ML20127L320

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Ler:On 750713,during Normal Operation,Small Leak Developed in Reactor Pressure Gauge.Cause Unknown.Gauge Replaced.W/
ML20127L320
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 07/23/1975
From: Hill W, Mayer L
NORTHERN STATES POWER CO.
To: Anthony Giambusso
Office of Nuclear Reactor Regulation
References
LER-LER-750723, NUDOCS 9211230493
Download: ML20127L320 (2)


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NORTHERN 5TATKS POWER COMPANY MIN N E A POLIS. MIN N E SOTA SS40%

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July 23, 1975 Ifr A Giambusso, Director Division of Reactor Licensing

'.. 7 U S Nuclear Regulatory Commission Washington, DC 20555

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Dear lir Giambusso:

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lONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Inoperable Reactor Water Level Sensor The Licensee Event Report for this occurrence is reproduced on the back of this letter.

Yours very truly,

, ho L 0 }!ayer, PE lbnager of Nuclear Support Services LOM/MIV/ak y.

cc: J G Keppler G Charnoff i.'

1TCA Attn: J W Ferman h

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-over-9211230493 750723 PDR ADOCK 0507)O263 -

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LICENSEE EVENT REPORT CONTROL BLOCK-[ l l l l l

l (PLEA 8E PRINT ALL REQUIRED INFORMATION) g 1

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Q l dN lMl NlP lIl l 0l 0l-l 0 l Ol 0l 0l0 l-l 0l Ol l 4 l 1 l1l ll il l0l1l 7 89 14 15 25 26 3C 31 32 typI SYun$

CAsecour oo:sti Nuvot A EvtN1 DA f t HEpo4T Catt a CON 1 l P l 0 l

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[ 0l7 l1 l3 l7l Sl 10 l7l 21 31 715l 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCAiPTION

@l During normal operation a small leak developed in a Reactor Pressure Gauge. The l

7 89 80 El l 1eak Icucred the reference leg level for the_ scram and ECCS initiating Yarway l

7 89 80 El l Level instruments connected to the same process tap causing incorrect level l

7 89 80 DE l indication. Redundant Yarways were operable. No previous similar occurrences.

l 7 89 80 gl Pressure Gauge isolated.

(A0 50-263/75-12) l 89

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? 89 10 11 12 17 43 44 47 48 CAUSE DESCAIPTION DE I A leak developed in the sourdon Tube or neise Model cms 7646 0-1500 psig I

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@l pressure Gauge. Cause of leak unknown. Gauge to be replaced.

l 7 89 80 DE I I

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vtTH00 OF Status

% PCWEA 0' MEA STafv5 C'500vf AY OtSCOVERY DE SC AtP TtON J

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l Received Level Alarms l

7 8 9

10 12 13 44 45 46 80

'[cT v[v CONTENT AELE ASEC OF AELE ASE AMOUNT 05 Ac tivit y LOC AT!ON OF AEtt ASE 3

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7 8 9

10 11 44 45 80 PERSONNEL EXPOSUAES NuV0ER TYFE DE SC A)P fiON Q l 0l 0l Q ]

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7 89 11 12 13 80 PEASONNEL INJUAiES NuvsIA DE SC A4p T,0N E l 0 l 0l OI l NA l-7 89 11 12 Bo OFFSITE CONSEQUENCES Ql NA l

7 89 80 LOSS OR OAMAGE TO FACILITY Tvpf OtSC4PfON B] W l NA l

7 89 10 80 PUBUCITY

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7 89 80 ADDITION AL FACTORS

@l Occurrence also affected system IB l

7 89 80 bI l

7 89 80 NAME.

W J Hi,11 ps&c 612-295-5151

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