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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
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PilILADELPillA ELECTRIC COMi%NY 10CPR50.90 NUCLliAR GROUP lillADQUARTliRS 955-65 CllliSTl!RilROOK llLVD.
WAYN!!, PA 19087-5691
"*" January 12, 1993 NucttAR $1:RVirl.S !)l fwl4 MENT DOchot Hon. 50-352 50-353 Licensu Noo. NPF-39 NPP-85 U.S. Nuclear Regulatory Commianlon ATTH: Document Control Desk washington, DC 20555
Subject:
Limerick Gonorating Station, Units 1 and 2 Technical Specifications Chango Roquest Incorporation of Changos Roquestod by the NRC Gentlemon:
Our lotter dated April 3, 1992, oubmittod -Technical Specifications (TS) Chango Roquest No. 90-20-0, That submittal requested that the TS Survoillanco Roquiremonto (SRs) for the Standby Liquid control (SLC) system be changed to: 1) uno the daily check of the SLC syatem pump suction piping temperature to verify system operability, rather than verifying heat tracing operability; 2) verify that the SLC oystem piping in not blocked by pumping the SLC system solution from the storage tank to a test drum, rather than to the test tank; and 3) requiro only ono SLC ntorage tank heater to be operabla for system operability, rather than the two heators that are currently required.
The NRC responded to our April 3, 1992 TS Change Roquest by lottor dated July 16, 1992, and requestod that we considor substituting the portinent sections of the SLC system requiromonto in the draf t improved Standard TS (STS) (i.e., NUREG-1433). As otated in tho. Ju)y 16, 1992 NRC letter, substitution of the portinent SRs specy fietl in-the draft improved STS would provido more flexibility wn.L mspect to verifying system operability since the STS requiromonto focus on the paramotorn important to safety, such as verifying that the temperature of the sodium pontaborate solution is above the point where it would precipitate out of solution, rather than-the various means of achieving this result.
l In kooping with this focus, the STS doen not contain SRs for the heat tracing or storage tank heators.
- e, <di 9a02aioi42 DR 930n2 AfQ ADOCK 05000352 I von y
i,
', / i
. j U.S. Nuclear Regulatory Commission Pago 2 Because of the clear benefits that would result from adopting the portinent STS SRs, we agrood to the NRC requestod substitution.
Accordingly, we re-evaluated the incorporation of the portinent STS :
SRs into our April 3, 1992 Chango Roquest, and datormined that our !
original conclusions with respect to the Significant- Ilazards Consideration of the proposed changes remained valid. .Thoroforo, thir; lotter submits the requested substitution of the portinent STS '
SLC system SRs to replace the proposed changes in our April 3, 1992 Chango Roquest.
. Information supporting our conclusion that substitution of the portinent STS SRs in place of our originally proposed changes is bounded by our original consideration of significant hazards is contained in Attachment 1 to this lettor. The proposod roplacement pages for the 14S, Unit 1 and Unit 2 TS are contained in Attachment ,
- 2. We request that, if approved, the Amendments bo issued by ;
February 5, 1993, and bo immediately offectivo, in order to take advantage of the . STS improvements during the second Unit 2 i refueling outage scheduled to begin on January 23,-1993. -The ability to use the STS SR' 1 r establishing and maintaining the SLC .
system operability will .. a substantial bonofit with respect to i the outage schedule.
If you have any questions or require additional information, please do not hositate to contact us.
Very truly.yours, ,
/ Gk G. Dock, Manager Licensing Section GJB:on Attachments cc T.T. Martin, Administrator, Region I, USNRC (w/ attachments)
T.J. Kenny, USNRC, Senior Resident Inspector, LGS (w/ attachments)
W.P. Dornolfo, Commonwealth of Pennsylvania (w/ attachments) liquid.ltr
.+ ,-
COMM0!iWEALTi{ OF PElitiSYLVAliIA I ss.
COUllTY OF CliESTER t D. R. 11elwig, being first duly sworn, deposos and sayst That he is Vice President of Philadelphia Electrio Company; the Applicant heroint that he has road the foregoing revised-Application for Amendments to Facility Operating Licenso lios.
IIPF-39 and fiPF-85 (Technical Specifications Change Roquest 11o.
90-20, Rovision 1) to change the Standby Liquid control system survoillance requirements, and knows the contents thoroof; and that tho statomonts and matters not forth thoroin are true and correct to the best of his knowledge, information and belief.
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-Vice Pros t Subscribed and sworn to beforo f mo this . }b- -
< - day of MIA . 1993.
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'I ATTACllMENT 1 LIMERICK GEllERATIllG STATION UNITS 1-AND'2 ;
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Docket Nos. 50-352 !
50-353 License Nos. NPF-39 i llPF-85 F
i REVISED TECIINICAL-SPECIFICATIONS CilANGE REQUEST- i No.-l90-20-0, Revision;1
" Revision of' Standby Liquid Control
.Surveillanco.Roquirements" Supporting Information for Chang 0s - 4-pagos '
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Attachment 1 pago 1 This revised Technical Specifications Chango Roquest substitutos the pertinent Standby Liquid control (SLC) system ;
Surveillanco Requirements (SRs) from the draf t improved Standard TS !
(STS) (i.e., NUREG-1433) in place of the changes proposed in our lotter dated April 3, 1992. This substitution was requested by the NRC in its lottor dated July 16, 1992. This substitution of the STS SRs results in the following proposed changes.
- 1) Allow the flexibility in the method (s) used to verify that the heat traced SLC system piping is unblocked rather than ,
specifying a test flow path. *
- 2) Doloto the requirement to maintain both of the SLC system storage tank heaters operable, since operability of tho 1 SLC system is based in part on the temporature of the sodium pontaborato solution in the SLC system storage tank rather than the method used to achiavo a particular temperaturo (i.e., verifying operability of the tank heaters). !
- 3) Clarificationc with respect to when and the period within ,
which certain SRs are to be performed.
A description of the proposed TS changes, and a discussion of applicability of the information supporting a finding of No Significant Hazardo Considoration and information supporting an t Environment Assessment provided in our April 3, 1992 Change Request to the revised proposed TS changes, are provided below.
We request that, if approved, the Amendments to the Limerick i Generating Station (LGS), Unit 1 and Unit 2 TS be issued by February 5, 1993, and bo immediately offectivo in order to support ,
the scheduled activities during the Unit 2 second refueling outage.
This refueling outage is scheduled to_begin on January 23, 1993.
Dgscription of the Proposed Changer 2 The following is a- description of the proposed. .changos, including identification of those proposed changes that have been revised to incorporate the pertinent STS SRs.
- 1) Change TS- SR 4.1.5.a.3 from requiring that the SLC system heat tracing circuit be demonstrated operable, to requiring that tho temperature of each SLC; pump suction
- i. piping be greater than or equal to 70*P.
- 2) Revise the original proposed change to add the following to the footnote for TS SR 4.1. 5.b. 2 : "within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after water or boron addition or solution temperature is i restored."
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Attachment 1 page 2
- 3) Reviso tho original proposed chango to TS SR 4.1.5.d.2 and associated footnote to require that all heat traced piping betwoon the SLC system storage tank and SLC system pump
( suction piping is veriflod to be unblocked, and that thi.
verification shall also bo performed whenover SLC system pump suction piping temperature drops below 70'F, within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after solution temperature is rantored.
- 4) Reviso the original proposed change to TS SR 4.1.5.d.3 to requiro that only the "A" storago tank heater bo demonstrated operable by deleting the requiremont to demonntrate that the SLC system storago tank hohtors are operablo.
b plncussion of Apolicability of Original Information GupnortiDG_a l'iDt11Ag_ of No SiG Dificant Hazards Consideration to ti l o Revised Proposed TS ChangCR The information supporting a finding of No Significant 11azards Consideration provided in our April 3, 1992 Chango Roquest was ovaluated with respect to the revised TS changos proposed hero.
The basis of our original conclusion that the proposed changes do not involve a Significant llazards considoration reflected the recognition that the verification of SLC system operability should focus on maintaining or recovering the required temperature of the sodium pontaborate solution, and not on the means of achieving the solution temperature required to provent precipitation. Sinco the-revised proposed changos are consistent with this focus, our original conclusion that the proposed changes do not involve a.
Significant flazards Consideration remains unchanged based on the information provided below.
- 1) The revised nronosed TS chancos do nn.t__involvo a sionificant increase in the probability or consecuences of v
an_ngcident nrg,iousiv ovaluated.
The revised proposed SR to verify that the SLC system pump suction lino is unblocked does not delineate a specific flow path.
The current TS SR specified flow path from the SLc system storago tank to the test tank croatos a largo amount of liquid wasto requiring special handling as a result of the pcst-test pipe flushing. An alternativo testing method would be to pump solution from the storage tank to a test drain. This would reduco the amount of piping and equipment subjected to the flow of the sodium pontaborate solution and the subsequent required flushing.
Accordingly, the result of performing the proposed SR would be equivalent to performing the current. SR; affected heat traced piping would continuo to be verified unblocked. The revised proposed SR dolotes'the prescribed method specified in tho current and originally proposed TS,_and thereby allows flexibility in the
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4 Attachment 1 Page 3 methods employed to perform this SR verification. The revised proposed SR also includes a clarification of the period during which this SR is required to be performed if the piping temperaturo drops below the low temperaturo limit (i.e., 70*F).
The revised pro?osed SR changes includo dolotion of the required demonstratnon of SLC system storage tank heater operability. This proposed chango is based upon the ultimate objective of datormining SLC system operability as a function of the temperature of the sodium pontaborato solution in the storage tank, which the TS will continue to require to be checked daily, and not on the method of achieving this verification.
Specifically, the storage tank heators are the "A" heator, a 10KW cycling heater (i.e. , controlling solution temperaturo betwoon 75* F and 85'F), and the "B" heater, a 40KW manually oporated heator used primarily during solution mixing activities. The storage tank is located within heated spaces of the Reactor Enclosure that are normally maintained at or above the "A" heator low temperature activation sotpoint of 75'F. Furthermoro, low storage tank solution temperaturo (i.e., 70'F) is alarmed in the Main Control Room.
In addition, the revised proposed SR includes clarification of the period within which the verification of solution concentration is required to be performed after water or boron is added to the storage tank, or .f the solution temperature drops bolow 70'F.
This clarification is based on the recognition of realistic tino limits to perform actions to preclude precipitation of the sodium pontaborato.
Based on the above discussion, our previous concluuion that the proposed changes do not involvo an increase in the probability or consequences of an accident previously evaluated remains unchanged.
2)- The= revised nronosed TS chances da not creato the possibility of a new or different kind of accident fr2m any accident nreviously evaluateh The revised proposed changes to the SLC system SRs do not add or doloto any equipment, and do not involve any systems or equipment that would creato an accident. Thorofore, our previous-conclusion that the proposed changes da not create the possibility of a new or different kind of accident from any accident previously evaluated remains unchanged.
- 3) The revised nronosed TS chances do not involve a sinnificant reduction in marain of safety.
The revised proposed changes to the SLC system SRs do not involve physical changes to the system, and continuo to provido an 1
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Attachmont 1 page 4 equivalent level of assurance that the SLC system will be capable of performing its safety function. Thorofore, our previous-conclusion that the proposed changes do not reduce the margin of safety remains unchanged.
Dj ecussion_ of Appligability of. original Information Supnpitino an EnvironmorttalAgngEment to the Revised _Fronosed TS_ Chanti qg our conclusion that an environmental assessment is not required for the changes proposed in our original Change Roquest dated April-3, 1992, remains unchanged with respect to the revised changes proposed here. The revised proposed changes do not involve a significant flazards Consideration as discussed in the preceding section. The revised proposed changes still do not involve a significant change in the types or significant increaso - in the amounts of any offluents- that may be reloaned offsite. In addition, the revised proposed changos still do not involve an increano in the individual or cumulative occupational radiation exposure. Thorofore, the revised proposed TS changes continue to conform to the critoria for " actions eligiblo for categorical exclusion" as specified in 10CFR51.22 (c) (9) .
Conclusion The Plant Operations Review Committoo and the Nuclear Review ,
Board have reviewed those revised proposed changes-to the LGS Unit i
- 1 and Unit 2 TS, and have concluded that they do not involve-an ;
unreviewed safety question, or a Significant flazards Considoration, and will not endanger the health and safety of the public. 1-1
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