ML20129G292

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Monthly Operating Rept for Apr 1985
ML20129G292
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 04/30/1985
From: Orser W, Wildfong L
PORTLAND GENERAL ELECTRIC CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
WSO-337-85, NUDOCS 8507180009
Download: ML20129G292 (6)


Text

_

5 OPERATING DATA REPORT DOCKET NO. sn-14a DATE 9 1 n; COMPLETED BY r

- --- Mildfong TELEPHONE rsnai MR6-3713 Ext. 397 OPERATING STATUS

1. Unit Name: 'Prnj nn Aoril 1985
2. Reporting Period:

3411

3. LicensedThermalPower(MWt):

1216

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe).1130 1122
6. Maximum Dependable Capacity (Gross MWe):

1nnn g _.,,

7. Maximum Dependsble Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) 9M :e Last Report. Give Reasons:

n/a n/a

9. Power Level To Which Restricted,If Any (Net MWe):

n la

10. Reasons For Restrictions.If Any:

9 This Month Yr..to.Date Cumulative 719 9A70 7R 07M

11. Hours in Reporting Period 719.0 7776_9 as an7 g
12. Number Of Hours Reactor Was Critical 0.0 0.0 3.887.4
13. Reactor Reserve Shutdown Hou s 719.0 2719.5 45,055.0
14. Hours Generator 0n.Line 0.0 0.0 3,249.0
15. Unit Reserve Shutdown Hours 2,435,935 9.113.046 143.099.208
16. Gross Thermal Energy Generated (MWH) 770,374 2,914,002 46,469,782
17. Gross Electrical Energy Generated (MWH) 736.896 2.781.444 41 911,974
18. Net Electrical Energy Generated (MWH) 100.0 94.5 59.3
19. Unit Service Factor 100.0 94.5 63.6
20. Unit Availability Factor 94.9 89.5 53_6
21. Unit Capacity Factor (Using MDC Net) l 90.7 85_5 s1 ?

l

22. Unit Capacity Factor (Using DER Net) 0.0 6.I 16.6
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each):

Cycle.7/8 refuelina outaae scheduled for nhutdown on May 2-19R5 and power escalation on July 8, 1985.

n/a

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Prior to Commerciai Operation):

Forecast Achieved i

n/a n/a INITIAL CRITICALITY n/a n/a INITIAL ELECTRICITY COMMERCIAL OPER ATION n/a n/a 8507180009 850430 DR ADOCK 050003 4 (o/77)

{

SURESARY OF OPERATING EXPERIENCE DOCKET NO: 50-344 DATE: 5-1-85 COMPLETED BY:

L.

A. Wildfong TELEPHONE:

503-556-3713 Ext. 397 OPERATION:The plant averaged between 98% and 100% power for the month of April.

Operations was slightly limited due to difficulty in controlling Feedwater Heater levels due to leakage in heaters 2 and 4, and erratic operation of the EHC Control System.

The plant experienced some small (approximately 40 MWe) load perturbations (increases) during the month due to EHC control problems with the load limit potentiometer.

On April 12 at 0116, power was reduced by 10% for turbine valve testing, and held at 90% from 0134 to 0210.

Reactor Power was returned to 100%

at 0230.

On the 15th one steam line high flow bistable came in momentarily.

Dose equivalent iodine was approximately constant at 25%.

MAJOR SAFETY-RELATED MAINTENANCE:

1.

'A' hydrogen recombiner temperature controller inspected.

2.

'B' emergency diesel generator speed switch / governor repaired.

3.

Replaced mechanical seal on

'D' service water booster pump.

4.

Replaced oil seal and bearings on

'B' boric acid transfer pump.

5.

'B' auxiliary feed pump coupling inspected for wear and/or key shift.

6.

'B' train ESF equipment room coolers cleaned and inspected.

7.

Preventive maintenance performed on MOVs:

a.

MO-8700B (RHR suction valve) & MO-8804B (RHR to S1 suction valve),

b.

MO-8807B (SL to RHR cross-connect) & MO-8703 (RHR disch to hot legs 2 & 4).

MISCELLANEOUS MAINTENANCE:

1.

Performed 5 year preventive maintenance on chlorinator evaporators.

2.

Repaired spent fuel pool bridge crane hoist.

3.

Overhauled

'A' screen wash pump.

4.

Performed preventive maintenance on breakers from A2 for Joy Air Compressor and

'C' CCW pump.

5.

Vented

'C' Reactor Coolant Pump seal water flow transmitter.

6.

Continued spent fuel pool reracking.

7.

Repaired stator cooling sample valve.

8.

Continued main steam support structure weather proofing.

9.

Fire proofed structural steel in

'A' EDG Room.

LICENSE CHANGES:

Amendment No. 104 to the Technical Specifications clarifies surveillance testing requirements for the pressurizer power-operated relief valves when used for low temperature overpressure mitigation.

Also included is an amendment to the bases for thermal-hydraulic limits to incorporate

. changes due to the upflow modification to the reactor vessel internals.

Amendment No. 105 incorporates additional Technical Specifications for equipment added for Post-TMI improvements approved by the NRC in NUREG 0737.

The equipment, which has been added in response to NRC Generic Letter 83-37, is as follows:

Noble gas monitors, containment high range radiation monitors, containment water level monitors, and sulfur dioxide detectors to meet Control Room habitability requirements.

SUMMARY

OF' OPERATING EXPERIENCE DOCUMENT NO:

50-344

.Date:

5-1-85 COMPLETED BY:

L. A. Wildfong TELEPHONE:

503-556-3713 Ext. 397 MISCELLANEOUS:

The plant transferred to Pacific Daylight Time at 0200 on April 28.

Operating data reflects losing one hour in advancing the clock.

p.

AVERAGE DAILY UNIT' POWER LEVEL DOCKET NO: 50-144 UNIT: Troian DATE:

5-1-85 COMPLETED BY:

L.

A. Wildfong TELEPHONE:

(503) 556-3713 Ext. 397 MONTH Anril 1985 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 1025 17 1022 2

1020 18 1024 3

1015 19 1024 4

1034 20 1032 5

1032 21 1033 6

1029 22 1022 7

1029 23 1025 8

1027 24 1023 9-1027 25 1023 10 1032 26 1022 11 1029 27 1019 12 1025 28 979 13 1028 29 1022 14 1026 30 1019 1017 31 n/a 15 1019 16 l

t INSTRUCTIONS

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E!EE Portland General Electric Company Trojan Nuclear Plant P.O. Box 439 Rainier, Oregon 97048 (503)556-3713 May 6, 1985 WSO-337-85 Office ~ of Resource Management U.

S.

Nuclear Regulatory Commission Washington, D. C.

20555 Gentlemen:

In.accordance with the Trojan Nuclear Plant Technical Specifications reporting requirements, the monthly report is submitted for April, 1985.

Sincerely, N

b t

W.

. Orser General Manager

,eur WSO/GGB/ LAW st Attachments ci-MOR Distribution

' File 93.2b (Q)

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