ML20137H068

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Forwards Response to Violations Noted in Insp Repts 50-282/97-02 & 50-306/97-02.Corrective Actions:Movement of 22 RCP Upper Bracket & Rotor Back to Stator Place on Hold Until Specific Procedure Could Be Written & Approved by Oc
ML20137H068
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 03/26/1997
From: Sorensen J
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
IEB-96-002, IEB-96-2, NUDOCS 9704020049
Download: ML20137H068 (18)


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, Northern States Power Company Prairie Island Nuclear Generating Plant 1717 Wakonade Dr. East Welch, Minnesota 55089 March 26,1997 10 CFR Part 2  ! l U S Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 l PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket Nos. 50-282 License Nos. DPR-42 50-306 DPR-60  ; Reply to Notice of Violation (Inspection Report 97002), inadequate Procedural Control for Management of Heavy Loads i l Your letter of February 25,1997, which transmitted Inspection Report No. 97002, l required a response to a Notice of Violation. Our response to the violation is contained  ; in the attachment to this letter. Note that this response discusses three heavy load lifts, not just the one discussed in the Notice of Violation. The reason we are presenting it ' this way is because of the relationship between the three lifts, the total heavy load control program at Prairie Island, and the corrective actions necessary to address all of the issues associated with the total heavy load program. Rather than singling out the problems with this one lift and the corrective actions to address only those problems, it is more appropriate to discuss the whole picture in one report. In this response we have made no new Nuclear Regulatory Commission commitments; those corrective steps that will be taken to avoid further violations, discussed in the response, have already been committed to in our Licensee Event Report for Unit 2 (LER 2-97-01), dated March 17,1997. I 9704020049 970326 [ h' I l PDR ADOCK 050oo282 G PDR 0.10039 gippllppip,liRJW I

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     ,                                                                                               i USNRC                                           NORTHERN STATES POWER COMPANY             l
March 26,1997  ;

Page 2 - l i Please contact Jack Leveille (612-388-1121, Ext. 4662) if you have any questions , related to this letter. ,

.                                                                                                    i i                                                                                                    t 3

Joel P Sorensen l Plant Manager Prairie Island Nuclear Generating Plant c: Regional Administrator - Region lil, NRC , Senior Resident inspector, NRC NRR Project Manager, NRC J E Silberg

Attachment:

RESPONSE TO NOTICE OF VIOLATION I l IR97002. DOC

i ! i ) - - RESPONSE TO NOTICE OF VIOLATION  ! VIOLATION j 10 CFR 50, Appendix B, Criterion V, " Instructions, Procedures, and i j Drawings," required, in part, that activities affecting quality shall be l l prescribed by documented instructions, procedures, or drawings of a type  ; i appropriate to the circumstances and shall be accomplished in accordance  ; with these instructions, procedures, or drawings. { { ) _ Contrary to the above, on February 19,1997, during movements of heavy  ; l loads with a mobile crane in the Unit 2 side of the plant screenhouse, l , Procedure D58, Revision 26, " Control of Heavy Loads," was not appropriate j

to the circumstances because it did not contain adequate administrative l controls for handling heavy loads over or in proximity to safe shutdown j- equipment located in the screenhouse nor instructions for evaluating the use of mobile cranes from a reactor safety standpoint in general.

{ L j This is a Severity Level IV Violation (Supplement 1). j p . I RESPONSE TO VIOLATION  ! } Backaround  ! i l

On January 24,1997, Unit 2 was taken off-line and shutdown in preparation for i j refueling.' It remained shutdown throughout the period during which the three events  !

I described here occurred. First Heavy Load Lift in Violation of D58 Requirements: (Figure 1) On 2/4/97, it was determined that 22 Reactor Coolant Pump (RCP) upper bracket and rotor (heavy load - 21 tons) was moved over irradiated fuel on 2/3/97, without a specific load handling procedure defining the safe load path and without containment j isolated (Figure 1); This occurred when the RCP upper bracket and rotor, which are I handled as a unit, were being moved from the RCP vault to the motor stand as part of ' ) the 10 year RCP motor inspection under WO_9608888. (Note that WO is the beginning designator for work order numbers.) The movement of this heavy load in

                          ~ containment did not follow the reactor building safe load path requirements stated in Operations Manual Section D58, Control of Heavy Loads. (Note that all documents referred to in this report as Dxx are Operations Manual Section procedures.) D58 states that "With the reactor head removed, loads greater than 2100 lb. SHALL NOT be moved within 15 horizontal feet of the irradiated fuel without specific written procedures per step 5.3.5" and containment isolation requirements satisfied.                                   ;

1 Second Heavy Load Lift Using a Mobile Crane: (Figure 2) The second event involving the control of heavy loads occurred on 2/19/97, when 22

I . h.997

                 .        .                                                           Page 2 i               Circulating Water (CW) Pump motor was being reinstalled under WO 9700434. This heavy load was being moved with the use of a mobile crane near safe shutdown
equipment located in the Screenhouse (Figure 2). D58 was reviewed before moving i the heavy load, but D58 does not contain specific guidance pertaining to the use of
mobile cranes. Before the heavy load was moved the safe load path was considered j and the designated load path discussed with the mobile crane operator and riggers j . performing the lift. The movement of this heavy load was not over any of the safe i shutdown equipment located in the Screenhouse.

! Third Heavy Load Lift Using a Fork Lift: (Figure 3) !: The third event involving the control of heavy loads occurred on 2/25/97, when a concrete trench cover was removed from the Unit 2 Auxiliary Building trench under WO 9614795. The trench cover was removed to allow ASME XI Inservice inspection j (ISI) of pipes in the trench from the Refueling Water Storage Tank (RWST) to the - l Containment Spray Pump (CSP) room. The concrete trench cover, which weighed

approximately 6000 pounds and measured 107"L,53"W,12"T, was lifted and moved 1

with a fork lift. The trench cover was lifted to a height that was approximately 1"

..             above the surrounding floor and then set off to the side of the trench. This heavy load j               lift was made over the Train A Residual Heat Removal (RHR) discharge piping to the           ,

i Safety injection (SI) pump suction and the RWST to charging pump piping. The 4 movement of this heavy load was not over any safe shutdown equipment. i i ! EVENT NARRATIVE -(CHRONOLOGICAL DESCRIPTION) ! First Heavy Load Lift 9/4/96 WO 9608888, D15.2; 10 year RCP Motor inspection, prepared with procedure D15.2, Reactor Coolant Pump Motor Cleaning Procedure. 12/19196 D58, Rev. 25 - Control of Heavy Loads, reviewed by Operations Committee and approved for use. Revision 25 added requirements for moving loads over Spent . Fuel Pool (SFP) enclosure as a result of a review of the heavy loads program per NRC Bulletin 96-02, " Movement of Heavy Loads over Spent Fuel Pool, Over Fuel in the Vessel, . . ." This revision also revised the turbine laydown area for smaller  ! low pressure turbine rotor stands. 12/20/96 Read and sign training exercise on the Rev. 25 changes to D58 sent to the  ; Engineering and Tech Staff (E&TS) by computer. 1R37002. DOC I

4 1 AttichmInt March 26,1997 Page 3 1/21/97 ] ' Maintenance riggers and repairman received training on Rev. 25 changes to D58.

This training did not include the entire procedure, only the Rev. 25 revisions made j for moving loads over the SFP enclosure. Traveling maintenance personnel (travelers) assigned to P1 for the upcoming outage were also included in this
)

training session. 112719 7  ; WO 9608888,' D15.2; 10 Year RCP Motor inspection, isolated per D15.2 and given I Shift Supervisor (SS) Approval to Start Work (ASW). Maintenance personnel started work on 22 RCP motor per D15.2. Work on 22 RCP progressed over the next week until the section of the procedure for removing the upper bracket and rotor was reached. 2/3/97 The system engineer contacted the day shift maintenance supervisor and made arrangements to have maintenance personnel remove 22 RCP upper bracket and rotor from the stator and move it to the RCP motor stand. The maintenance supervisor assigned the task to the traveling maintenance supervisor and the lead rigger assigned to containment. Once in containment the system engineer, traveling maintenance supervisor, lead rigger and crane operator briefly discussed what needed to be done and that the control room should be contacted before anything was taken over the refueling pool. Nr discussion about D58 requirements for moving a heavy load in containment was included. The lead rigger contacted the control room and informed a SS that they were , preparing to remove 22 RCP rotor. This would involve moving the polar crane l empty hook over the refueling pool to go pick up the RCP motor lifting fixture.  ! Once this was attached to the hook it would be brought back over the pool and j then lowered into 22 RCP vault. I After the lifting fixture was in the RCP vault, the lead rigger along with the  ! machinists working on 22 RCP, attached the lifting fixture to the lifting lugs on 22 RCP upper bracket. Once this was done the lead rigger inspected the rigging,  ; load bearing componenis; shackles, turnbuckles, lifting fixture cable clamps and j cable. When satisfied that all the lifting equipment and connections were i satisfactory, the load was lifted enough so it could be checked for level. The load had to be set back down, adjusted, and then lifted again to check for level. This  ! had to be repeated several times to ensure that load was level so the rotor would IR97002. DOC

Attachm:nt March 26,1997 Page 4 not make contact with the motor stator as it was being removed. Before making the lift the lead rigger contacted the control room again to inform the Unit 2 SS that they were ready to lift 22 RCP rotor out of the vault and move it over the edge of the pool to the motor stand. During this conversation tiiere appears to have been some misunderstanding between the two individuals on what the load path was going to be. The lead rigger thought the SS gave the OK to move the load across the pool. The SS understood that the load would follow a safe load path near the edge of the pool. Neither individual remembered that a heavy load couldn't be moved within 15 horizontal feet of the irradiated fuel without a specific written procedure. Sometime around 1130,22 RCP motor upper bracket and rotor were lifted from the pump vault and moved to the RCP motor stand. The path taken to the motor stand was as follows (refer to Figure 1): the RCP upper bracket and rotor lifted vertically out of the motor stator and vault untilit was above the CRDM piping on the pool side of the vault, the load was then moved horizontally to approximately a third of the way cut over the refueling pool, the polar crane bridge was then rotated to a position that would allow the trolley to move the load to the stand, the loaa was then moved horizontally across the pool to the RCP motor stand. The RCP motor stand is located on top of the removed pressurizer missile shield sitting on the 755' level of containment near 21 RCP vault. According to the lead rigger l the heavy load was within the 15' area of the core for approximately 2 minutes. l For a part of this 2 minutes the heavy load crossed over a portion of the core. Maintenance electricians complettd inspection, testing and cleaning of 22 RCP rotor per D15.2. I I 2/4/97 22 RCP upper bracket and rotor ready to be moved from the RCP motor stand back to the stator in 22 RCP vault. Maintenance personnel prepare to move the RCP rotor from the stand by attaching the motor lifting fixture to the upper bracket. The lead rigger contacted the control room and informed the Unit 2 SS of the move they were ready to make. During this phone conversation the SS questioned the path the load would be taking and was told it would be over the refueling pool to the pump vault. With fuel handling in progress, going over the refueling pool with a heavy load was a concern to the SS, so he told them to wait until he did some further checking to determine if it was OK. The SS discussed this with Shift Manager (SM) and it was determined from reviewing D58 that the heavy load move could not be made. The lead rigger was told they couldn't make the move without an approved procedure. The lead rigger informed the system IR97002. DOC

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l r , Attichment j- March 26,1997

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! engineer of shift management's decision. The system engineer contacted the SM i to find out what was going on and why the rotor couldn't be moved. When told i that a specific procedure was required to move the rotor across the refueling pool,  !

if the load would be coming within 15 feet of the irradiated fuel, he informed the '

SM that the rotor had been moved across the refueling pool to the motor stand the l day before without an approved procedure. From this discussion and further i review of the D58 requirements for moving a heavy load in containment it was l determined that the rotor had been moved within 15 feet of the irradiated fuel on the previous day (2/3/97) in violation of the D58 requirements. D58 was violated i by not having an approved written procedure and containment isolated. i i The job was placed on hold until further evaluation of the situation could be completed. It later was determined that a specific procedure would have to be written and approved by the Operations Committee (OC) before the RCP upper bracket and rotor could be moved back across the refueling pool to the RCP vault. 21519 7 WO 9700661 was written to lift and move 22 RCP upper bracket and rotor in accordance with the D58 requirements.' The procedure was reviewed and approved by the Operations Committee on 2/5/97. 22 RCP upper bracket and rotor were then moved from the RCP motor stand to the motor stator in accordance with this procedure. 2/7/97 1450 - The determination wa. made that Prairie Island Unit 2 was in a condition outside of the design basis of the plant on 2/3/97 when 22 RCP upper bracket and rotor was moved over the core and the requirements of D58 were not met. 1625 - The plant made a 1 hour Non-Emergency notification to the NRC informing them of the event that took place on 2/3/97 that placed Unit 2 in a condition outside the design basis.- Between First and Second Heavy Load Lifts The first event was self-identified and short term corrective I ctions were taken immediately to prevent a similar event from recurring before the long term corrective actions could be implemented. One of the short term corrective actions taken was to communicate to all site personnel about heavy loads to heighten their awareness of the requirements of D58, Control of Heavy Loads. This increased awareness to the movement of heavy loads prompted some personnel to question the heavy load moves they had observed. From this increased awareness the second and third heavy load events were questioned and D58 IR97002. DOC

Attichment March 26.1997 i' . Page 6 i, reviewed to determine if the requirements were followed. For these heavy load

' moves it was discovered that D58 doesn't specifically address moving a heavy i load near safe shutdown equipment or over available equipment using a mobile l crane or fork lift..

i l From the first event investigation it was determined that D58 was difficult to use

and would need to be revised. To help maintenance personnel and other site personnel ensure that the requirements of D58 were being applied before moving

, a heavy load with any of the plants installed cranes, a checklist was developed to 1 ensure that D58 requirements were applied. This checklist did not include mobile cranes because D58 did not include the use of mobile cranes. i 2/19/97 i The cleaning and inspection of 22 CW pump motor under WO 9700434 was i' completed and the motor was ready to be reinstalled. Also,21 CW pump was

prepared to be removed after setting 22 CW pump motor because of the extra precautions and requirements that needed to be satisfied to set up the mobile
crane in this area. The system engineer reviewed D58 and found that the
procedure did not contain specific requirements pertaining to the use.of a mobile i crane for moving a heavy load. From this review it was concluded that the i requirements in D58 didn't apply to the use of a mobile crane and did not specify a

. safe load path requirement for heavy loads in the area of the Plant Screenhouse,

so no specific procedure was prepared to cover the movement of 22 CW pump motor or the removal of.21 CW pump. The WOs did address the use of a mobile i.. crane to lift the heavy load and identified the weight of the loads, but the WOs did i not identify a safe load path. The precautions pertaining to nearby electrical equipment and the load path to follow for avoiding safe shutdown equipment in the Screenhouse were verbally addressed at the pre-job briefing.

[ Back on 1'/28/97, when 21 & 22 CW pump motors were removed under WOs 9700434 & 9614599, the system engineer took the same precautions concerning the use of the mobile crane and made sure that the mobile crane operator and riggers understood the load path to be followed. This information was presented to the personnel involved with the load handling operations at the pre-job briefing held prior to the start of the job. Around OM, the system engineer held a pre-job briefing with the riggers, mobile crane operator, maintenance supervisor and other personnel who would be seinstalling 22 CW pump motor and then removing 21 CW pump. The briefing included a' discussion on where the mobile crane should be set up, where the flat bed truck carrying the pump motor should be parked, the load path for moving the motor from the trailer into the Screenhouse. The location of the mobile crane and IR97002. DOC l l 1

  • AttSchment March 26,1997
      .                                                                    Page 7 flat bed truck were established to prevent accidental contact with nearby electrical equipment. The load path described was to stay clear of the center area of the Screenhouse roof which is over the diesel cooling water pumps and to stay clear of the Unit 2 electrical transformers and high voltage lines.

Tne rigging equipment was inspected and attached to the CW pump motor following standard NSP rigging requirements and practices, which meet ANSI and OSHA standards. The CW pump was lifted from the flat bed trailer and moved into the Screenhouse through an opening in the Screenhouse roof (refer to Figure 2). The pump was lowered to the lower level and set in place. After 22 CW pump motor was set in place,21 CW pump was rigged and removed through the Screenhouse roof opening and placed on the flat bed trailer. The NRC Resident inspector observed the lift of 22 CW Pump motor and the removal of 21 CW pump and had a concern with the potentialimpact on safe shutdown equipment in the Screenhouse because of the load paths close proximity to the area of the Screenhouse roof over the safe shutdown equipment. The NRC Resident inspectors determined that D58 was not adequate in that it did not contain the necessary administrative controls for handling heavy loads over or near safe shutdown equipment when using a mobile crane. 2/21/97 Before reinstalling 21 CW pump a specific procedure, WO 9614600 Attachment 1, was prepared and approved by the Operations Committee to lift and move the Unit 2 Screenhouse hatch cover and to lift and move 21 CW pump from the turbine building to the Screenhouse. This procedure defined special considerations and defined a safe load path which avoided identified safe shutdown equipment and the Unit 2 transformers. Third Heavy Load Lift 2/25/97 System engineer requested maintenance to remove one of the concrete trench covers from the Unit 2 Auxiliary Building trench for ISI of pipes in the trench per WO 9614795. Using a fork lift, eye bolts, shackles and lifting beam maintenance personnel attached these to the trench cover. The equipment was inspected per NSP rigging requirements. The trench cover was then lifted and moved back and set on the edge of the trench opening (refer to Figure 3). IR97002. DOC l

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l . Attichment

March 26.1997 i . Page 8 Later a QC inspector arrived to witness the inspection of the RWST to charging i pump piping. When in the area of the trench, he noticed the concrete trench l l cover, that had been removed earlier, sitting along side the trench. Because of its i apparent size and weight and the increased awareness on site concerning the  !

movement of heavy loads, the inspector questioned if the removal of this trench i

cover fell under the requirements of D58 because of its weight and the RHR piping i located in the trench. This concern was passed on to another QC inspector who )

determined that the weight of the cover met the definition of a heavy load (>1799 1 pounds), but the guidance in D58 did not specifically address the lifting and l movement of the trench cover. Before moving the cover back the conservative l approach was taken and a specific procedure prepared and approved for I replacing the cover. 1 Inspection of the piping in the trench was completed. 2/28/97 WO 9701169, Replace SI/RHR Trench Cover, was prepared and approved by the Operations Committee for replacing the trench cover. The WO applied the requirements of D58 Appendix B and section 5.7 for moving a heavy load over equipment that is required to be operable. 3/3/97 The Unit 2 Auxiliary Building trench cover was replaced per the instructions of WO 9701169. Reason for the Violation

SUMMARY

OF FACTORS THAT INFLUENCED HUMAN PERFORMANCE (First heavyloadlift)

        ' Inappropriate Action I: Failure to follow D58, Controlof Heavy Loads, while moving 22 RCP rotor.

Habit intrusion - removal of 22 RCP rotor was performed based on similarities to past heavy load lifts with the reactor vessel head in place. Mindset/oreconceived idea - the lead rigger felt that by informing the SS of the heavy load move he would be kept from making a heavy load move that wasn't allowed. Wrona assumptions made - the lead rigger assumed that a heavy load could be l moved anywhere in containment with permission from the SS. I j nmn.we I

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Attichment ! March 26,1997 1 } . . Page 9 i

l. Insufficient degree of attention anolled - before making the heavy load move, the
system engineer, traveling maintenance supervisor, lead rigger and crane operator I did not adequately apply D58 as instructed by the steps in D15.2.

l l Lack of specific knowledge - the system engineer in charge of the RCP work was I l not familiar with the D58 requirements for moving a heavy load in containment. The

lead rigger and SS contacted were not aware of some of the specific D58  !

l requirements that should be applied when the reactor head is off (e.g. heavy load I i can't come within 15 feet of irradiated fuel). The traveling maintenance supervisor i i and crane operator knowledge of D58 was limited to the pre-outage training l j . received on the revisions made to D58 for SFP heavy loads, i i Not familiar with task - the lead rigger was experienced in lifting heavy loads, but had not lifted 22 RCP rotor at a time when the reactor head was removed and the pool flooded. Note: In Unit 2 containment only 22 RCP rotor has to be transported across the refueling pool to get to the motor stand. The crane operator had not moved any heavy loads in containment before this outage.

SUMMARY

OF CAUSES (First heavyloadlift)

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Ilnappropriate ' Action lU Failure to follow D58, .Control of Heavy Loads,- while movingF

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22 RCP mtor. ' Primary Cause(s): Work Practices - D15.2 procedure was not followed. D15.2 references that the heavy Icad be moved in accordance with DSB instructions and guidelines. D58 was not adequately applied before making the move to ensure that all the requirements were met (e.g., approved written procedure and containment isolated).~ The use of D58 for handling heavy loads ensures that load handling operations meet the safe load path requirements described in the plant's Design Bases Document for Heavy Loads. Work Organintion/ Planning -job scoping by the system engineer and the maintenance personnel did not identify the need for a specific written procedure and containment isolation to perform the heavy load lift. Training /Oualification - a check of the training records could not determine if D58 refresher training had been provided over the years. Task analysis did not identify that requalification training was necessary for D58 and it appears that training was not coordinated over the years with the changes that were made to D58. Personnel invcived with the initial raove of 22 RCP rotor did not have an adequate

                                . understanding of D58 to know that additional requirements and precautions had to IR97002. DOC

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          -                                                                      Page 10 be taken before moving heavy loads in containment with the reactor vessel head removed. It should be noted that adequate training was provided before the Unit 2 outage to address the most recent changes made to D58 for the control of heavy loads over the SFP enclosure.

Secondary Cause(s): , Verbal Communication - During the phone conversation with the control room l some pertinent information was not transmitted between sender and receiver  ! because oflimited knowledge of certain D58 requirements.  ! l Second and third heavyloadlifts  ;

SUMMARY

OF CAUSES (apparent) l lnappropriate Action (apparent): _D58, Control of Heavy Loads, did not contain l adequate information to provide guidance formoving heavy

                                                                                                                    \

loads with the use of mobile cranes orforklifts..

            ' Primary Cause(s):

Change Management - The previous interpretation of NUREG-0612, " Control of Heavy Loads" and other original documents associated with the control of heavy j loads did not identify mobile cranes or fork lifts as being in scope. J l Corrective Steos Taken and Results Achieved Immediate corrective actions

1. Movement of 22 RCP upper bracket and rotor back to the stator placed on hold until a specific procedure could be written and approved by the OC. completed 2/427
2. Work order 9700661, " Lift 22 RCP Upper Bracket and Rotor," written and approved to cover the move of 22 RCP upper bracket and rotorin accordance with reactor building safe load path requirements per D58. completed 2/5/97
3. General Superintendent of Maintenance issued a Training Request for training to ,

review D58, " Control of Heavy Loads", safe load paths in the reactor buikiing with l Pl and traveling maintenance riggers and repairman. Course number Fi]5L-105 rev. O training performed on 2/5N7 & 2/6/97. 1 1

4. Communications made to Engineering, Maintenance and Operations personnel to increase their awareness of the recent events involving the movement of heavy loads and of the requirements of D58, Control of Heavy Loads and management's expectations to follow procedures.. Engineering informed 2/8/97, Maintenance informed 2/5/97 & 2/6/97, Operations informed 2/7/97.

IR97002. DOC

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l t AttichmInt i March 26,1997

. . . Page 11 l
- i i 5. General Superintendent of Maintenance developed and issued a checklist to help Riggers. System Engineers and Maintenance Supervisors determine if D58 i requirements should be applied prior to a heavy load lift. completed 2/12/97
                                                                                                                                   )
6. WO 9614600 attachment 1, for lifting and moving 21 CW Pump, prepared and  ;

approved by the OC. completed 2/21/97  :

           - 7.       The General Superintendent of Plant Maintenance, Supt. Mechanical Systems,                                 i General Superintendent of Engineering, and system engineers are assisting with                             j heavy load reviews for the interim until corrective actions #16 & 17 are                                   :

nmplemented. completed 2/26/97 i .i

8. All outstanding outage work orders reviewed to identi*y any work that would ,

2 require a heavy load lift and require the preparation and approval of a specific  ;

procedure to cover the movement of the heavy load completed 2/26/97 i
i. 9. MSIP 6003, Control of Heavy Loads, written and issued. completed 2/27/97  ;
10. WO 9701169, " Replace Sl/RHR Trench Cover", for moving the trench cover j prepared and approved by the OC completed 2/28S7  ;
11. Conduct "just in time training" on MSIP 6003, Control of Heavy Loads for '

i maintenance personnel. completed on 2/28/97 i

;             12. Conduct "just in time" training on MSIP 6003, Control of Heavy Loads for                                       )
!                     construction personnel and other personnel who may have been missed.                                       )
                    - completed 3/3/97                                                                                           l J
            - 13. Plant Manager held a meeting with the General Superintendent of Engineering,                                     '

General Superintendent of Plant Maintenance, Issues Training Manager, Error Reduction Task Force representative, Licensing and Management issues engineer, and design standards engineer on 3/5/97, to discuss the heavy load events of the outage and issues related to the control of heavy loads. completed 3/5/97

14. D58, Control of Heavy Loads, revised and revision 27 issued. completed 3/6/97
15. Perform heavy loads familiarization training for Engineering Support personnel, site Quality Services personnel, Nuclear Generation Services personnel, and Operations personnel. completed 3/17/97 IR97002, DOC I

i . l 4.

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. l ~ Attechment I March 26.1997

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j Corrective Steos That Will Be Taken To Avoid Further Violations: i I

1. Perform a comprehensive review of the original source documents including  ;

NUREG-0612, Control of Heavy Loads, Phase I and ll Technical / Safety j Evaluation Reports, related NSP-NRC correspondence, and Bulletin 96-02.

j. documentation to determine the scope of the heavy loads program, including ,

j mobile cranes. Review DBD TOP-08 and related DBD, USAR, and D sections. l l Determine if they adequately describe the scope of the program. Update license- ! related documentation accordingly. In addition, revise, as appropriate, D58, Control of Heavy Loads, related D ssctions,5AWI 8.6.0, Material Handling and

;               Control of Heavy Loads, MSIP 6003, Control of Heavy Loads, to ensure these               i i                procedures are properly coordinated and that they implement the requirements               l for the control of heavy loads. Human engineering factors will be considered in such changes to reduce the likelihood of similar events in the future.
2. Assign a heavy loads program owner to be the focal p '+ of the heavy loads program and the site expert for people to contact when questions arise on the control of heavy loads.

I

3. Conduct a job task analysis of the heavy loads program. Ensure this analysis  !

includes and adaresses the bullet items listed below.

  • Analyze the site organization (include travelers) and determine who needs D58 knowledge and skills training and how often. Conduct training for these groups / individuals on the Control of Heavy Loads.
                 . Add a heavy loads sign-off requirement on the " Prairie Island /Monticello Overhead Crane Operator Qualification" form.
                 . Establish a method that provides D58 initial and refresher training as determined by the analysis. Ensure the appropriate traveling maintenance personnel coming to PI for the outage are included in this refresher training.
                 . Ensure that initial training is provided for maintenance personnel who              l transfer to PI from other NSP plants.                                               !
4. The maintenance, operations, and engineering training PACS will review D l Sections _in order to identify procedures that require job and task analyses. l' Identified D Sections will have job and task analyses performed.
5. Outage planning group will develop a method that will consider / identify the  ;

movement of heavy loads in future outage planning and schedules. ' We will 1 consider tying this to the Shutdown Safety Assessment checklist. IR97002. DOC

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                 .                                                                                                                                      Attachment March 26,1997 l                               *             .                                                                                                          Page 13 3                                                                                                                                                                                                4 i'

The Date When Full Comoliance Will be Achicyst  ; 1 Full compliance has been achieved. 1 i I' .+ e t f r 9 i i i

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l 1 IR97002. DOC

j,. Attichment j March 26,1997 1 . Page 14 Figure 1 Unit 2 Containment

                                ,                                                              I 4                       s
-- g ,

1 90" 20* l g I foo

                                                                                                               -22 RCP
  • Vault I

h Przr Vault 2 i

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