ML20127J235
| ML20127J235 | |
| Person / Time | |
|---|---|
| Site: | Monticello |
| Issue date: | 09/30/1974 |
| From: | Neils G, Shamla W NORTHERN STATES POWER CO. |
| To: | Chapman S US ATOMIC ENERGY COMMISSION (AEC) |
| References | |
| NUDOCS 9211190243 | |
| Download: ML20127J235 (4) | |
Text
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OE NSED NORTHERN STATES POWER COMPANY M IN N E A PO L.4 8. M I N N E s OTA 58401 October 7, 1974 i
Office of Plans & Schedules Directorate of Licensing U S Atomic Energy Comission Washington, DC 20545 Attention: Mr S C'tapman Gentlemen:
MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Monthly Operating Data September 1974 Atteched is the operating status information from the Monticello Nuclear Generating Plant for the month of September,1974 as req.icsted in the i
February 19, 1974 letter from Mr L Manning Muntzing. Changes proposed in the September 12, 1974 letter from Mr D F Knuth have been incorporated into this report.
Very truly yours, 1
G 11 Neils General Superintendent of g
l Nuclear Power Plant Operation l
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20f5' fbnticello Nuclear llNIT Generat iny, Plant j
DATl! ()gjtpher 4,.1974 C(YIPL).Tl:D liY y;n.ne A.Ada DAILY INIT POER OUTIUT i
FDNTil _Sep1 Caber 1974
-net AVERAGE il0W1Y We'"
DAY AVLPAGE 110URLY h!h'c DAY 1
336 25 432 432 26
._ 432 2
3 432 27 432 4
432 28 480 5
432 29 480 480 30
.432 6
432 31 7
432 8
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9 480 10 432 9
480 11 432 i
12 4
432 i
13 480 i
14 15 432 i
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16 480 432 17 480 18 432 19 432 20 480 21 432 432 23 480 24 F
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2026 RN-I UNIT NVIE AD.VTICill
.UCL13R GEhIPATINy1.BT j
IATli October 3, 1974 COMPLET13 BY W. A. Shamla T612T 29f,- 5 fM-lTx~t. 111~
OPERATING STATilS 1.
REPORTING PLRIOD:
0000740901 TO _ _240074930 GROSS IrURS IN IEPORTING PLRIOD:
720 2.
CURRINFLY AlD110RIZED P0h1R LIAT.I. h!Kt 1670 FMe-h1T 538 3.
POWER LINEL TO h11101 RESTRICTED (IF AhT):
None 4.
RFASONS FOR RESTRICTIONS (IF ANY):
4 TlilS Cth0LATIVE FDh~ll!
YR-TO-DATE 10 DATL J
5.
Il0liRS RFACTOR WAS CRITICAL 720
- 4,939 21,376 W
6.
REACTOR RESERVE Sl!LT110lG ll0URS 0
0 0
7.
Il0llRS CINERATOR ON-LINii 720 4,576_
20,423 8.
UNIT RESERVE SlflDIG.5 llCURS 0
0 0
9.
GROSS TilEIDL\\L IOllER ClIbiV.TEL (Phil) 989,894.4 6,310,514.4 30,821,755.4
- 10. GROSS FLECTRICAL P0hTR C15ERATED (>NI) 338,390 2,160,820 10,551,050
- 11. NET ELFCTRICAL 10hTR ClNFLiTID (?!hil) 325,046 2,061,778 10,079,576 75.4%
75.0%
12.
RFACTOR AVAllABILI1T FAciG (1) 100%
- 13. UNIT AVAILABII.I'lY FAcron (2) 100%
69.9%
71.6%
- 14. UNIT CAPACI'lY FACTCR (3) 83.9%
58.5%
65.7%
15.
FORCf.D OUTAGE RALE (4) 0.0%
2.92%
14.66%:
- 16. SillfrD0hNS SCHEDULED TO BEGIN IN NINT 6 MOVDIS (STATE TYPE, DATE, AND DURATION Ohi "rN fop tor Recirc Bypass Loop Inspection
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() ?fMW', FIbu O
$ six weeks duration IF SHlTrDOWN AT END OF Ih. PORT TIk1 D,/7' 'rlmTED DATE OF STARTUP:
N/A (2) Refuelin Outage 12 17.
- 100 (1) REACTOR AVAIIABILITY FACTOR = Il00RS RFACTOR WAS CRITICAL i1055 liOUits IK RLroR'iING HRT0ii
- 100 (2) UNIT AVAILABILITY FACTOR = liOURS GlEEPATOR ON-LIhTi CEU55'TGIRS IN RR0l'Ji1NG PlTUM (3) UNIT CAPACITY FACTCR = hTT Fl.LCTRICAl T0hT!R GENERATED
- 100 Fl"TfDDNSTRUEG55~TRRtNTEToRTING iTTGM
- 100 (4) FORCED Olfr3GE RATE = FORCED OLTTAGE liOURS liCIU5 GiMRXiG G-LINE + 1OEIii!_ECIXE HOUR 3 l
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- 1 LLL'u ~e TO: Mr. Steve Chapman UNIT NMIE GI21 RATING PIM
- StM.fARY Operated as base loaded DATE October 4, 1974.
unit. No outages.
REPORT FONIll September CONPLETED 11Y Wayne A Shamla USIT SIUTD0'.CiS TYPE ill'IIDD OF F-FORCED IURATION SlUITING FGO:
.NO.
DATE S-SCilllULED (IOURS)
REASON (1)
'IliL REACTOR (2)
COliEJS I
i (1) REASON:
(2) STTHOU A-EQUII"EJ FAILURE (EXPL1IN)
A-SLM* m B-Fl\\IN. OR TEST B-31MIil.
C-REFUELING SCRXi D-RECUL\\ TORY RESTRICTION C-AlfrG'AT E-CPERATOR TRAINING 6 SCR41 LICENSE EXXIIMTION F-MIINISTPATIVE G-OPERATIONAL ERROR (Explain)
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