ML20135C745
| ML20135C745 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 06/30/1985 |
| From: | Woodard J ALABAMA POWER CO. |
| To: | |
| Shared Package | |
| ML20133G947 | List: |
| References | |
| NUDOCS 8509110516 | |
| Download: ML20135C745 (8) | |
Text
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te JOSEPH M. FARLEY NUCLEAR PLANT UNIT 1
' NARRATIVE
SUMMARY
OF OPERATIONS JUNE, 1985 i
During the month of June, there were two (2) automatic' shutdowns which occurred on 6-8-85 and 6-23-85.
The following major safety-related maintenance was performed in'the
. month of June:
1.
Miscellaneous corrective and preventive maintenance was 4
performed on the diesel' generators.
d 2.
Replacement of containment tendon field anchors is complete.
-3.
Two control rod drive system cables were repaired. An electrical short had occurred in the containment electrical penetration causing the reactor trip on 6-23-85.
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3 8509110516 850715 i
PDR ADOCM 05000348 R
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OPERATING DATA REPORT 1
DOCKET NO. 50-348 i
DATE Julv 3 1985 t
COMPLETED BY
- 3. D. Woodard TELEPHONE (205) 899-5156 OPERATING STATUS Notes
- 1. Unit Name:
Joseph M. Far1ev - Unit 1 June, 1985
- 1) Cumulative data since j
- 2. Reportug Penod:
2652 12-1-77, date of commercial
- 3. t *W Thermal Power (MWt):
860 operation.
- 4. Namepiste Ratmg (Gross MWe):
829
- 5. Demen Electncal Rating (Net MWe):
860.9
- 6. Maximum Dependable Capacity (Gross MWe):
816.5
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
N/A I
N/A
- 9. Power Level To Which Restncted.lf Any (Net MWe):
N/A
- 10. Reasons For Restrictions. If Any:
1 f O This Month Yr.-to.Date Cumulative 720 4,343 66,455
- 11. Hours la Reportag Period 4
- 12. Number Of Hours Reactor Was Critical 691.7 3,098.6 45,227.6
- 13. Reactor Reserve Shutdown Hours 0.0 o,o 3,650.0
- 14. Hours Generator On-Line 670,7 2,986.6 44,011.0
- 15. Unit Reserve Shutdown Hours nn 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1.655.189 7,533,878 111,434,453
- 17. Gross Electncal Energy Generated (MWH) 540.662 2,435,952 35,530,266
- 18. Net Electncal Energy Generated (MWH) 508,014 2,288,746 33,417,792 93.2 68.g 66.2
- 19. Unit Service Factor 93.2 1
- 20. Unit Availability Factor 68.8 66.2 86.4 64.5 63.0
- 21. Unit Capacity Factor (Using MDC Net) 85.I 6,_6 60.7
- 22. Unit Capacity Factor (Using DER Net)
- 23. Unit Forced Outage Rate 6.8 3.7 12.6
'4. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each t:
1 N/A
- 25. If Shur Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status iPrior to Commercial Operation):
Forecast Achieved 08-06-77 08-09-77 INITIAL CRITICALITY INITIAL ELECTRICITY 08-20-77 08-18-77 COMMERCIAL OPERATION 12-01-77 12-01-77
]
DOCKET NO.
50-348 1
UNIT DATE July 3, 1985 COMPLETED BY
.T.D. Woodard (205) 899-5156 TELEPHONr.
b June, 1985 310NTI!
4 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL QlWe-Net)
OlWe-Net) 017 546 g,
g7 821 2
629 13
~~
~
~~705 --
821 3
..__..__g9_.
4 4
- A 813 825 3
21 f
816 823 6
,n 498 7
792 23 l
0 37.5 g
34 l
357 ~
473 9
3 10 810 26 818 Al?
27 4
812
[2 3
815 l
13 819 3
R??
822 14 30 812 15 3g 1
l 16 812 I
1 1
!?GUGONS On this form:t. list the aversge dssly unit power !cvet in MWe-Net for each d:y in the reporting month. Compute to j
, the neare:t whole me;swatt.
(9(77)
.i O 4
-._,.,n.
. -,,, _,. - - - - - ~,,,..,..,,,, _,. -, - -
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UNIT SilUTDOWNS AND POWER REDtXmONS DOCKET NO.
50-348 UNIT NAME J. M. Fdrley - Unit 1 DATE Juiv 1.
1985 COMPLETED gay
.T. n. Woodard REPORT MONTil Tne-19R5 TELEPliONE (705) R99-5156 r,
b.
.$ E Ej Liccusee E v,
- L Cause & Cossective 3gx Event u?
3 Acehm to No.
Date -
(
gg dEU u
o6 s2 jgg Repost #
Pstvent Hecunscuce 6
6 004 850600 F
25.2 G
3 85-010-00 AB BU A reactor' trip occurred due to under-frequency on the reactor coolant pump (RCP) buses. The underfrequency condition occurred because the RCP bus power sources had not been realigned to the startup transformers prior to trip-ping the main turbine.
This event was caused by personnel error and procedural inadequacy. The individuals involved i
have been counseled.
The appropriate procedures have been changed to prevent recurrence.
005 850623 F
24.1 A
3 85-012-00 AA CBL4 A reactor trip occurred due to an elec-trical short between two control rod drive system ca,bles which were routed through the same containment electrical penetration. The cables have been re-paired and re-routed.
i 2
3 4
F: Forced Reason:
Method:
Exhibia G - Insisuctions S: Siheduled A-Equipment Failure (Emplain) 1 Manual for Prepasation of Data B. Maintenance of Test 2 Manual Scram.
Entry Sheets for I.icensee C-Refucimg 3 Autouweic Scram.
Event Repm (LER)FileINUREG-i D-Regulasiuy Resisicsion 4 Oslics (Emplaio) 0161)
E-Operator Tsaining a license Examination F Adninistrative 5
G Opesational Estos (Emplain)
Exhibis ! Same Sousec (9/77) ll Othes (E xplain)
- /~
JOSEPH M. FARLEY NUCI. EAR PLANT UNIT.2 NARRATIVE
SUMMARY
OF' OPERATIONS
' JUNE, 1985 There were no unit shutdowns or significant power reductions during the month of June.
The following major safety-related maintenance was performed in the month of June:
1.
Miscellaneous corrective and preventive maintenance was performed on the diesel generators.
t
m 4
i OPERATING DATA REPORT
)
i DOCKET NO. 50-364 DATE July J.
1985 J
J.
D. Woodard COMPLETED BY TELEPHONE 205-399-5156 OPERATING STATUS l
seph M. Farley - Unit 2 Notes
- l. Unit Name:.
l
- 2. Reporting Penod.
3-1985
- 1) Cumulative data since
- 3. t ** Thennal Power (MWt):
2652 7-30-81, date of commercial 860 operation.
- 4. Namepiste Rasmg (Gross MWe):
829
- 5. Demon Electncal Rating (Net MWe):
850.2
- 6. Maximma th,
"': Capacity (Gross MWe):
807.2 l
- 7. Maximum I', "': Capacity (Net MWe):
q
- 8. If Changes Occur in Capacity Ratags (Items Number 3 Through 7) Since Last Report, Give Reasons:
N/A
- 9. Power Level To Whach Restncted. lf Any (Net MWe):
- 10. Reasons For Restrictions. If Any:
N/A i
This Month Yr.-to Date Cumulative
~
720 4,343 34,368 i1. Hours In Reportag Period y'
- 12. Number Of Hours Reactor Was Critical 7?n n 2,563.8 29,482.3 0.0
- 13. Reactor Reserve Shutdown Hours nn 1u n 720.0
- 14. Hours Generator On-Line
? s19 n 29.097.1 0.0
- 15. Unit Reserve Shutdown Hours 0.0 0.0 4
- 16. Gross Thermal Energy Generated (MWH) 1 R65 7?s 6,260,885 73,113,633
- 17. Gross Electncal Energy Generated (MWH) 618.858 2,078,366 24.024,648 i
- 18. Net Electncal Energy Generated (MWH) 589,612 1,952,084 ZZ,//1,006
- 19. Unit Service Factor 100.0 58.0 84,7
- 20. Unit Avadability Factor 100.0 58.0 84.7 a
101.5 ss.7 81.3 i
- 21. Unit Capacity Factor (Using MDC Net) 98 8 54.2 79.9-
- 22. Unit Capacity Factor (Using DER Net) j
- 23. Unic Forced Outage Rate 00 1.1 5.1 l
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each):
y N{A f
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
I
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALJTY 05-06-81 05-08-81 05-24-81 05-25-81 INITIAL ELECTRICITY 08-01-81 07-30-81 COMMERCIAL OPERATION (9/77)
.. ~....
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DOCKET NO.
50-164 UNIT DATE July 3, 1985 J. D. Woodard COMPLETED BY
)
(205) 899-5156 TM ** HONE f
June, 1985 St0NTl!
DAY AVERACE DAILY FOWER LEVEL DAY AVERACE DAILY POWER LEVEL OlWe-Ner)
(31We-Net) 811 17 817 t,
809 818 3g
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.._..____..___...g9--
822 4
818 20 827 825 3
gi9 21 816 821 6
, 22 820 820 819 816 g
S14 9
3 819 817 10 815 3
818 817 gg 27 820
[2 j
gi9 819 33 828 g
o 07 822 14 30 827 IS 3g 16 819
(?GUCTION5 J
On this formst. list the aversge daily umt power levelin MWe Net for esch d:y in the reporting month. Compute to
, the neare:t whole me;swatt.
i (9f77)
! O I
i 3
n o
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UNIT SiluTDOWNS AND POWER RElHK'HONS DOCKET NO.
50-164 UNIT NAME J.M. Farley - Unit 2 DATE July 3, 1985 REPORT MON fil June, 1985 COMPLETED NY J.D. Woodard TELEPilONE (205) 899-5156 v.
E Licensee Ev, j*l, w
jg
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}N'}
Cause & Cosreceive No.
Danc g
gg
,sx Event g'il AI'"' '"
MU EU b
o3 3$F Repust #
uo Pigvent l(ccutscuce a
2d THERE WERE NO UNIT SHUTDC WS OR Sl GNIFICANT P0i'ER R : DUCTIONS DURING THE MONTH OF JUNE.
4 i
i 1
3 4
F: Forced Reason:
Method:
Exhibis G Instructions S. Stliedided A-Eiguipinens Failure (Explain)
- 4. Manual for Psepasailun of D4:a 11 Maintenance of Test
- 2. Manual Scraan.
Entry $licens for Licensee C Refuelung 3 Automatic Scrans.
Event Repint (l ER) File INUREG-D Regulatiuy Resniction 4-Other (Explain) 0161)
E-Operator Tsaining A license Examination F Administrative 5
G Openati. mal Lesus (Explain)
Exhibis I Same Source (9/77)
It Othes (Explain)
-