Similar Documents at Cook |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
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1: N.R.C. OPERATING DATA REPORT DOCKET NO. 50-316' i DATE 4/2/85 COMPLETED BY CLIMER TELEPHONE 616-465-5901 OPERATING STATUS 1.-Unit Name D. C. Cook' Unit 2 -----------------------
- 2. Reporting Period Mar 1985 inotes .:
- 3. Licensed Thermal Power (MWt) 3411 ! i
- 4. Name Plate Rating (Gross MWe) 1133 : :
- 5. Design Electrical Rating (Net MWe) 1100 6 .. Maximum' Dependable Capacity (GROSS MWe) 1100 i !
- 7. Maximum Dependable Capacity-(Net MWe) 1060 -------- -- --------
- 8. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since Last' Report-Give Reasons __________________________________ ___
9.-Power Level'To Which Restricted. If Any (Net MWe) ___ ._
- 10. Reasons For: Restrictions. If Any: __
This Mo. Yr. to Date Cumm.
- 11. Hours in' Reporting Period 744.0 2160.0 63528.0
- 12. No.-of Hrs. Reactor-Was Critical 744.0 1869.0 44949.0 1 13.-Reactor' Reserve-Shutdown Hours 0.0 0.0 0.0
- 14. Hours Generator on Line' 744.0 1850.5 43849.1
- 15. Unit Reserve Shutdown Hours 0.0- 0.0 0.0
- 16. Gross-Therm. Energy Gen. (MWH) 2461488 6094080 139172141-
- 17. Gross Elect. Energy Gen. (MWH) 815840 2018110 45803540
- 18. . Net. Elect. Energy Gen. (MWH) 787771 1948364 44166098
- 19. Unit Service Factor 100.0 85.7 71.9
- 20. Uni t . Avail abili ty Factor 100.0 85.7 71.9
- 21. Unit Capacity Factor (MDC Net) 99.9 85.1 68.4
- 22. Unit Capacity Factor (DER Net) 96.3 82.0- 66.9 23.' Unit Forced Outage Rate 0.0 11.7 .
~ 12. 6,
- 24.'Shutduans Scheduled over Next-Six Months (Type,Date,and Duration):
_--------= .._ - .--- -----
- 25. If Shut Down At End of Report Period, Estimated Date of Startup:
- 26. Units in Test Status-(Prior to Commercial Operation):
l Forcast Achieved INITIAL CRITICALITY INITIAL. ELECTRICITY
. COMMERCIAL OPERATION i
l e506070037 eso331 /
PDR ADOCK 05000316' R PDR y y, e r-v-+ -+ap--g g y.-y-, 9- y - g y--+ -c- 9-- o..- e. _y.-e-.
y , --w ---i.,ev c----,
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO. 50-316 UNIT TWO DATE 4/2/85 COMPLETED BY CLIMER TELEPHONE 616-465-5901 MONTH Mar 1985 AVERAGE DAILY AVERAGE DAILY DAY POWER LEVEL DAY POWER LEVEL 1 1097 -17 1094 2 1096 18
- 1093 3 1099 19 1080 4 1098 20 1092 5 1085 21 1094 6 1096 22 1093 7 1098 23 1087 8 1098 24 1092
. 9 1090 25 1091 10 1099 26 1080 11 1097 27 1090 12 1086 28 1093 13 1094 29 1093 14 1095 30 471 15 1094 31 668 16 1093 l
i DOCKET NO. 50-316 . .
UNIT SituTI) OWNS AND POWER REDUCIlONS UNIT NAME D.C. Cook Unit 2-
- 1) ATE 4-5-65 8
March, 1985 COMPT ETED BY B.A. Svensson
+
NEPORT MON 11f TEl.EPilONE 616/465-5901 1, -
% .3 Eit:CnSec h9, 4 Canst & CsHsective a oU N.. . Da.e e n , E-ist u MV Ac ..ne ...
Pievent Rcensscnce M
$$ $ M Repent #
6 160 850330, F 0 A 4 N.A. CH VALVEX Reactor power was reduced to 9% to permit isolation of the normal feed-water to No. 4 Steam Generator and to transfer to the auxiliary feed-water supply. This action was re-quired due to a severe packing leak 1
on the No. 4 Steam Generator feed-water regulating valve. The repack-ing was successfully completed and reactor power was returned to 100%
on 850331.
i 1 2 3 4 1: l'aH ced Reason: Methud: Exhibit G . instancliinis S: Sthedulcal A-Equipmer.t I;ailme (Explain) 1 Manual fo Psepasatism ol' Data la Maintenance ni Test 241 annat Scsam. Enisy 3Incess lin IJeensee C Refueling 3- Anto.aatic St sam. liven Repuso ll.liR)17ile INilRI.G-4 Othes IEmplain)
D Regulatoiy Restoiction 01611
- IM)pesatos Isaining & 1icense I:xamination
' 5 I Asinunisesative ,
G Openanimal I inus IExpl.nni lixinbit I - Same Somee j p8/1'li 11 Othes IEsplaini J
l l
a . .w .c , . .~ -..-. - . .- - .- . -
UNIT SHUTDOWNS AND POWER REDUCTIONS INSTRUCTIONS This report should desenbe 211 plant shutdowns during de m accordance with the taole appestmg on the report form.
report penod. In addiuon. it should be the source of explan. If category 4 must be used. supply brief comments.
anon of sigmficant dips :n average power levels. Each signi.
ficant reducnon in power level (yester than 20% reduction LICENSEE EVENT REPORT =. Reference the applicable m sverage daily power level for the preceding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) reportable occurrence pertsmmg to the outage or power should be noted. even though e umt may not have been reducton. Enter the erst four parts (event year. sequenusi shut down completelyl . For such reductions in power level. report numcer. occurrence ecde 2nd report type) of the Sve tne durst2on should be !isted as :ero. the method of reducuan part designation as descnbed in item 17 of Instruccons for should be listed as 4 (Other). 2nd the Cause and Correenve Preparanon of Data Entry Sheets for L:censee Event Report Action to Prevent Recurrence column should explcin. The (LER) File (NUREG.0161). This information may not be Cause and Correenve Acuan to Prevent Recurrence column immediately evident for all such shutdowns of course. since should be 2 sed to provide any rieeded explanation to fully further mvesugation may be required to ascertam whether ur describe the circumstances of the outsge or power reduction. not a reportable occurrence was involved.) If the outage or power reduction will not result in 2 reportable occurrence.
NUMBER. This column shculd indicate the sequential num. the posittve indication of thts lack of correistion should be ber assigned to each shutdown or sigruncant reductionin power noted as not applicable (N/A).
for that c:lendar year. When 2 shutdown or signiScant power SYSTEM CODE. The system in whica the outage or power reduction begins in one recort pened and ends m another. -
sn entry should be made for both report genods to be sure reducti n Ortsmated should be noted oy the two digit ecde or.
- 11 shutdowns or stamde:nt power reducuans are reported. ExMit G . Insanons for Prepar:non or Data Entry inuu Unt:1 a urut has sch'ieved its Erst power generstion, no num. f r Licensa Ennt Repan RER) Fde NREG@61L ber should be assigned to each entry. Systems that do not tit any existing code should be designa.
ted XX. The code ZZ should be used for tnose events where DATE. This column should indicate de date of the start a systert is not appticsole.
of each shutdown or ugmncant power reduenon. Report as yest. month. 2nd day. August 14.1977 would be report.d COMPONENT CODE. Select the most appropnate component as 770S!;. When a shutdown or ugnincant power reduction (ccm Exhstt i . Instruenons for Preparat:en of Data Entr) begmsin one report per:od sac ends m anoter, an entry should Sheets for Licensee Event Report (LER) File (NUREG.0161).
be made for both report penods to be sure all shutdowns usmg the followmg critiena:
or ugmncant power reduccons are reportes.
TYPE. Use "F" or "S" to indicate etter " Forced" or " Sche.
Juled." respectively. for each shutdown or signincant power S. If not a component fadure. use the related cornponent:
reducnon. Forced shutdowns include those required to be e.g., wrong valve operated through erron list valve as
- nstisted by no later than the weekend following discovery component.
of an off. normal condition. It is recognized that some judg.
ment is required in categonz:ng shutdowns in this way. In C. If a : ham of failures occurs the Hrst component to mai.
general. a forced shutdown is one that would not have been function should be listed. The sequence of events.includ.
completed in the absence of the condiuon for which corrective ing the other components wh:ch fail. should be descnbed acuan was taken. under the Cause and Correenve Acuan to Prevent Recur.
rence column.
DURATION. Se!f. explanatory. When a shutdown extends beyond de end of 2 report penod. count only the time to the Components that do not St any emstmg code should be de.
signated X CCCC(. The code 777777 should be used for l end of the report penod and pict up the ensumg down time in the following reeott penods. Report duranon of outages events where 2 component designation ts not spoiicsole.
rounded to the nearest tenth of an hour to facitate summanon.
The sum of the total cut 26e heurs plus tne hours the genera. CAUSE & CORRECTIVE ACTION TO PREVENT RECUR.
! RENCE. Use the column m a narranve fashion to ampiify or tor was on 'ine should equal the Jross hours in the reportmg 1 penod. explam the circumstances of the dutdown orpower recuenon.
The column should include the spec 2Sc cause for each shut.
l down or sigmdcant power reducnon and tne immediate anc REASON. Categortze by etter deugration m accordance with the table acecanny un the report form. If category H ontemolated tung term correenve acnon taken, if sppropn.
l must be used, suecay bnet eumments. ste. T*rus column should also be used for a desenption of the maior safety.related correenve maintenance performed dunna METHOD OF SHUTTING DOWN THE REACTOR OR de outage or pm moucnon inM.g m dennde:tbn
' REDUCING power. Categonze tw numner designauen 'O' # "'*I E* * " 'I *"d * " E " #',*"Y "" N' " N *** #' q r:diosenytty or im#e radtation exposure spectrie:dy cssue:.
INote that this difrers from the Ecison Electne Insatute sted with the out:ge which accounts for more tnan 10 :er.ent TEED dennitions of "Foreed Parual Outage" sne -Sene. di the 211owaaie unual values.
Juleu P:rtral Cut 2p." For these temu. hEl uses a hange at For :ong textual *eoorts continue carrattve on se:zr:re ;.soer
.0 MW as the break ;vmt. For targer power reacturs.30 MW and re:eren e tiie shutdown or power redu uun foi int,
, :s too imail a .har:ge tu wanarts evi:. nation. narrattve.
l Ni--
~* "*
. ~ . _ _ . .__ _
b.
. , Dockst No.: 50-316
- - Unit Namn D.C. Cook Unit 2 Completed By: D. A. Brucx }
Telephone: (616) 465-5901 Date: April 3, 1985 Page: 1 of 2 MONTHLY OPERATING ACTIVITIES - MARCH, 1985 HIGHLIGHTS:
The reporting period began and ended with the Unit in Mode 1 at 100% rated thermal power. One major power reduction occurred to repair a packing leak on feedwater regulating valve, 2-FRV-240.
Total electrical generation for the month was 815,840 MWH.
SUMMARY
3-05-85 At 0601, a power decrease tc 97% was started for C&I Surveillance Testing. Power reached 97% at 0707.
At 1345, a power increase to 100% was started, reaching 100% at 1430.
3-12-85 At 0603, a power decrease to 97% was started for C&I Surveillance Testing. Power reached 97% at 0633.
At 1420, a power increase to 100% was started, reaching 100% at 1457.
3-19-85 At 0605, a power decrease at 97% was started for C&I Surveillance Testing. Power reached 97% at 0643.
At 1615, a power increase to 100% was started, .-, aching 100% at 1720.
3-26-85 At 0607, a power decrease at 97% was started for C&I Surveillance Testing. Power reached 97% at 0700.
- AT 1730 a power increase to 100% was started, reaching 100% at 1859.
3-30-85 At 0915, a power decrease to 9% began to repair feedwater regulating valve, 2-FRV-240.
At 1852, a power increase to 100% began.
- - Docket No.: 50-316 Unit Nans: D.C. Cook Unit 2 Completed By: D. A. Bruck .
Telephone: (616) 465-5901 Date: April 3, 1985 Page: 2 of 2 3-31-85 At 0255, the power increase was stopped a 48% due to guadrant power tilt calculated at 1.037.
At 0355, because of a trailer fire inside the protected zone, an Unusal Event was declared.
At 0405, the fire was out and the Un'usal event terminated.
At 1015, the power increase resumed, reaching 100% at i 2134.
The control Room Cable Vault Halon System remains inoperable as of 1707 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.495135e-4 months <br /> on 4-14-83. The backup CO 2 System remain operable.
. . - _ - - _ _ _ . _ _ . , _ . _ _ _ , . ...m., ___.y_ _ _ , _ _ . - , _ , ___, ,,,
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DOCKET NO. 50 - 316_
UNIT NAME D. C. C ook - Unit No. 2 DATE 4-5-85 COMPLETED BY B. A. Svensson TELEPHONE (616) 465-5901 PAGE 1 of 1 IIAJOR SAFETY-RELATED MAINTENANCE MARCH, 1985 There are no significant safety-related maintenance items to report.
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- van IMDMMA &_MICMB_ALERCERLC COMPAN1 Donald C. Cook Nuciner Plant P.O. Son 458, Bridgman, Mohigan 49106 April 5, 1985 Director, Office Of Management Information and Program Control U. S. Nuclear Regulatory Commissicn Washington, D. C. 20555 Gentlemen:
Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 2
. Technical. Specification 6.9.1.6, the attached Monthly Operating
-Report for the Month of March, 1985 is submitted.
Sincerely,
(/W W. G.
V Smith, Jr.
Plant Manager WGS:ab Attachments cc: J. E. Dolan M. P. Alexich R. W. Jurgensen NRC_ Region III B. L. Jorgensen R. O. Bruggee R. C. Callen S. J. Mierzwa R. F. Kroeger B. H. Bennett P. D. Rennix J. H. Hennigan Z. Cordero J. J. Markowsky J. F. Stietzel PNSRC File INPO Records Center ANI Nuclear Engineering Department l' ,\
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