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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20126E7871976-03-29029 March 1976 RO 76-01:on 760317,during Operation,Water Accumulation Rate in Drywell Sump Began to Increase from Normal of 0.2 Gph. Caused by Leak Found in Cleanup Line Between Vessel & first-off Isolation Valve.Cleanup Line Replaced 1976-03-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20211J6651998-12-31031 December 1998 10CFR50.59 Annual Rept of Changes,Tests & Experiments for 980101-981231 for Humboldt Bay Power Plant,Unit 3 DCL-99-045, 1998 Annual Financial Rept for PG&E Corp. with1998-12-31031 December 1998 1998 Annual Financial Rept for PG&E Corp. with ML20151U1691998-08-28028 August 1998 Rev 2 to DSAR for Humboldt Bay Power Plant,Unit 3 ML20216C8821998-04-0808 April 1998 Safety Evaluation Supporting Amend 32 to License DPR-7 ML20203J6601998-02-28028 February 1998 Post-Shutdown Decommissioning Activities Rept for Humboldt Bay Power Plant,Unit 3 ML20195F4541997-12-31031 December 1997 10CFR50.59 Annual Rept of Changes,Tests & Experiments for Jan-Dec 1997 ML20217G5151997-12-31031 December 1997 1997 PG&E Corp Annual Rept HBL-97-013, Annual Rept of Changes,Tests & Experiments for Plant for Jan-Dec 1996,per 10CFR50.591997-12-19019 December 1997 Annual Rept of Changes,Tests & Experiments for Plant for Jan-Dec 1996,per 10CFR50.59 ML20205F5881997-07-24024 July 1997 Decommissioning Cost Estimate for Diablo Canyon Power Plant,Units 1 & 2 ML20205F5991997-04-12012 April 1997 Decommissioning Cost Estimate for Humboldt Bay Power Plant, Unit 3 DCL-97-045, Pacific Gas & Electric Co 1996 Annual Rept1996-12-31031 December 1996 Pacific Gas & Electric Co 1996 Annual Rept ML20129J4311996-10-18018 October 1996 Safety Evaluation Approving Corporate Restructuring & Establishment of Holding Company Under Temporary Name PG&E Parent Co.,Inc of Which PG&E Would Become Wholly Owned Subsidiary ML20058P6281993-08-31031 August 1993 Rev 6 to Pacific Gas & Electric Co Humboldt Bay Power Plant Unit 3 - Safstor QA Plan ML20141M0471991-12-31031 December 1991 Pge Annual Rept - 1991 ML20236E0581988-12-31031 December 1988 Pacific Gas & Electric Co Annual Rept 1988 ML20151G2361988-07-19019 July 1988 Safety Evaluation Supporting Amend 23 to License DPR-7 ML20151P6951988-04-30030 April 1988 Pacific Gas & Electric Co,Humboldt Bay Power Plant,Unit 3 Safstor QA Plan ML20196F3641988-01-31031 January 1988 Monthly Operating Rept for Jan 1988 ML20148Q3281987-12-31031 December 1987 PG&E 1987 Annual Rept HBL-87-086, Annual Rept of Design Changes,19861987-12-29029 December 1987 Annual Rept of Design Changes,1986 ML20237H7861987-07-31031 July 1987 Monthly Operating Rept for Jul 1987 ML20236G8241987-07-31031 July 1987 QA Plan for Humboldt Bay Power Plant Unit 3 - Safstor ML20237K8471987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML20235C9311987-06-23023 June 1987 Rept to ACRS Re Humboldt Bay Unit 3 - Core II ML20237K4221987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20210C5311987-04-30030 April 1987 SER Re Decommissioning of Facility ML20237K5311987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20211C5721987-02-11011 February 1987 Safety Evaluation Supporting Amend 22 to License DPR-7 ML20205C0891987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20204H4331986-12-31031 December 1986 PG&E Annual Rept for 1986 ML20212P8841986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 ML20211Q0541986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20211H3401986-10-31031 October 1986 PG&E Responses to Public Comments on Des for Decommissioning Humboldt Bay Unit 3 ML20212L8991986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20207F8221986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20207D6041986-08-31031 August 1986 Monthly Operating Rept for Aug 1986 ML20212N4921986-08-26026 August 1986 Safety Evaluation Supporting Amend 21 to License DPR-7 ML20215D4281986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20214L7861986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20206H1771986-06-16016 June 1986 Safety Evaluation Supporting Amend 20 to License DPR-7 ML20206C3131986-06-15015 June 1986 Comments on Des for Decommissioning Humboldt Bay Power Plant,Unit 3. Monetary Cost Estimates & Data on Contamination from Early Pool Leak Should Be Provided ML20205Q0061986-05-31031 May 1986 Rev 2 to Safstor QA Plan ML20205D6071986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20154Q0541986-03-31031 March 1986 Rev 1 to Safstor QA Program ML20197D1711986-02-28028 February 1986 Monthly Operating Rept for Feb 1986 ML20203E0151986-01-31031 January 1986 Monthly Operating Rept for Jan 1986 ML20210F2361985-12-31031 December 1985 Monthly Operating Rept for Dec 1985 ML20138C5521985-12-31031 December 1985 1985 Annual Rept ML20138L8501985-12-31031 December 1985 Rev 1 to Humboldt Bay Power Plant Unit 3 - Safstor QA Plan ML20137U3771985-11-30030 November 1985 Monthly Operating Rept for Nov 1985 1998-08-28
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e LICENSEE EVENT REPORT CONT ROL BLOCK I ll l l l l
' LIC E NS E EVENT LIC E NS E E TYPE TYPE NAME LICENSE NUMBER
- 10101-10101 010101-1010] l hllli 1111130 10111 ElCI9 A l HIM lB l it14 15 25 26 31 32 REPORT MEPORT REPORT DATE ,
CATEGORY TYPE SOURCE DOCKET NUMBER E VENT D ATE
- ECONTIP101 LTJ LL_J 10151 01-101113131 10131117 17161 1013121917101 60 61 68 69 74 75 80 7 8 57 58 59 E VENT DESCR6PflON O I On Feb.16, during normal operation, the rate of water accumulation 801 7 89 0 i in the drywell sump began to increase from a normal of 0.2 gph. The l
((ratereached11.8gphonMarch 17, 1976 when the Unit vss shut down *80 -
[f to investigate. Leak was found in clean-up line between vessel and i' first-off isolation valve. (f46 hNo, 7/o-O/)
VIOL ATION '
CODE CO E [Ilj O Ieili trJ l hOMPONE NT CODE 111P P$ IE 1Zl 19 6 R IX MANiACTJRER IXj 44 47 43 7 89 10 11 12 17 43 CAUSE DESCRIPTION )
[i@l IIA-Sect 3- of clean-up line was replaced in kind. During repair, onel Sch 40 pipe was discovered and replaced with required 8j yisectic 7 89 30 l
g GE I Sch 80. 80 y, 7 89 f ACILIT Y METHOD OF OTHE R ST AT US DISCOV E RY OfSCOVERY DESCRIPTION ST ATUS 8 LEJ
% PiWE R I lOld15I NA l [B._j iRoutine leak detection non- l 7 8 e 10 12 13 44 45 46 itoring60
,g,g, ACTIVIT Y CONTE NT
^ " '""'
g ""LJ' 1 Dry # 1 I EU"'i 10 E' c^"r%~c' EEM'"'":
11 44 45 80 7 8 9 PE RSONNE L E XPOSURES '
Q[U@l'0l $' i "dA'lfo"exposuresattributabletorelease) 80 l
7 8b 11 17 13 PE RSONNEL INJURSES EE DESCRIPTION 80 7 8 9 11 12 PF400 ADLE CONSE QUENCES 1
HI li A 80 7 89 t OSS OR D AM AGE TO F ACILITY Ot SC RIP TION
@T@YPE t Cmn2_1 circumferential crack in 2 inch line. Less of power cen. I 80 7 89 10 F i m i. ICIT Y
@L Ucvs release to local inedia 80 l
7 85 ADDitlON AL F ACTORS
@l 7 89 I!DT examination of re.aininn 2 inch clean-un line 80 1
gl showed proper thickness (all clean-up suction pipe is now Sci) 80) l
, 80
- - Walker T. Rapp 707 hb3-2787 PHONE.
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