ML20128C524

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Monthly Operating Rept for June 1978 for Monticello Nuclear Generating Plant
ML20128C524
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 06/30/1978
From: Mayer L, Myrabo A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF ADMINISTRATION (ADM)
References
NUDOCS 9212040460
Download: ML20128C524 (6)


Text

_ _

POR NSlp NORTNERN 5TATES POWER COMPANY MIN N E A PO Li t. MIN N E S OTA 9940t 2.)

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July 11, 1978 Director, Of fice of Managetnent Information & Program Control ii c/o Distrib ation Services Branch, DDC. ADM U S Nuclear Regulatory Commission Washington, DC 20555 Dear Sirs IDHTICELLO NUCLEAR CENERATING PIANT Docket No. 50-263 License No. DPR-22 Monthly Operating Report June 1978 Attached are two copies of the Monthly Operating Report for June, 1978 for the Monticello Nuclear Generating Plant.

l Yours very truly, h.

N L 0 Mayer, PE

,;,r Manager of Nuclear Support Services

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LDM/ak cc Director, IE-111, USNRC (1)

Director, IE, USNRC (c/o DSB) (10)

MPCA Attnt J W Ferman 781950027 1

6 9212040460 780630 PDR ADOCK 05000263 y I{(

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NARRATIVE SlMARY OF OPERATING EXPERIENCE DOCKET NO.

50-263 LNIT hbnticello 00WLETED BY A. L. Myrabo IMili July 6, 1978 bbnth June 6/1/78 Power Operation.

6/2/78 Reactor scram. hbde switch inadvertently placed in shut-down after loss of motor control center due to trip of breaker at 55% power.

6/3/78 Scheduled outage to repair top works of relief valve and to feedwater heater leaks. Nm11: Reactor was in a shutdown 6/5/78 condition prior to the start of this outage.

i 6/5/78 Reactor scram. During startup, oscillating mechanical pressure regulator caused a reactor feedwater pump trip on reactor high water level.

Restart of RFP resulted in an IIN high flux scram.

6/6/78 to Power Operation.

6/8/78 6/18/78 Reactor scram. After power reduction to 55% for load following, oscillating mechanical pressure regulator caused an APRM high flux scram.

6/9/78 to Power operation.

l 6/13/78 6/ /78 Power reduced to 65% to repair condensate feedwater pump.

6/20/78 6/21/78 to Power operation.

6/30/78 NOTE: The Unit load - followed on 12 days during this period.

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OPERATING DATA REPORT DOCKET NO.

50-263 DATE 7-6-78.___

COMPLETED BY A. L. Myrabo TELEPHONE 612/290-5151 OPERATING STATUS INotes 1

1. Unit Name Montienllo 1

I

2. Reporting periods JUNE I

I

3. Licensed Thermal Power (MWt):

__l670 1

1 4

Nameplate Rating (Gross MWe):

_ _ __5 6 9 I

I S. Design Electrical Rating (Net MWe):

545.4 I

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6. Maximum Dependaole Capacity (Gross MWe): __564 I

I

7. Maximum Dependable Capacity (Net MWe):

536 l __ _

l 8

If Channes Occur in Capacity Ratings (Items Number 3 Through 1) Since Last Report, Give Reasons

__N/A 9

Power Level To Which Restricted, i f Any (Net MWe): ___N/A

10. Reasons For Restrictions, if Any

__N/A This Month Yr.-to-Date Cumulative

11. Hours in Reporting Period 720 4343 61368
12. Number Of Hours Reactor Was Critical

___646.5

___4196.1

__ 49364.5

13. Reactor Reserve Shutdown Hours 0.0 0.0 940.7
14. Hours Generator On-Line 630.9

___4150.7

__ 47928.1

15. Unit Reserve Shutdown Hours 0.0

__0.0

_0.0

16. Gross Thermal Energy Generated (MWH)

_ 858055

_ 6516521

_ 80171095

17. Gross Electrical Energy Generated (MWH) __286880

__2219320

__24592010

18. het Electrical Energv Generated (MWH)

__273100

__2133766

__23510140

19. Unit Service Factor

__ 87.6%

___ 95.6%

____ 78.1%

20. Unit Availability Factor

__ 87.6%

___ 95.6%

78.1%

21. Unit Capacity-Factor (Using MDC Net)

__ 70.8%

___ 91.7%

____ 71.5%

22. Unit Capacity Factor (Using DER Net)

__ 69.5%

___ 90.1%

____ 70.2%

23. Unit Forced Out991 Rate 5.9%

1.2%

_' 7.4%

24 Shutdowns Scheduled Over Next 12 Months (Type Date, and Duration of Each)

Refuelino Outage, October 16, 1978, 40 days ___

_ - =

25. If Shut Down At End Of Report Period. Estimated Date of Startups__N/A___
26. Units in Test Status (Prior to Commercial Operation): N/A Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCI AL OPERATION i

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

50-263-UNIT Monticello__

DATE 7-6-78_

COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 j

MONTH ___

JUNE DAY AVERACE DAILY FONER LEVEL DAY AVERAGE DAILY POWEH LEVEL (MWe-Net)

(MWe-Net) 1 530____

l7 337 2

35___

l8

_326__

3

-4_

19 321__

4

- 4 __ _ _

20 335___

5 124 21 408__

6

_405_

22 518______

1 495 _ __

23 533 8

1 4 2__ ___

24

_413___

9

___ _____424_______

25 447__

539__

10 533 26 11 441 27

_____535__

28 537_

12 542 13

___460___

29

__534_

30

_537___

14

___ _ ___296_______

15 309 31 l6

__327__

INSTRUCTIONS On this format. list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the neares t whole menawatt.

DOCKET NO.

50-263 UNITSHUTDOWNS AND POWER REDL*CTIONS UNIT N AME bbnticello DATE _ "' 6 - 7 A OMERD W A_f__ M60 f

REPORT MONTH Jtric TELEPHONE 617/7Q9-5191

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Act.on s..

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Date s

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Present Reicurrente 2E

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6-2-78 F.

19.5 G

2

- N/A ZZ ZZZZZZZ Moce switch inadvertently placed in shutdown.

5 6-2-78 S

49.7 B

4 N/A CC VALVEX Outage taken to repair 'D' relief valve top works and..xdwater heater

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leaks.

NOIE: Reactor was in shutdown mode prior to the start of this oute-

' age.

I 6

6-5-78 F

10.0 11 3

N/A CC INSTRU-C Oscillating mechanical pressure reg-ulator caused reactor feedwater ptmp trip. - Restart of ptaip resulted l in IRM high flux scrun.

I 3

4 F forceJ Reawn -

Method:

Eslutna G - Instrucisons 5 Schcotiled A-Equipmen Failure t E splaini

!41anaal for Preparati no of Data Batainienance of Test 2-Wnual Scrain.

Entr3 Sheets t'er Licemce C-Refueling 3 Autonutic Siram.

Esen Repost iLER) Fde iWREG-D-Rc;ufatory Resirs,; tion J Oshes t Esplaint O l e.I l 1 -Operaior Teaining & I atenw F unmiaison F-Admarmtrati.e 5

G-Operational Fir.is iF spla:.i Esh:t>is ! Sane S.nsrce s'8 ~~ l li-Ot he r i E splair.1 R

  • ' Reflects correction to yearly sequence ntspber.

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UNIT SliUTDOWNS AND POhER REDUCTIONS DOCKET NO.

'50-263 UNIT N AME Monticello DATE _ 7-6-78 t

COMPLETED BY A. L. Mrrabo 1

REPORT MONTH Jtme TELEPHONE 612/295/5151 F

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E jg j [55 Liu nsee

,E q, Cauw & Corre(seve

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4 Ei Event 3 'v1 E-3 Asinon su

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jgg Report :

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Presen Resurrente v:

6 7

6-8-78 F

10.0 H

3 N/A CC INSTRU-C Oscillating mechanical pressure reg-ulator caused high flux APRM scram at 55% power.

8 6-14-78 F.

O B

4.

N/A 01 PlNPXX-B Condensate feedwater pump high vibra-tion. Power mduction to 65% to repair.

2

+

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9.

6-24-78 S

0

-4

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N/A ZZ ZZZZZZZZ Pre-conditioning after rod adjust-ment.

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4 F F.irced Reaum:

Method Estuhn G - Instructions

< 5,heduled A.Eqaspment FailureiEsplain!

!-Man:ssi for Preparation of Data B-Maintenance of Test 2 Manual Scrain.

Entry Sheets s'er Liensee C.Refueline

.i. Autom iic Stram.

Esent Report I LE RI File (W REG.

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l D-Rc;ulaisir> Restristion 4 Othe: (Explaml Oleil l 1 Operator Trainin;1 Eisenw ITamination l

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G-Operational Eirus ti spf a:.0

' Esh:bn I ; Same S..urse i s ~~ l iI-Ot her i E splair. )

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