ML20128L768
| ML20128L768 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 01/31/1993 |
| From: | Julie Hughes, Woodlan D TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| TXX-93085, NUDOCS 9302190369 | |
| Download: ML20128L768 (5) | |
Text
F' U
'O A
log # TXX-93085 File # 10010.2 Ref. # 10CFR50.36
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TUELECTRIC February 15, 1993
% i!!!am J. Cahlil, Jr.
Gwsp t h e f'rrudent U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES) - UNIT 1 DOCKET NO. 50 445 MONTHLY OPERATING REPORT FOR JANUARY 1993 Gentlemen:
Attached is the Monthly Operating Report for January 1993 prepared and submitted pursuant to Technical Specification 6.9.1.5 contained in Appendix A to the Comanche Peak Ste,am Electric Station Unit 1 Operating License No. HPF-87.
Sincerely, William J. Cahill, Jr.
By:
D. R. Woodlan Docket Licensing Manager RC/rc Attachment c - Mr. J. L. Hilhoan, Region IV Hr. T. Reis, Region IV Resident inspectors, CPSES (2)
Mr. T.
A.
Bergman, NRR 220009 ggpit I
9302190369 930131
.m N. onve snect t n. 81 t w u.Te m 75 mt I
PDR ADOCK 0S000445 i
-R PDR.
c Mischmerit 1 t) TXX 93006
- Page 1 of 4 COMANCHE PEAK STEAM ELECTRIC STATION, UNIT 1 NRC MONTHLY OPERATING REPORT DOCKET NO:
60 4 -
UNIT: -
CPSES1 DATE:
Februar/11,1993 COMPWTED BY:
- Janet Hughos.
TE2 PHONE:
817407 4331 OPERATING STATUS 1.
Reporting Period: JANUARY 1993 Gross hours in reporting porlod:
2M~
2.
Currently authorized power level (MWI):'
Mil Man. depend. capacity (MWe Net): 1150
- Doston Electrical Rating (MWo. Net):
11.10 3.
Power level to which restricted (if any) (MWo Not):
NOME 4.
Reasons for restrictton (if any):
THIS MOMH -
YRTO DATE - CUMJt.ATIVE 5.
Number of hours reactor was critical MA MA 16,223 0L 0
2256.6 6.
Reactor reserve shutdown hours 8884 m
15.6474 7.
Hours generator on line 0
0.
0 8.
Unit reserve shutdown hours 1A 103-1.E.103 49245.930 9.
Gross thermal energy generated (MWH) 656A27
'050A27 16.291.592 L
10.
Gross electrical energy generated (MWH) 11.
Net electrical energy generated (MWH) 623,121 823,121 15A65A97 _
12.
Reactor Service factor 94.7 94.7 74.9 13.
Reactor availability factor 94.7 94 7
. 654 14 Unit service factor 92.6 92 6 73.2
- 15. Unit availability factor 92.6 92 6 73 2 72 2 72 &
a2.1.
- 16. Unit capacity factor (Usine MDC)
. 72 2 72 2 -
621 :
17.
Unit capacity factor (Using Design MWe) l 74 7#
7#
18.
Ur:lt forced outage rate 19 ; Shutdowns scheduled ovor next 6 months (Type. Date, and Duration of each);
20.
If shutdown at end of report period, estimated date of startup:
- 21. Units in test status (prior to commerclal operation):
ACHEVED Commercial Operation 900813 Estimated I
l f[
L
..:.- -. - - -.. 2.-- - -.. -. -
J
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. to TXX. 9xe5 Page 2 of 4 AVERAGE DAILY LNIT POWER LEVEL DOCKET NO:
' SO445 UNIT:
CPSGS 1 DATE:
February 11,1993 COMPLETED BY:
Janet Hughes TELEPFONE:
617+375331 MONTH: JANUARY 1993 DAY AVERAGE DAILYPOWER LEVEL CAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWo Net) 1 530 g7 1090 2
555 to 512 3
W 19 36-4 895 20 375 5
907 21 732 6
22 1071 7
909 23 12 8
12 24 513 9
1000 25 0
-10 1093 26 510 11 1091 27 930 12 1009 28 1074 13 1089 29 1066 14 1100 30 1000 15 1092 31 1095 16 BBS
+.
Attachment I to TXX 93086 Page 3 of 4
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NOi W4 UNIT:
CPSES1 j
OATE:
February 11.1993 CCMPLETED BY:
Janet Hughes - ___
TELEPHONE:
8174874331 I
i l
MONTH: JANUARY 1993
)
i 0141 0000 Unit started rnonth in MODE 1, continuing ascent to full power following second rofueling '
l outage.
01r18
-1144 Reactor tripped due to intermediate Range (IR) Hgh Flus inadvenently unblocked while i
performing surveillanco lost. Unit entered MODE 3. LER 93 001 to be submitted.
01/19 0745 Unit entered MODE 2, 0822 Reactor is crtical.
128 Unit entered MODE 1.
1317 Synchronized to the gnd.
01/24 1112 Reactor tripped duo to pressurizer pressure transtnitter spiked low causing ono -
' ovenemperature N16 channol to trip white another chantwlwas in trip 1of surveillanco tostingi l
- Untt entered MODE 3; LER 93 002 to be submitted.
01/25 0530 Unit entered MODE 2.
0608 Reactor is craical.
1636 Unit entered MODE 1.
l 1862 Synchronized to the grid.
01/31 2400 Unt inded rnonth in MODE 1.
1 l
( ':'
. -.. ~.,... _
..._..,n.._
...,.; m ;, a.- _
t Attachtnent 1 to TXX-4Trn Page 4 of 4 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKETNO-N UNIT:
CPSES1 DATE.
Fetuuary 11,1993 COMPLETEDBY:
M Hughes 1
m 817497 6 131 REPORT MONTH JANt;ARY 1993
)
wTHOooF TE SHUTTNGDOMe Ff0RCED DOHATE N TFEREACTOROR M1
.DATE SSCFEDULED N,
FEASO4 FEDUCNG POWEF1 CORRECTWEACTIOPGCOMMENTS l
1 930118 F
25 6 G
3 Interrnediale Range Q Fnsu Reactor trip
. I j
madvertenlly urtlocked at 100% RTP.
LER 93-00t to be submeted i
' 2 500124 F
29.7 A
3 Over Ter@erature N-16 Reactor trip due to pressurizer pressure transnailler +4 edlow.
LER 93-002 to be sutwnIIed.
1)-
FEASCN
- 2) N A EOUIPENTFAILUFE(EXPLAN)
E OPERATORTRANNG AND UCENSEEXAMNATION.
1: MANUAL i
B: MANTOR TEST '
P. ADWilSTRATWE 2-MANUALSCRAM
- C: FEFUE1JNG G-OPERATIONALERROR(EXPUWN) 3: AUTOMATICSCRAM D: ' FEGLAATORYFESTHCTION H: OTFER(EXPLMN) 4: OT)ER(EXPUnJN) 4 t
4 r
4
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