checklists before the June,1985 events occurred. Because experience has now shown that checklists limited to system inoperability are not always adequate, the maintenance and operating departments have developed additional checklists which go beyond previous lists by now requiring some testing at the component level. This consideration of finer levels of detail should aid in the selection of testing requirements adequate to demonstrate operability after either maintenance or. modification. Accordingly, it is believed that these new lists will help to prevent recurrence of these types of events.
- 3. Review Committee To further ensure the adequacy of tests of safety-related modifications, an additional level of review of post-modification tests for their ability to determine the operability of modified equipment has been established. This review will be conducted by a committee which will include the Technical Staff Supervisor, an Operating Engineer or an Assistant Superintendent, and the cognizant Modification Engineer. This committee will review the adequacy of any modified equipment before it is declared operable.
DATE WHEN FULL COWLIANCE WILL BE ACHIEVED Full Compliance has been achieved. The effectiveness of the Review Committee will be _ evaluated by March,1986 to determine whether the committee should become a permanent part of the post-modification review process.
- 18. Technical Specification 3.5.2 requires at least two Emergency Core Cooling Systems (ECCS) to be operable in the shutdown condition.
With both of the required subsystems / systems inoperable, one subsystem must be restored to operable status within four hours or secondary containment integrity be established within the next eight hours.
Contrary to the above, with the three ECCS Divisions inoperable on June 5, 1985, secondary containment integrity was not established within eight hours.
ADMISSION OR DENIAL OF THE ALLEGED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION Same as in Item 1A.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED Secondary Containment integrity had been reestablished before it was discovered that the Division I ECCS Systems were inoperable. No further corrective action was nece sary.
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CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION Refer to Item 1A.-
' DATE WHEN FLLL COWLIANCE WILL BE ACHIEVED Full' Compliance has been achieved.
IC. 10 CFR Part 50, Appendix B, Criterion VI, as implemented by the
. Commonwealth Edison Company's Quality Assurance Manual, Quality Requirement 6.1, requires that a document control system be used to assure that documents such as drawin's be distributed to and used at the locations where the prescribed activity is performed.
Contrary to the above, Field Change Request 85-123 dated April 4, 1985 was issued to' correct an error in Modification M-1-2-84-136; however, it was not distributed to and used at the location where the prescribed activity was performed. As a result, piping for two switches was installed backwards rendering Division I of the Unit 2 Emergency Core Cooling Systems inoperable.
. ADMISSION OR DENIAL OF TIE ALLEED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation' resulted from an inadequate document control procedure.
The Station's procedure for controlling Field Change Requests (FCR) did not require the FCR's to list contractor drawings. Therefore, FCR 85-123.did not list all of the drawings for revisions to the instal-lation details for 22 instruments. For 20 of those instruments, the installation details had been revised on the contractor's drawings. For i the remaining two instruments, the contractor's production drawings reflected only the original designs because the drawings had not been
-modified in accordance with the FCR. The FCR had not indicated that those drawings would be affected.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED
.The installation of the two instruments was corrected and tested to demonstrate the proper. reinstallation. To ensure that similar problems had not been missed, all other FCR's nenerated durina the outage were 7
reviewed, and found not to contain any further errors.
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r CORRECTIVE ACTION TAKEN TO AVOID FURTFER VIOLATION To prevent a recurrence of this type of error, we have added mandatory cross-references to the Stations' procedures. Station Administrative Procedure LAP 1300-5 " Field Change Requests" has been revised to require an FCR to include a list of all affected documents / drawings, including contractor production drawings. In addition, both the mechanical and the electrical contractors have prepared and implemented procedures to formalize the control of FCR's and requirements for Quality Control field inspection. These procedures require checks to ensure that FCRs are properly posted to all affected drawings.
DATE WHEN FULL COM3LIANCE WILL BE ACHIEVED Full compliance his been achieved.
- 10. 10 CFR Part 50, Appendix B, Criterion X, as implemented by the Commonwealth Edison Company Quality Assurance Manual, Quality Requirement 10.1, requires that Quality Assurance inspections be conducted at the site during modification activities to verify conformance to applicable drawings.
Contrary to the above, Quality Assurance inspections were not conducted at the site during Modification M-1-2-84-136 to verify conformance to the applicable drawing (FCR 85-123).
ADMISSION OR DENIAL OF THE ALLEGED VIOLATION Connonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation resulted from a failure to specify adequate hold points in the instructions for installing modifications.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED All accessible elements of the modifications performed during the outage were completely walked down . To ensure an independent review, this walkdown was conducted by persons who had not been involved with the installations. Moreover, the results of these walkdowns were documented.
It was found that all final installations were in acenrd with the approved final designs.
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- s CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION Station procedures have been substantially modified to ensure that inspections will be conducted during modification activities. LaSalle has developed and implemented an administrative procedure LAP 1700-3,
" Guidelines for Quality Control Hold Points". This procedure provides guidance to Station Quality Control and Contractor Quality Control personnel in establishing hold points. That guioance requires mandatory hold points for field inspections to verify that safety related modifications have been installed in accordance with approved drawings and specifications.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full Compliance has been achieved.
IE. 10 CFR Part 50, Appendix B, Criterion XI, as implemented by the Commonwealth Edison Company Quality Assurance Manual, Quality Requirement 11.1, requires that the test program include those tests necessary to demonstrate that systems will perform satisfactorily in service following plant maintenance or modifications.
Contrary to the above, Operational Test LIS-N8-204 performed following U1e completion of Modification M-1-2-84-136 did not adequately demonstrate system operability in that the test only verified the instrument and electrical connections. The piping configuration of the reactor pressure vessel water level reference and variable legs was not verified.
ADMISSION OR DENIAL OF THE ALLEGED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation resulted from an inadequate post modification test which was improperly limited to testing the instrument and its electrical connections.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED l To ensure that similar problems in other equipment had not been l overlooked, all safety-related instrumporation m,dified durinn tha outage was retested. The retests verified correct instrument response to varying process parameters. All installation errors identified were corrected and retested to verify that the final "as installed" plant condition reflected the "as designed" condition.
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- l' CORRECTIVE ACTION TAKEN TO AVOID FURTE R VIOLATION We believe that the new procedures discussed above in Item I.D will prevent a recurrence of this event. Those procedures, especially the new guidelines for identifying adequate post-modification tests and, in the interim, the committee review of those tests for adequacy, should ensure that all relevant parameters are tested and verified.
DATE WHEN FULL COW LIANCE WILL BE ACHIEVED Full Compliance has been achieved.
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2A. Technical Specification 3.3.2 requires the isolation actuation instrumentation channels shown in Table 3.3.2-1 to be operable with their trip setpoints set consistent with the values shown in Table 3.3.2-2. The Residual Heat Removal (RHR) shutdown cooling pump suction high flow instrumentation is included for Operating Conditions 1, 2, and 3. Technical Specification 3.3.2.c. requires that with the number of operable channels less than the minimum operable channels per trip system required for both trip systems, place at least one trip system in the tripped condition within one hour and take the action required by Table 3.3.2-1. Action Item 25 of Table 3.3.2-1 requires the isolation valves to be closed and locked for the RHR shutdown cooling mode and the system to be Jeclared inoperable.
Contrary to the above, from April 7, 1985 until July 12, 1985, while the plant was in Operating Conditions 1, 2, and 3, the Unit 1 RHR shutdown cooling pump suction high flow sensors would not have met the designated isolation setpoint in that the isolation actuation instrumentation channels were inoperable. With the channels inoperable, the actions required by Action Item 25 of Table 3.3.2.1 were not taken. The isolation valves were not closed and locked for the RHR shutdown cooling mode and the system was not declared inoperable.
ADMISSION OR DENIAL OF THE ALLEGED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation resulted fran our reliance on post-modification tests which did not accurately determine the operability of the RHR Shutdown Cooling High Flow isolation switches.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED The discovery of the inoperable switches was made when the plant was in an Operational Condition which did not require those switches to be operable. Accordingly, no immediate action was required. Before entering an Operational Condition in which those switches were required to be operational, the piping errors were corrected, and it was verified that the switches could perform their isolation functions, rn4RfrTTvF Ar*TinN TAL'FM TO AVOIO FURTHER VIOLATION Refer to Item 1A.
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DATE WHEN FlLL C0bPLIANCE WILL BE ACHIEVED Full Compliance has been achieved.
2P. 10 CFR Part 50, Appendix B, Criterion VI, as implemented by the Commonwealth Edison Company's Quality Assurance Manual, Quality Requirement 6.1, requires that a document control system be used to assure tha*. documents such as drawings, be distributed to and used at the locations where the prescribed activity is performed.
Contrary to the above, Drawing Change Request 7383, issued to document a piping change to Modification M-1-1-82-054, was not distributed to and used in the development of Modification M-1-1-84-091. As a result, the Unit 1 Regenerative Heat Removal shutdown (RHR) pump cooling suction flow isolation channels were inoperable during power operations from April 7, 1985 until the unit was shutdown on July 12, 1985.
ADMISSION OR DENIAL OF THE ALLE ED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION This violation resulted from the failure to ensure that changes to the plant were reflected on current plant drawings. The violation occurred as described below.
On May 10, 1982 it had been discovered that the original flow switches lE31-N012A and lE31-N0128 were piped backwards due to the High and Low Process Lines being reversed inside the Suppression Pool. Accordingly, WR #L15576 and modification #M-1-1-82-054 were issued to correct the piping and (in addition) install pressure snubbers. Snubbers were added and the repiping was performed by reversing the tubing locally at the instrument rack. Upon satisfactory resolution of M-1-1-82-054, Drawing Change Request #73-83 was submitted to reflect: (1) The inclusion of pressure snubbers, and (2) the changes to the process line, root valve, and Excess Flow Check Valve numbers associated with lE31-N012A and B (with the Drywell Penetration Numbers remaining the same). Based on their request for more information with regard to the snubber installa-tion, the Architect Engineer (A/E) rejected DCR 73-83. OCR 73-83 (which included the revised drawing #M-2096-5) was inadvertently closed out without the appropriate changes being made. Therefore, when lE31-N012A and R warp rpmnvad and later rpnlanaq hy IFT1 uni?an/DA/Aa/RA, their process inputs (High vs Low) became crossed, due to drawing #M-2096-5 having never been revised.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED Our investigation of the situation revealed that it had resulted from a failure to properly complete action on a Drawing Change Request (DCR).
To ensure that similar problems had not been overlooked, the Station's, the Architect Engineer's (A/E), and the Station Nuclear Engineering Department's (SNED), Drawing Change Request logs were reviewed to identify DCRs which had been rejected or cancelled. All rejected, open or cancelled DCR's were verified to reflect properly on the critical drawings and/o' r the appropriate drawing aperture cards. No further discrepancies were found. The DCR for Modification M-1-1-84-91 reflected the previously rejected drawing change request.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION This incident alerted us to a procedural deficiency in our handling of DCR's. On that basis, SNED initiated a review of its procedure for control of DCR's. This review indicated that SNED had revised its DCR procedure in August 1984 to provide a specific procedure for handling DCRs rejected or cancelled by the A/E. This procedure was not in effect at the time this incident occurred. It is believed that the current procedure will prevent the recurrence of a similar problem.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED Full compliance has been achieved.
< 2C. 10 CFR Part 50, Appendix B, Criterion XI, as implemented by the Commonwealth Edison Company Quality Assurance Manual, Quality Requirement 11.1, requires that the test program include those tests necessary to demonstrate that systems will perform satisfactorily in service following plant maintenance or modifications.
Contrary to the above, the post-installation testing performed following the completion of Modification M-1-1-84-091 did not adequately demonstrate system operability in that the test did not detect that the Regenerative Heat Removal pump suction high flow
. isolation switches were piped backwards prior to returning the instruments to service.
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' ADMISSION OR DENIAL OF THE ALLEED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE-VIOLATION See Item 2A.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED See Item 2A.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION Refer to Item 1A.
DATE WHEN FULL COWLIANCE WILL BE ACHIEVED Full Compliance has been achieved.
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- 3. '10 CFR Part 50, Appendix B, Criterion XI, as implemented by the Commonwealth Edison Company Quality Assurance Manual, Quality Requirement 11.1, requires that the test program include those tests necessary to demonstrate that systems will perform satisfactorily in service following plant maintenance or modifications.
Contrary to the above, during this inspection period, the operability test for two Unit 2 shutdown cooling high flow isolation switches was not performed correctly. Specifically, walkdown of the piping
'to these switches identified no problems although the piping to the switches was installed backwards. This error was discovered by an alternate test that was not specified for proof of operability testing.
, ADMISSION OR DENIAL OF THE ALLEGED VIOLATION Commonwealth Edison admits the violation.
REASON FOR THE VIOLATION As a result of previously identified installation errors a system
. walkdown was designated in June, 1985 as corrective action to verify that all piping was installed in accordance with design drawings modified during the outage. A Technical Staff Engineer was assigned to perform.a walkdown of the RHR Shutdown Cooling pump suction high flow isolation switches. The Engineer who performed the walkdown had traced the piping to a wall penetration and when he went to the other side of the wall he reoriented himself with informal markings on the piping which were reversed. The remainder of the inspection was performed utilizing the reversed reference.
CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED Our investigation to determine the cause of the walkdown error identified the problems that could have contributed to it. As a result, a second walkdown of all process instrumentation piping which penetrated walls was conducted by two Technical Staff personnel, one on either side of the wall. Moreover, all differential pressure instrumentation was verified by performing a second test by varying the process which the .
instrumentation measured. The piping was corrected and it was verified that the installation was correct by conducting a retest which measured flow in the system.
CORRECTIVE ACTION TAKEN TO AVOID FURTHER VIOLATION Refer to Item 1A.
-OATE WEu r:1L com LInwrc wits _ w Am IEyEO Full Compliance has been achieved.
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