ML20136C362
| ML20136C362 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 06/22/1979 |
| From: | Hariston W ALABAMA POWER CO. |
| To: | |
| References | |
| FNP-79-0762, FNP-79-762, NUDOCS 7909190492 | |
| Download: ML20136C362 (1) | |
Text
NRC.
- 366 U.S. NUCLEAR REGULATERY COMMISSION
'4 itCENSEE EVENT REPORT GDNTROL BLOCK: l l
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lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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8 60 61 DOCKET NU*ABER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l Westinghouse notified Alabama Power Company that a high energy lino b ra nte inefan l
10 ; J l l Containment could result in heatup of the steam nenerator level traneitter referanea l LO_f 41 I legs.
A resulting error in steam Renerator level indication in th e nnn-cnnnorvnr4va l ITITl l direction could occur that could affect reactor trip and auxiliary feedwater I
I 10 le i l initiation signals. Review of this notification resul ted in n dorarninneinn nn l0l7l l 6/22/79 that this condition is potentially reportable under Tech. Snac. 6.4.1_R(hi.
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101811 The health and safety of the oubli c vere nn e a f fec ted.
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10 Il 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LE R 'RO EVENT YE AR REPORT NO.
CODE TYPE N O.
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33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lilol l Increased reference leg water column temp. will result in a decrease of the water I
I1 Iii l column density with a consequent apparent increase in the indicated S.C. un ear l ovn1 1 Ii l2I l (i.e. apparent level exceeding actual level). This matter is under investigation.
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53 l3l l A supplemental IIE will be issued upon completion of the investigation.
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7 8 9 10 NAME OF PREPARER PHONE: