ML20125A412

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Monthly Operating Rept of Subj Facility for Aug 78.(Encl to 7809150479
ML20125A412
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 09/05/1978
From: Myrabo A
NORTHERN STATES POWER CO.
To:
References
NUDOCS 7809150482
Download: ML20125A412 (4)


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NARRATIVE SIM RRY OF OPERATING EXPERIENCE l

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Docket No.

50-243 Unit Monticello 3-i Capleted by A. L. Myrabo t

Date Septenber 5,1978

!O mi August I

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8/01/78 Unitofflinefrom7/29/78shutdwn. Outage extended i

due to high reactor water conductivity.

e 8/01/78 to Pwer operation.

8/08/78 i

j.

8/09/78 Reactor scram. Oscillating mechanical pressure regulator resulted in APmt high flux scram.

8/10/78 l

to Pwer operation.

8/23/78 j

8/24/78 Reactor scram. LPRM pwer supply failure resulted in APRM high flux scram.

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l 8/25/78 l

to P wer operation.

8/31/78 i

l NJrE: The unit load-follwed on 7' days in this period.

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OPERATING DATA REPORT DOCKET NO.

50-263 i

DATE 9-5-78 COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 a

l OPERATING SI'ATUS INotes I

Monticello I

1. Unit Name :

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2. Reporting periods AUGUST I

1

3. Licensed Thermal Power (MWt):

__l670 t

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4. Nameplate Rating (Gross MWe):

569 1

1

5. Design Electrical Ratina (Net MWe):

b45.4 I

i 3

6. Maximum Dependable Capacity (Gross MMe): __564 1

1 2

7. Maximum Dependable Capacity (Net MWe) e _

536 1

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8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)_ Since Last i

Heport Give Reasonse __N/A

9. Power Level To Which Restricted, i f Any (Net MWe): __._N/A_

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10. Reasons For Restrictions. If Anys __N/A__

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This Month Yr.-to-Date Cumulative 744

_5831 62856

11. Hours In Reportina Period

-- 725.9 5587.9

.__ 50756.3 l

12. Number of Hours Reactor Was Critical l
13. Reactor Reserve Shutdown Hours 0.0 0.0 940.7 14 Hours Generator On-Line 709.2 5519.5

_ 49296.9 0.0 0.0 i

15. Unit Reserve Shutdown Hours 0.0 i
16. Gross Thermal Energy Generated (MWH)

-_1067938

_ 8578993-

_ 82233567 l

17. Gross Electrical Eneroy Generated (MWH) __359660

__2913670

__25286360

18. Net Electrical Energy Generated (MWH)

__341310

__2792406

__24168780

19. Unit Service Factor.

__ 95.3%

___ 94.7%

78.4%

20. Unit Availability Factor

__ 95.3%

___ 94.7%

____ 78.4%

21. Unit Capacity Factor (Using MDC Net)

__ 85.6%

___ 89.3%

71.7%

22. Unit Capacity Factor (Usino DER Net)

__ 84.1%

87.8%

70.5%

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23. Unit Forced Outage Rate 4.7%

3.0%

7.5%

24. Shutdowns Scheduled Over Next 12 Months (Type.-Date, and Duration of Each) i Refueling Outage -October 14, 1978. 40 Days _
25. If Shut-Down At End Of Report Period Estimated Date Of'Startups__N/A_
26. Units In Test Status (Prior to Commercial Operation): N/A Forecast Achieved INITIAL CRITICALITY i

'INIT!AL ELECTRICITY

= = - -

COMMERCIAL OPERATION

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AVERAGE DAILY UNIT P0nER LEVEL, i

5 DOCKET NO.

50-263-UNIT Monticello__

i DATE 9-5-78.___

1 CohPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 i

I

-t MONTH AUGUST f

DAY AVERAGE DAILY PonER LEVEL DAY AVERAGE DAILY PONER LEVEL (MWe-Net)

(MWe-Net) i 1

_, 34_

17-535____-

i 2

327 18 536 3

448 19 395=

l 4

_ 470 20 493 _

5 413 21 519 l

6 467__

22

--534 7

519__ _ _

23 5 3 7_,._

8 539 24

~362_

4 9

285 25 370__

l 10 342__

26 532 11 512 27 541 12

__531_

28 532__

13 430 29 441__

=

)

14 534_ ___

30 505_

i 15 527 31 475_

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__537 l-t INSTRUCTIONS

- Un this format, list the average daily unit power level in MWe-Net-for-each day in the reporting month.

Compute to the nearest whole mecawatt.

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50-263 DOCKET NO.

UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Mtmticello DATE kmt-5 1078 COMPLETED BY A_"L Mrrabo TELEPHONE 612/295-5151 REPORT MONTH Asimiet

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Cause & Corrective b.

Date 3

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g jg5 Event 5?

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Attain to

2. E E

j5g Repors =

AC y'

Psetem Recurrena 2-

'11 8-1-78 F

17.8 A

4 LER-78-14 RB VALVDP Continuation of 7-29-78 outage. Out-age extexled due to high reactor water conducitivty.

12 8-9-78 F

9.5 H

3 N/A CC INSTRU-C Oscillating mechanical pressure reg-ulator caused APRM high flur scraan.

-13 8-13-78 S

0-H 4

N/A ZZ ZZZZZZ. Imad following per system dispatcher.

14 8-19-78 S

0

-B 4-N/A ZZ ZZZZZZ Weekly surveillance and pican.iition-l

~

ing after rod adjustment.

15 8'24-78 F

7.5 A

3 N/A IA INSTRU-E APRM high flur scram caused by LPRM power styply failure. Power supply replaced.

I' 2

3 4

F Forced Reason:

Method:

Exlubs: C. Instructions S Scheduled A-Equipment Failure f Esplaint I-Manual for Preparai6.sn of Data B-Mainte:iance of Test 2-Manual Scram.

Entry Sheets for Lseensee C.Refuefing

.L Automatic Stram.

Event Report (LERI Fde tNUREG-D-Regulatory Resirsction 4-Other t Esplain)

Oltit i E-Operator Training & Lkenw rsamination F-Adnunistrative 5

Estubit I Same S.m se G-Operationat Eeror iFsp12:,0

(*8 ~7)

Il-Other t E splano