ML20133B394

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Notice of Violation from Insp on 850716-30.Violation Noted: Diesel Generator a Inoperable Due to Water & Sediment Content in Fuel Tank & Remaining Generator,Low Pressure Core & Containment Cooling Subsystem Not Tested Until 850726
ML20133B394
Person / Time
Site: Pilgrim
Issue date: 09/20/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20133B392 List:
References
50-293-85-21, EA-85-104, NUDOCS 8510030261
Download: ML20133B394 (2)


Text

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i NOTICE OF VIOLATION Boston Edison Company M/C Nuclear Docket No. 50-293 Pilgrim Nuclear Power Station License No. DRP-35

, EA 85-104 On July 16-30, 1985, an NRC special inspection was conducted to review the circumstances associated with two violations of the Technical Specifications, one of which was identified by the licensee and reported to NRC. In each case, abnormal pla'nt conditions were identified by the non-operational staff, but a i Failure and Malfunction Report (F&MR) was not immediately initiated, as re-quired, to ensure prompt review by the operations staff of -the potential safety significance of the malfunctions. As a result, actions required by the Tech-j nical Specifications were not taken, as required. The failure to promptly complete the F&MR in each case constitutes a third violation of NRC require-ments.

In accordance with the NRC " General Statement of Policy and Procedure for En-

! forcement Actions",10 CFR 2, Appendix C (Enforcement Policy), the violations i are set forth below:

A. Technical Specification Limiting Condition for Operation 3.7.C.1 requires,

'in part, that whenever the reactor is critical, secondary containment in-tegrity be maintained. Section 1.N of the Technical Specifications de-fines secondary containment integrity and requires as one of its condi-tions that all automatic ventilation system isolation dampers must be operable or secured in the closed position.

Contrary to the above, for approximately 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> between 3:00 p.m.,

July 15,1985 and 10:00 a.m. , July 16, 1985, secondary containment in-tegrity was not maintained while the reactor was critical in that auto-matic ventilation system isolation damper A0-N-90 in the exhaust venti-lation duct from the refueling floor was identified as open and inoperable at 3:00 p.m. on July 15, 1985, and the damper was not secured in the closed position until 10:00 a.m. on July 16, 1985.

This is a Severity Level IV violation (Supplement I).

B. Technical Specification (T.S.) Surveillance Requirement 4.5.F.1 specifies that when one diesel generator is inoperable, the remaining diesel gen-erator, and all low pressure core cooling and containment cooling systems shall be tested immediately and daily thereafter.

l l Contrary to the above, on July 23, 1985, Diesel Generator A was found to be inoperable because the water and sediment content in the diesel fuel tank T-126A was in excess of the limits in Table 1 of ASTM D975-77, required

^

by T.S. 4.9.A,1.e, and the remaining diesel generator, the low pressure core cooling subsystems, and containment cooling subsystems were not tested until July 26, 1985.

0FFICIAL RECORD COPY CP NOTICE PILGRIM - 0006.0.0 8510030261 85 m 09/20/85 PDR ADOCK 05000293 G PDR

Notice of Violation 2 This is a Severity Level IV Violation (Supplement I).

C. Technical Specification 6.8.A requires, in part, that written procedures be established, implemented and maintained that meet or exceed the re-quirements and recommendations of Section 5.1 and 5.3 of ANSI N18.7 -

1972 and Appendix "A" of NRC Regulatory Guide 1.33.

Station Procedure 1.3.24, Failure and Malfunction Reports, Revision 11~,

dated February 6,1985, written as required by T.S. 6.8.A states that (1) a Failure and Malfunction Report (F&MR) shall be initiated whenever mal-functions identified during surveillance testing of safety related com-ponents could prevent the components from fulfilling their intended func-tions and (2) the objective of the F&MR is to ensure an adequate initial review of events with potential safety significance.

Contrary to the above,

1. At 3:00 p.m. on July 15, 1985, secondary containment ventilation damper A0-N-90 was identified as malfunctioning (would not fully close) during a routine damper surveillance inspection, and an F&MR was not initiated.
2. On July 23, 1985, water and sediment in excess of limits was dis-covered in the T-126A diesel generator fuel oil storage tank during a monthly surveillance test, and a F&MR was not initiated.

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Boston Edison Company is hereby re-quired to submit to this office within thirty days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, in-cluding for each violation, (1) the corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending this response time.

l OFFICIAL RECORD COPY CP NOTICE PILGRIM - 0006.1.0

09/20/85 i

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