ML20126F903

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Ack Receipt of 921218 Response to Violations Noted in Insp Repts 50-295/92-25 & 50-304/92-25 Re Assessment & Evaluation of EDG & Electrical Sys at Facilities
ML20126F903
Person / Time
Site: Zion  File:ZionSolutions icon.png
Issue date: 12/28/1992
From: Miller H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Reed C
COMMONWEALTH EDISON CO.
References
NUDOCS 9212310193
Download: ML20126F903 (2)


See also: IR 05000295/1992025

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DEC 2 81992

Do'cket No. 50-295

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Docket No. 50-304

Commonwealth Edison Company

ATTN:

Mr. Cordell Reed

Senior Vice President

Licensing Department-Suite 300

Opus West III

1400 Opus Place

Downers Grove, IL

60515

Dear Mr. Reed:

SUBJECT:

NOTICE OF VIOLATION (NRC INSPECTION REPORTS NO.

50-295/92025(DRS); 50-304/92025(DRS))

This will acknowledge receipt of your letter dated

December 18, 1992, in response to our letter dated November 20,

1992, transmitting a Notice of Violation associated with

Inspection Reports No. 50-295/92025(DRS) and No.

50-304/92025(DRS).

Thece reports summarized the results of the

assessment and evaluation of the emergency diesel generator and

electrical systems at your Zion Nuclear Power Station.

We have

reviewed your corrective actions and have no further questions at

this time.

These corrective actions will be examined during

future inspections.

Sincerely,

pr(rnai E H y! W " M '. Zns

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H. .J.

Miller, Director

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Division of Reacter Safety

See Attached Distribution

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Commonwealth Edison Company

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DEC 2 81932

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Distribution

cc:

M.

J.JWallace, Chief, Nuclear

Operating Officer

T.

Kovach, Nuclear Licensing

Manager

R. Tuetken, Site Vice

President

S.

Kaplan, Regulatory

Assurance Supervisor

T. Joyce, Station Manager

cc W/ltr dtd 12/18/92:

DCD/DCB (RIDS)

OC/LFDCB

Resident Inspectors-Byron,

Braidwood, Zion

R.

DeFayette, RIII

D.

Funk, RIII

Richard Hubbard

Mayor. City of Zion

J. W.

McCaffrey, Chief

Public Utilities Division

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C.

Shiraki, LPM, NRR

Robert Newmann, Office of Public

Counsel, State of Illinois

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Center

Robert M.

Thompson, Administrator

Wisconsin Division of Emergency

Government

State Liaison Officer

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'Crmm!nwealth Edistni

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December 18, l_992

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U.S. Nuclear Regulatory Commission

Washington, D. C,

20555

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Attn:

Document Control Desk

Subject:

Zion Nuclear Power Station Unit'I and 2

Response to Inspection Report 50-295(304)/92025

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NRC Docket Number 50-295 and 50-304

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Reference:

-H. J. Miller l'etter to Cordell-Reed' dated

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November 20, 1992, transmitting Inspection-Report

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50-295(304)/92025,-

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Enclosed is Commonwealth = Edison Company's-(CECO) response to:the. subject-

violation which was transmitted with the referenced letter.

The violation-concerns:the establishment of a'cceptance: criteria.-.the

evaluation of test results and-issuance of discrepancy reports when-

established acceptance criteria--is not met.

If there are'any' questions or comments regarding this. response, please-

contact Sara Reece-Koenig, Compliance Engineer, at 708/5.15-7250.

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Very truly yours,.

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T. J. Kovach

Nuclear Licensing _ Manager

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cc:$hE5ErMDavlsgRegionalAdministrator-Region:III

C..Shiraki. Project Manager. NRR-

J. Smith, Senior Resident Inspector, Zion

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REPLY TO NOTICE OF VIOLATION

NRC INSPECTION REPORT

295/92025; 304/92025

VIOLATION:

10 CFR 50, Appendix B, Criterion XI, requires that a test program be

established to assure that all testing required to demonstrate that

components will perform satisfactorily is identified and performed in

accordance with test procedures which incorporate the requirements and

acceptance limits contained in the applicable design drawings.

Test

results must be documented and evaluated to assure that test

requirements have been satisfied.

Contrary to the above, during the performance of the 18 month inspection

and maintenance activities conducted March through June 1992 on the

emergency diesel generators: (1) the licensee failed to perform an

adequate evaluation of generator winding insv'; tion resistance

measurements obtained on diesel generators lh and 18 that did not meet the

acceptance criteria; (2) the acceptance criteria for calibration of the

Megsense Card on the "0" EDG was not met and the licensee failed to

evaluate the discrepancy; (3) acceptance criteria were not specified for

the EDG rotor to stator air gap measurements o' " 9 phase to phase winding

insulation resistance data recorded by the cra;=

This is a Severity Level IV violation (Supplement I).

RM10LE)R THE VIOLATION

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Commonwealth Edison Company (CECO) acknowledges the violation.

The failure to perform an adequate evaluation of generator winding

insulation resistance on the iA and 1B Emergency Diesel Generators (EDGs)

and the failure to detect and resolve the Magsense card acceptance

criteria discrepancy were cue to the fact that both the lead worker and

the supervisor were not meticulous in their follow through in the

evaluation of test data and the submission of Discrepancy Renorts where

appropriate.

The lack of acceptance criteria in procedure P/E009-2N for the EDG rotor

to stator air gap measurement was due to the fact that acceptance criteria

was not provided for in the vendor manual for the EDG.

The measurements

were included in the procedure so that they would be available for review

by the cognizant electrical maintenance supervisor and Technical Staff

engineer.

A contributing cause to this lack of acceptance criteria in procedure

P/E009-2N is that the Zion Administrative Procedure (ZAP 110-01) governing

procedure content and format does not address requirements for considering

inclusion of acceptance criteria in Electrical Maintenance procedures.

ZNLD/2378/2

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REPLY TO NOTICE OF VIOLATION

NRC INSPECTION REPORT

295/92025; 304/92025

C0HECIIYLACIION TAKEN AND RESULTS ACHIEVED

The insulation resistance readings and calculations performed for the 1A

and IB EDG were evaluated and found acceptable by CECO's corporate Systems

Operational Analysis Department (SOAD).

The Magsense acceptance criteria was reviewed and a new acceptance

criteria has been developed by the Zion Diesel Group engineers.

Based on

their review it has been determined that the as-found/as-left reading of

2.198 Vdc is acceptable.

This criteria is located in procedure P/E009-2N

and will be updated during the revision of that procedure currently in

progress.

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To correct the lack of acceptance criteria for the air gap measurement

between the stator and the rotor, the Original Equipment Manufacturer

(OEM) was contacted and requested to provide an acceptance criteria for

the air gap dimension.

The OEM has provided ace ptance criteria which has

been reviewed and approved by SOAD.

The appropriate procedure changes

have been initiated.

On October 19, 1992 a meeting-was held between the Master Electrician and

all Electrical Maintenance supervisors.

This meeting reviewed in detail

the circumstances leading to the issuance of this violation and the

importance of acceptance criteria and the need to ensure proper evaluation

of test data and generation of Di~screpancy Reports when appropriate.

Each

supervisor was directed to review this violation with their Bargaining

Group Lead Electrician and to reinforce the standards for documenting test

results and understanding the importance of acceptance criteria.

CORRECTIVE ACTION TO BE TAKEN TO AVOID FURTHER VIOLATION

To ensure that all required acceptance criteria for the EDG inspection

procedure P/E009-2N have been identified and are based on current vendor

recommendations, IEEE Standards, and SOAD requirements, the procedure was

sent to SOAD for a technical review.

This review has been completed and

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procedure P/E009-2N is currently undergoing revision.

Zion Administrative Procedure (ZAP) 110-01 " Procedure Content ano Format"

will be changed to ensure that the inclusion of.necessary acceptance

criteria is considered whenever Electrical Maintenance department

procedures are rewritten or new Electrical Maintenance department

procedures are developed.

Zion Station will issue an Operating Experience Report on this violation

and corrective actions.

The report will emphasize the importance of

acceptance criteria and the need to be thorough in evaluation of test

data. The requirements for issuance of Discrepancy Reports will also be

addressed.

This report will be reviewed with the Zion Technical Staff and

all Zion Maintenance departments.

This report will be issued for review

by February 15, 1993.

ZNLD/2378/3

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REPLY TO NOTICE OF VIOLATION

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NRC INSPECTION REPORT

295/92025; 304/92025

DATE WHEN FULL COMPLI_ANCE WILL BE ACHIfyID

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The revision of procedure P/E009-2N will be completed by February 28, 1993.

The change to ZAP 110-01 will be completed by February 28, 1993.

Zion Station will be in full compliance by February 28, 1993,

ZNLD/2378/4

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