ML20133P241

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Insp Rept 50-482/85-22 on 850423-25.No Violations or Deviations Noted.Major Areas Inspected:Followup on Allegations
ML20133P241
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/22/1985
From: Ellershaw L, Madsen G, Martin L
NRC - WOLF CREEK TASK FORCE, NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20133P232 List:
References
50-482-85-22, NUDOCS 8508140228
Download: ML20133P241 (10)


See also: IR 05000482/1985022

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APPENDIX

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC Inspection Report:

STN 50-482/85-22

Construction Permit:

CPPR-147

Docket:

50-482

, Category:

81

Licensee:

Kansas Gas and Electric Company (KG&E)

P. O. Box 208

Wichita, Kansas

67201

Facility Name: Wo1f Creek Generating Station

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Inspection At: Wolf Creek Site, Coffey County, Burlington, Kansas

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Inspection Conducted: April 23-25, 1985

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Inspectors:

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L."E. Ellershaw, Reactor Inspector

Date

Project Section A, Reactor Project Branch 2

h W&

j-/8-SS

G. L. Madsen, Reactor Inspector

Date

Project Section A, Reactor Project Branch 2

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Approved:

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m

L.~ET Martin,

ief, Wolf Creek Task Force

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Inspection Summary

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Inspection Conducted April 23-25, 1985 (Report STN 50-482/85-22)

Areas Inspected:

Routine, announced inspection of the followup on

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allegations. The inspection involved 50 inspector-hours onsite by two NRC

inspectors.

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Results: Within the areas inspected, no violations or deviations were

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identified.

8508140228 850802

PDR

ADOCK 05000482

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DETAILS

1.

Persons Contacted

Kansas Gas and Electric Company (KG&E)

W. J. Rudolph II, Manager, Quality Assurance (QA)

R. M. Grant, Director, QA

C. A. Snyder, Manager, Quality First

H. Curry, Supervisor, Quality Control Inspections

D. Madsen, Quality Control Engineer

Thc NRC inspectors also interviewed other site personnel during the

course of the inspection.

2.

Followup on Allegations

a.

(Closed) Allegation 4-84-A-019:

The alleger indicated several items

of concern principally relating to structural construction.

Findings relating to these items follows:

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(1) The alleger indicated that material traceability of structural

steel shims was not verified during installation"and shim plate

sizes may be questionable.

Material traceability (in terms of heat numbers) is not

generally considered important since shims are always com-

pressively loaded.

Any traceability required would relate to

providing a degree of assurance that shims are of a weldable

material, since shims are usually welded to assure they will

remain in place.

The resolution of the structural _ welding

issue has provided adequate-assurance that shims are' weldable

and therefore no further action is warranted.

Shim material

was a subject included in CAR (Corrective Action Report) 46

which was reviewed by the NRC.

This allegation was considered substantiated, however, there

is no safety significance.

The licensee's corrective actions

to resolve this issue were satisfactory.

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(2) It was alleged that structural steel inspections were not

accomplished because of a breakdown in assignment of

responsibilities, and QC supervision attempted to cover-up the

situation by coloring in control status drawings to show that

work had been done.

The above information precipitated an extensive NRC inspection

which subsequently substantiated that the inspection program

for safety-related structural steel welds was not adequately

executed to assure conformance to the requirements, nor were

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adequate records kept to document the quality of the welds.

The attempted cover-up was investigated by the Office of

Investigations and will be documented in a subsequent inspection

report.

As a result, the NRC issued a-Notice of Violation and an

Imposition of Civil Penalty.

KG&E's corrective action included a 100% reinspection of all

accessible safety-related structural steel welds. All of the

actions required to be taken by KG&E in order to provide

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adequate resolution to the structural steel welding issue, were

performed and are documented in their Final Report Corrective

Action Request No. 19, dated January 21, 1985.

The NRC

performed verification of KG&E corrective actions and

documented this activity in NRC Inspection Reports 50-482/85-12

and 50-482/85-13.

This allegation was substantiated, however, appropriate

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corrective action was taken.

This item is considered closed.

(3) It was alleged that KG&E's surveillance report S-372 did not

adequately address the failure to inspect and/or document the

results of structural steel inspections.

Surveillance report S-372 was a precursor to Daniel

International Company's (DIC) Corrective Action Reports (CAR)

29 and 31, and subsequently to KG&E's CAR 19.

The major

findings identified in the surveillance report dealt with

electrical support weld inspection documentation. The resolution

of the structural' steel welding problems has satisfied the

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technical elements of this item.

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This item is considered closed.

(4)- It was alleged that pipe whip restraints were inspected / signed

off in a manner'similar to structural steel.

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CAR-19 was written primarily to address weld deficiencies and

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missing inspection documentation relative to the structural

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steel welding program. To assure that problems similar to

those identified in structural steel did not exist in other

safety-related programs using AWS D1.1 welding, CAR-19 was

expanded to require an analysis of those programs, including

. pipe whip restraints.

This effort revealed no similar con-

ditions or causes generic to the pipe whip restraint program.

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Programmatic elements utilized in the inspection and

documentation of the various applications of AWS D1.1 welding

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differed depending upon the Quality discipline responsible for

inspection activities.

Nondestructive examination (NDE) was

identified as a differing element of the pipe whip restraint

program.

It was determined that pipe whip restraint welds were

100% nondestructively examined and accepted.

There were no

identified instances of missing NDE reports.

This item is considered closed.

(5) The alleger indicated that inspection of structural steel

bolting was neglected in the radwaste and turbine buildings.

Originally these buildings were a part of CAR 26; however, both

buildings were subsequently deleted from the scope of CAR 26.

A review of records revealed that the radwaste and turbine

buildings were deleted from the scope of CAR-26 in that the

purpose of the reinspection program was to determine the status

of high strength bolting connections in safety-related

structures.

The turbine and radwaste buildings (Non Category I

structures) were deleted from the scope of CAR 26 based on DIC

engineering disposition of deficiency report ISD-7844C.

(6) The alleger alludes to the improper torquing of the bolts for

the rail clips on the Polar Crane or the possible falsification

of the inspection records by the day shift inspector who got

sick the one time he did go up on the Polar Crane to inspect

these bolts.

The alleger also said that the second shift QC

inspector worked very hard on inspecting these connections,

while the day shift inspector did nothing.

A review of the time and attendance records and site first aid

records of the individual that allegedly did not perform the

above inspections or possibly falsified the inspection records

confirms that the inspector did get sick while working on the

Polar Crane rail and was subsequently helped down and taken to

first aid on site.

The inspector did not return to the site

for approximately three weeks.

A review of the inspection documentation for the Polar Crane

indicates that this inspector had inspected torquing of the rail

clip bolting on the one day in question.

Structural drawing

E-122 also provides positive indication that the other

inspections were performed by two other inspectors.

A subsequent interview of this inspector, by 01, confirmed that

this inspector had only inspected the torquing of these bolts on

the one occasion.

Structural drawing E-122 and its attachments

also indicates that the bolted connections, after initial

alignment were to be welded, which was accomplished.

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The allusion to improper inspection or possible falsification

of the inspection records for the torquing of the bolts in the

clips for the Polar Crane rail was not substantiated.

(7)

It was alleged that bolting holding down fuel rod storage

containers had no inspection documentation and the prints were

marked up wrong.

Installation of the New Fuel Storage Rack assemblies was con-

trolled and documented on Westinghouse Installation /Fabrica-

tion Traveler SAP-WC-018, revisions 0 and 1.

Pages 4 and 5 of

revision 1 to the traveler document the installation and

inspection of bolting and torquing requirements as evidenced by

the initials of the operator and the Quality Assurance Engineer,

with dates.

The installation of the Spent Fuel Storage Rack assemblies was

controlled and documented on Westinghouse Installation /Fabrica-

tion Traveler G-SAP-WC-030, revision 0.

Pages 10, 11, 14, and

15 of the traveler document the installation and inspection of

~ bolting and torquing requirements as evidenced by the initials

of the operator and Quality Assurance personnel, with dates.

This item is considered closed.

b.

(Closed) Allegation 4-85-A-44:

The alleger stated that there had

been a failure to conduct routine audits of onsite contractors at

the required frequency.

The FSAR for Wolf Creek states that the

management of each SNUPPS' utility is to assess the scope of imple-

mentation and effectiveness of the QA program to assure adequate

compliance with the utilities' policies and with 10 CFR 50,

Appendix B.

This assessment will be conducted every six months

during the first two years that the program is implemented.

Thereafter the evaluation process will be performed on an annual

basis.

This evaluation process may include audits performed by the

utility personnel or outside consultants.

KG&E Quality First received a similar concern from the alleger;

however, the concern was focused on procedures in the KG&E con-

struction procedure manual.

Quality First investigations disclosed

that construction procedures govern activities which are a dupli-

cation of quality related functions which are subject to QA audits or

in the case of Procedure KP-4503, do not control a quality related

function.

Quality First determined that a QA audit of the KG&E

construction procedure manual is not required.

The alleger was

contacted by Quality First on January 18, 1985, at which time he

acknowledged the receipt of a written summary regarding this concern

and he indicated no problem with the findings regarding this item.

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During the period 1977-1985, KG&E corporate and onsite QA conducted

some 190 onsite audits and 1040 surveillances of Wolf Creek con-

struction activities.

In addition to the audits performed by KG&E,

the site constructors performed some 545 audits of their own

activities.

On the basis of the above, the audit and surveillance of onsite

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construction is considered adequate.

c.

(Closed) Allegation 4-85-A-45:

The alleger indicated several items

relating principally to electrical activities.

Findings regarding

these items follows:

(1) The alleger indicated that equipment was moved from the

warehouse to the field without proper handling and installation

procedures.

A review of warehouse maintenance and QC

inspection records revealed damage to Power Supply Inverter

NN13 which had been identified and corrected.

However, Quality

Inspection personnel failed to initiate the appropriate

corrective action documents.

In spite of the oversight, the

Quality Program identified, resolved, and inspected the

deficiency.

In order to substantiate the acceptability of the

equipment, KG&E QC and QA personnel performed a visual

inspection of Inverter NN13 on May 1, 1985.

No evidence of

damage associated with this allegation was found.

(2) The alleger indicated concern about the turnover of the

procurement program to KG&E as .related to the KG&E Vendor

Control and spare parts program.

The alleger indicated a

concern that the KG&E QA group was performing inadequate

reviews of Bechtel and Westinghouse procurement.

The concern relating to vendor program control is believed to

be related to the control of vendor. instructions manuals which

were shipped with the equipment and were taken to the field

without benefit of proper approval or control. This concern

was identified on November 14, 1984.

QC investigations, to

determine if procedural control was in place for transmitting

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vendor generated documents from WCGS Receiving to Document

Control for processing, revealed that QCP 7.1, Revision 1,

failed to provide instructions for transmittal of Vendor

generated documents.

QCP 7.1, Revisi)n 2 was initiated on

December 17, 1984, to correct this condition.

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(3) The alleger is concerned over the use of a ground bar used

for instrument ground where other grounds are terminated.

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Isolated Grounding for Instrumentation is governed by the

following documents:

. P-XI-300, " Installation of Electrical Equipment and

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Instrumentation," Revision 9

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WP-X-301, " Grounding," Revision 3

3.

Bechtel Drawing E-0G8900, " Grounding Notes, Symbols and

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Details," Revision 13

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IEEE Standard 446, "IEEE Recommended Practice for Grounding

of Industrial and Commercial Power Systems"

-The Inspection of Isolated Grounding for Instrumentation is

governed by:

QCP-XI-300, " Inspection of Electrical Equipment,"

Revision 12

The NRC inspector reviewed the above documents and determined

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that they were satisfactory.

The isolated grounding system at WCGS is primarily for the

purpose of providing a noise free insulated isolated grounding

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method for instrumentation through a very low impedance path to

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station ground.

The inspector could not identify within the

above documents any prohibition against other grounds being

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terminated on the same ground bar that is used for instrument

ground.

The technical merits of this concern would only be

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relevant if it could be identified.that a specific non-

instrument ground, in fact, resulted in noise being induced

into the ground circuit of such a magnitude that the low

impedance cable connecting the ground bus to the station ground

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mat was not properly sized.

This would result in a spike being

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induced into the instrument ground.

This spike in and of it

self would be highly attenuated due to parallel paths.

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This allegation lacks specificity sufficient to pursue in

depth, and the grounding practices are typical of those

utilized elsewhere in the power industry.

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(4) It was alleged that cables were generally routed over sharp

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edges at all elevations in the cable spreading rooms,

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The NRC inspector conducted an inspection of the two cable

spreading rooms in the control building in order to assess the

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validity of the allegation.

Forty cable trays in both the

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lower spreading room at elevation 2032' and the upper spreading

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room at elevation 2073' 6" were observed.

There were no

instances identified where either cables were routed over sharp

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edges or that the minimum bend radii had been exceeded. . Where

cables either entered or exited a cable tray from the side, a

cable tray edge guard had been installed.

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This item was not substantiated and is considered closed.

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(5) It was alleged that a cable tray in the reactor building had

not been cleaned before the covers were put in place.

The

cable tray location was described as being at floor level to

the left of the main personnel hatch two or three levels down,

and passing through a wall separating two large tanks.

Reactor building drawings were reviewed to determine the

specific cable tray. involved and location.

A cable tray was

located that passed through a wall separating the accumulator

tanks. The cable tray was identified as IU2A, and located at

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the 2009' elevation of the reactor building.

The NRC inspector

requested that the covers be removed from the four segments of

the cable tray in order to observe the internal cleanliness

condition.

Covers were removed from segments IU 2A-39, -40,

-41, and -42.

With the exception of some dust, there was no

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debris observed.

This item is not substantiated and is considered closed.

(6) The alleger indicated that the inspectors inspecting anchor

bolts had neither the proper training nor procedures.

It was

indicated that a QC inspector had resigned on March 21, 1983,

prior to submitting an NCR relating to this matter.

He

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questioned KG&E's corrective action and whether a CAR was

issued.

He felt that corrective action should include a random

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audit with pull tests and a review of anchor bolt certifi-

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cations.

He. stated that there had been two companies furnishing

anchor bolts (one safety-related and one nonsafety-related).

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questioned whether or not KG&E maintained proper segregation.

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DIC NCR ISN-9711E, dated March 26, 1983, was initiated to

address the issue of " improper training and procedures" to

govern inspection of expansion anchor bolt installation.

This

NCR was voided with the following justification:

It is the

employer's responsibility to qualify the inspectors in each

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discipline for certification.

DIC Quality inspection

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management reviewed the program in question and determined that

the electrical support certiiication program was adequate for

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the required anchor bolt inspection criteria established at the

beginning of the program.

All inspectors were trained and

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tested prior to being certified and performing any inspections.

The approved Architect Engineer disposition of DIC NCR #ISN

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3476C, dated July 30, 1981, provided additional installation and

inspection criteria to governing documents in effect at that

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time.

As specified in the approved disposition of DIC NCR #ISN

9711E ". . . All inspectors participating in the program were

trained and tested to this criteria prior to being certified

and performing any inspections."

A review of DIC Purchasing and Warehouse records revealed that

concrete expansion anchor bolts were purchased as safety and

nonsafety-related.

The primary manufacturer was RAMSET.

Some

safety related bolting was purchased from Robert Isray Co.

These expansion anchors were "Hilti Cinch Anchors." These

expansion anchors were subsequently found to be incompatible

with site installation procedures and were returned for

salvage.

Warehouse storage maintenance practices for segregation of

safety and nonsafety-related bolting material is accomplished

by storing nonsafety-related bolting material in the area

designated as " Tool Room".

This area is located on the south

end of the warehouse.

The safety-related bolting material is

stored in the north end of the warehouse.

All safety-related

expansion anchor bolts are "Trubolt" as manufactured by RAMSET.

Visual inspection of the safety-related storage area would

readily identify nonsafety-related material inadvertently placed

in this area.

In addition, all nonsafety-related expansion

anchor bolts purchased from RAMSET are "Dynabolts".

Though

similar in appearance to the RAMSET "Trubolt," the difference.is

also readily apparent.

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Based on the information noted above, it was determined that no

corrective action is deemed necessary.

(7) The alleger stated that there were splices inside of cabinets

that were not being properly documented.

The cabinets described

appear to be located in the vital instrument power rooms.

The

cabinets were described as being located in a series of small

rooms.

The NRC inspector visually inspected cabinets NN01, NK51, NK51A,

NK41, NK43, NN03, NK03, NK44 and NK54 in the battery equipment

rooms.

Splices were observed on cables IRPK09DA and IRPK0908 in cabinet

NK41 and on cables 4RPK090A and 4RPK0908 in cabinet NK44.

A

review of electrical termination document E-17000A revealed

that pigtail splices were authorized for the subject cables in

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that the conductor wire size was too large to terminate on

equipment terminal blocks or other connection means.

(8) The alleger related concerns reletive to the routing and

termination of electrical cables within cabinets.

He recalled

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blue Honeywell cabinets located halfway into the auxiliary

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building on the main level as good examples.

He indicated that

cables in the cabinets were in thick bundles and were laying

over the troughs.

He stated that some terminations broke on

moving cable during a walkdown inspection and indicated the

details were in the walkdown notes.

He indicated that hairline

cracks in lugs were noted and that terminations in the upper

level of the pool area were the best examples.

The NRC inspector visually inspected Honeywell Cabinets RJ

160A, B, C and D and RJ 159 A, B, C and D in the south and

north penetration rooms on elevation 2026 feet.

The inspection

revealed no evidence of cable laying over troughs or hairline

cracks in lugs.

The inspector noticed the presence of a tag

within cabinet RJ-159A which indicated lug bends greater than 45

degrees on six cables and referenced Work Request 16654-84

dated December 21, 1984.

A review of the allegers walkdown record dated September 26,

1983, included identification of discrepancies similar to the

subject allegations.

Records indicate that a reinspection was

performed on October 24, 1984, and the conditions were found to

be acceptable.

However, upon correction of cable training,

construction lugs were found bent past 45 degrees. WR 16654-84

was issued for six cables within cabinet RJ 159A.

Reinspections

of cabinets revealed eight additional lugs bent beyond 45

degrees.

These additional damaged lugs were added to

WR 16654-84. WR 16654-84 was closed on January 27, 1985.

Inspections of cabinets on the upper levels of the fuel pool

building failed to reveal cracking of termination lugs as

indicated by the alleger.

3.

Exit Interview

The NRC inspectors discussed the scope and findings of the inspection,

with Messrs. R. M. Grant and W. J. Rudolph on April 25, 1985.

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