ML20117K237
| ML20117K237 | |
| Person / Time | |
|---|---|
| Site: | Braidwood |
| Issue date: | 05/24/1996 |
| From: | Stanley H COMMONWEALTH EDISON CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9606100219 | |
| Download: ML20117K237 (4) | |
Text
0)mmonwealth filimn Company tiraidwood Generating Station
, Route 81. Ilox Hi ligaceviHe, 11.60607 % 19
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Tri H l 5-158 2801 hiay 24,1996 United States Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Document Control Desk
Subject:
Progress Update for Braidwood Station Braidwood Nuclear Power Station Units 1 and 2 NRC Docket Nos. 50-456.50-457
Reference:
John C. Brons letter, to U.S. Nuclear Regulatory Commission, dated December 26,1995.
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in December 1995, Comed presented information to the NRC staff regarding performance i
goals for each of the Comed Nuclear Power Stations. During that meeting, Braidwood
. Station provided a list of goals on human performance and materiel condition issues to be completed prior to April 30,1996. This list is included in the referenced letter. Attached is summary of how Braidwood Station did in achieving these stated goals. A strong emphasis has been made at the Station to focus on equipment and employee performance, both of which are important factors in meeting the listed goals.
Overall, Braidwood Station realized many of the equipment performance goals. The Station has been challenged in meeting goals associated with human performance issues. As a result, this area is a major focus in the Improvement Initiatives being addressed by the Station.
If there are any questions or comments concerning this letter, please refer them to me at (815) 458-2801, extension 3600.
Respectfully, f
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- 1. G. tanley Site Vice President Braidwood Station 9606100219 960524 Enclosure PDR ADOCK 05000456 l'
P PDR cc:
J. hi. Taylor, Executive Director of Operations - NRR II. J. Niiller, Regional Administrator - Region til W. T. Russell, Director - NRR 1000%
A. B. Be ch, Deputy Regional Administrator - Region ill L. F. hiiller, Jr., Reactor Projects Branch Chief-Region til jj R. A. Capra, Director of Directorate 111 NRR yff/
R. R. Assa, Braidwood Project hianager - NRR l
C. J. Phillips, NRC Senior Resident Inspector - Braidwood F. Niziolek, Division of Engineering, Office of Nuclear Safety - IDNS l
A linicom Company K;/svp/96023, doc
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i SIGNIFICANT WORK ACTIONS TO BE REALIZED AS OF APRIL 30,1996 Hurnan Performance Continue Improvine Trend in Personnel Error LERs to < 2 hv Anril 30.1996. (1996 Goal-5)
There were 3 Personnel Error LERs.
l Continue Imorovine Trend in Consecuential Hurttan Errors to < I by Anril 30.1996.
l (1996 Goal-13) 4 Consequential Iluman Errors had occurred on or before April 30,1996.
i Continue Reducing OSHA Recordable Injuries to < 5 by Avril 30.1996. (1996-14)
There were 8 OSHA recordable injuries.
Extend Time Between Events to > 50 Days.
The average number of days between events occurring prior to May 1,1996, was 14 days.
Maintain Zero Significant Overdue Action Items.
The Station has been successful in maintaining zero significant overdue action items.
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Equipntent Performance Planned Maintenance Il'illNot Increase PRA by More Than a Factor ofil l
PRA factor average is 1.14. This figure represents the real risk profile for the year and relates to all l
equipment unavailability, including planned maintenance, and effects of events (such as the SAT trip).
Refurbished Condensate /Corulensate_ Booster Pumps ll'ill Be Operatine or Available l
95% ofthe Time.
The availability goals for the condensate / condensate booster pumps have not been met due to emergent discharge check valve problems.
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Disposition an Averaee of1 Operator IVorkaround Per Month.
An average of 3.25 operator workarounds have been dispositioned each month.
t Repair 80 Oil Leaks (209 Identified).
l 119 total grease / oil leaks have been fixed since December 1,1995.
I Reppir 100 Other Lianid Leaks (263 Identified. e.g.. Horated IVater. Pure IVater arul Cooline IVater).
410 total leaks were repaired for other liquid systems (245 boron leaks and 165 water leaks).
cthility to Operate VA Exhaust Fans in Each Plenum.
l One VA exhaust fan is available in each plenum.
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a SIGNIFICANT WORK ACTIONS STATUS AS OF APRIL 30,1996 Human Performance hnplentent Correctiveitetions Group Special Projects Group was established at the Station in January 1996. This group works with line management and provides resources for implementing corrective actions related to performance or process deficiencies identified through self assessments.
hnprove Utilization of the Problem Identifcation Systent The problem identification process was revised at Braidwood. The new process was imp %mented following a procedure revision (BwAP 1250-2, Revision 4). This procedure revision was approved on March 5,1996. Two of the new features include the following.
Provide timelv feedback to initiators ofPIFs One change made to the problem identification process is that timely feedback is provided to initiators of Problem Identification Forms (PIFs). Generally, feedback is given within five working days, Imorove trendine ofdata to provide more meaninefid information to line e
manaeers Data trending has improved. A Trend Analyst was appointed in September,1995 to identify potential trends. In addition, trends are assigned to Senior Managers for accountability and the status of trends are discussed weekly during Braidwood Leadership Meetings. There has been an increase in adverse trend identification (1994-16,1995-22, and 1996-11 as of April 30,1996).
Continue Contmunication ofthe Site Vision Through:
Reinforcement Sessions e
Reinforcement Sessions were held on January 12 and March 15,1996.
Plant Walkdowns Plant Walkdowns are done by Senior Managers each Wednesday.
Plantinformation Afeetines A plant inf;rmation meeting was held on March 13,1996.
RPAf Sessions Regular Planning Meetings (RPMs) are ongoing with supervisors.
Improve Develooment ofSite Personnel Produce Develonmentalplans for denartment headt e
0 Initial 1996 Personnel Performance Reviews (PPRs), including developmental sections, have been completed.
O Regular Planning Meetings (RPMs) are ongoing with supervisors.
O Individuals have attended an Office of Nuclear Business Leadership (ONBL)
Northwestern Leadership Program.
Fourteen individuals have completed the program.
Six people are scheduled to attend in the Fall 1996.
Approximately ten individuals are targeted to attend in 1997.
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SIGNIFICANT WORK ACTIONS STATUS AS OF APRIL 30,1996 l
Equipment Perfornmnce Work ControlImprovements Imniernent Work Week Manacers e
The work week manager process was implemented in December,1995.
i inspiernent OE/ Lead Unit Planner Usaye--hnorovement Initiatives e
Operations Unit Coordinators, previously referred to as Lead Unit Planners, were implemented in January 1996. This change improved the processes used by Operations personnel which allowed the OE's to focus more on big picture issues and less on day-to-day tasks.
Material Condition Improvements Renair 2B RU Seal e
Repair work on the 2B Ril seal was completed on February 3,1996.
Renlace OB WSSeals OB WS seals were replaced. This work ended on April 26,1996.
Cornolete U-1 Condensate / Condensate Booster Pumn Rehtrbishinents.
Refurbishments of the U-l condensate /cendensate booster pumps have been completed.
Rehtrhish 1 Aux. Buildine Exhaust Fan e
Work on the "B" fan is done. One fan is available in each plenum.
Renair Lianid System Leaks The following is a status of repaired liquid leaks.
O Boron leaks: 245 total repaired 0 Chemicalleaks: 45 total repaired 0 Grease / Oil leaks: 119 total repaiced 0 Water leaks: 165 total r: paired l
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