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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20117H6721996-04-25025 April 1996 NPDES Noncompliance Notification:On 960419 Discovered That Hydrazine Concentration in North Settling Basin Exceeded. Internal Outfall 602 & External Outfall 001 Closely Monitored for Hydrazine ML20064F9781994-03-0101 March 1994 NPDES Discharge Monitoring Rept Re Daily Ph Values Exceeding Maximum Daily Ph Limit of 9.0 Su Due to Unknown Causes. Monitor Ph Values Closely ML20058K0681993-11-24024 November 1993 NPDES Noncompliance Notification:On 931118,daily Outfall 001 Free Chlorine Sample Indicated 0.2 Mg/L Free Chlorine.Caused by Circulating Water Supplying to Much Chlorine.Mod to Plant Will Decrease Chlorine to Svc Water ML20045G3721993-06-18018 June 1993 NPDES Noncompliance Notification:On 930611,discovered That Outfall 601 Total Suspended Solids Value for Wk Exceeded Daily Limit Collected on 930609.Caused by Algae Bloom in Basin.Algae Population in Basin Will Be Monitored ML20141K5061986-01-14014 January 1986 NPDES Noncompliance Notification:On 851207,daily 2 H Discharge Limitation for Free Available Chlorine Exceeded at Outfall 001 ML20137B5221986-01-0404 January 1986 NPDES Noncompliance Notification:On 851209-26, Concentrations for Suspended Solids at Outfall 601 Found in Excess of 45 Mg/L Daily Limit.Caused by Algae die-off within Pond.Corrective Actions Not Stated ML20137Y0611985-11-26026 November 1985 NPDES Noncompliance Notification:Approx 815,000 Gallons of Solution Containing Water & Fluorescein Disodium Salt Will Be Discharged from Four Condensers Following Filling to Assist in Location of Cracks &/Or Leaks at Weld Points ML20133H5971985-08-0505 August 1985 NPDES Noncompliance Notification:Total Suspended Solids 30-day Weighted Average Discharge Concentration Limit Exceeded for Outfall 002 for Jul 1985.Consulting Firm Contracted to Determine Workable Solutions ML20133H1941985-07-29029 July 1985 NPDES Noncompliance Notification:On 850705 & 08,approx 120,000 Gallons Water/Ammonia Solution Discharged to Training Ctr Pond.Caused by Draining of Two Steam Generators.Release Data Encl ML20117G5291985-05-0303 May 1985 NPDES Noncompliance Notification:On 850430,total Suspended Solids 30-day Average Limit Exceeded at Outfall 002.Caused by Strong Westerly Winds & Heavy Rains.Collection Efficiency & Alternatives Being Assessed ML20100G2941985-03-28028 March 1985 NPDES Noncompliance Notification:On 850325,free Available Chlorine Daily Max Limit Exceeded at Outfall 1.Level of 3.0 Mg/L Caused by Improper Operation of Newly Installed Chlorination Valve.Valve Will Be Throttled ML20096B6801984-08-24024 August 1984 NPDES Noncompliance Notification:On 840820,total Suspended Solids Daily Max Limit Exceeded at Outfall 002.Caused by Higher than Normal Windspeeds & Rainfall Prior to Sampling Time.Suspended Solids Back within Daily Limit on 840823 ML20084S4781984-05-15015 May 1984 NPDES Noncompliance Notification:On 840514,daily Max Ph Exceeded at Outfall 002.Caused by West & Southwest Winds Kicking Up Solids from Pond Bottom.Carp Active in Disturbing Pond Bottom While Attempting to Spawn ML20082F6591983-11-17017 November 1983 NPDES Noncompliance Notification:On 831114 & 16,oil & Grease Limits Exceeded at Outfall 604.Caused by Surface Runoff During Heavy Rainfall & Melting Snow.Oil Absorbent Matl Placed within Outfall Areas 604 & 002 1996-04-25
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20205K8291998-12-31031 December 1998 Annual Exposure Rept for Davis-Besse Nuclear Power Station. with ML20206D2551998-12-31031 December 1998 Annual Radiological Environ Operating Rept for Davis-Besse Nuclear Power Station for 980101-981231 ML20206D2651998-12-31031 December 1998 Radiological Environ Monitoring Program (REMP) for Davis-Besse Nuclear Power Station for 980101-981231 ML20217M5381997-12-31031 December 1997 Annual Radiological Environ Operating Rept, W/Radiological Effluent Release Rept ML20236N4281997-12-31031 December 1997 Corrected Replacement Pages x,88 Through 90 & 108 Through 109 of Davis-Besse Nuclear Power Station 1997 Annual Radiological Environ Operating Rept, Including Radiological Effluent Release Rept ML20199G2991997-10-31031 October 1997 Oct 1997 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20198P4361997-09-30030 September 1997 Sept 1997 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20211E4571997-08-31031 August 1997 Telecommunicated Wastewater Rept for Aug 1997 ML20217N3381997-07-31031 July 1997 Jul 1997 Telecommunicated Hardcopy Wastewater Rept ML20149H1781997-06-30030 June 1997 June 1997 Telecommunicated Hardcopy Wastewater Rept ML20141F2851997-05-31031 May 1997 May 1997 Telecommunicated Hardcopy Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20138A9611997-03-31031 March 1997 Mar 1997 Telecommunicated Hardcopy Wastewater Rept for Davis-Besse Nuclear Power Station ML20137C3801997-02-28028 February 1997 Feb 1997 Telecommunicated Hardcopy Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20135C3171997-01-31031 January 1997 Jan 1997 Telecommunicated Hardcopy Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 ML20140D9411996-12-31031 December 1996 Annual Radiological Environ Operating Rept for Davis-Besse Nuclear Power Station for 960101-1231 ML20133P5251996-12-31031 December 1996 Dec 1996 Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 ML20136G0691996-12-31031 December 1996 1996 Annual Exposure Rept for Davis-Besse Nuclear Power Station ML20132F1891996-11-30030 November 1996 Nov 1996 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20134P0041996-10-31031 October 1996 Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 for Oct 1996 ML20129C2591996-09-30030 September 1996 Sept 1996 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20129F4781996-08-31031 August 1996 Aug 1996 Wastewater Rept for Davis-Besse Nuclear Power Station ML20129G8541996-07-31031 July 1996 Jul 1996 Telecommunicated Hardcopy Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20115F4071996-06-30030 June 1996 Wastewater Discharge Rept for Davis-Besse Nuclear Power Station for June 1996 ML20112J4741996-05-31031 May 1996 Wastewater Rept for May 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20112B9231996-04-30030 April 1996 Wastewater Rept for Apr 1996 for Dbnps,Unit 1 ML20117H6721996-04-25025 April 1996 NPDES Noncompliance Notification:On 960419 Discovered That Hydrazine Concentration in North Settling Basin Exceeded. Internal Outfall 602 & External Outfall 001 Closely Monitored for Hydrazine ML20107L1081996-03-31031 March 1996 Mar 1996 Wastewater Rept for Davis-Besse Nuclear Power Station ML20101B8281996-02-29029 February 1996 Feb 1996 Wastewater Rept ML20100G2251996-01-31031 January 1996 Wastewater Rept for DBNPS Unit 1 for Jan 1996 ML20108C6131995-12-31031 December 1995 Replacement Pages 128-137 of Davis-Besse Nuclear Power Station 1995 Annual Radiological Environ Operating Rept ML20107C3211995-12-31031 December 1995 1995 Radiological Environ Monitoring Program for Davis- Besse Nuclear Power Station, Final Monthly Progress Rept ML20107C2861995-12-31031 December 1995 1995 Annual Radiological Environ Operating Rept for Davis- Besse Nuclear Power Station ML20095E9431995-11-30030 November 1995 Nov 1995 Wastewater Rept for Davis Besse Nuclear Power Station Unit 1 ML20094J1791995-10-31031 October 1995 Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 for Oct 1995 ML20093H4001995-09-30030 September 1995 Wastewater Rept for Sept 1995 for Davis-Besse Nuclear Power Station,Unit 1 ML20098A3111995-08-31031 August 1995 Aug 1995 Wastewater Rept for Davis-Besse Nuclear Power Station ML20087G5701995-07-31031 July 1995 Wastewater Rept for Jul 1995 for Davis-Besse Nuclear Power Station,Unit 1 ML20086H2521995-06-30030 June 1995 Wastewater Rept for June 1995 for Davis-Besse Nuclear Power Station ML20085G3691995-05-31031 May 1995 Wastewater Rept for May 1995 for Davis-Besse Nuclear Power Plant ML20080H6321995-01-31031 January 1995 Wastewater Rept for Jan 1995 for Davis-Besse Nuclear Power Station,Unit 1 ML20077R5761994-12-31031 December 1994 Wastewater Rept for Dec 1994 for Davis-Besse Nuclear Power Station,Unit 1 ML20082V4051994-12-31031 December 1994 Annual Radiological Environ Operating Rept ML20078Q5201994-11-30030 November 1994 Wastewater Rept for Nov 1994 for Dbnps,Unit 1 ML20078D9961994-09-30030 September 1994 Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 for Sept 1994 ML20073B8471994-08-31031 August 1994 Aug 1994 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1 ML20072C4131994-07-31031 July 1994 Wastewater Rept for Jul 1994 for Davis-Besse Nuclear Power Station,Unit 1 ML20071H5591994-06-30030 June 1994 Wastewater Rept for June 1994 for Davis-Besse Nuclear Power Station Unit 1 ML20072S8321994-06-30030 June 1994 Radioactive Effluent Release Rept Jul 1993 - June 1994 ML20069N1711994-05-31031 May 1994 Wastewater Rept for Davis-Besse Nuclear Power Station Unit 1 for May 1994 ML20029E5001994-04-30030 April 1994 Apr 1994 Wastewater Rept for Davis-Besse Nuclear Power Station,Unit 1. W/940511 Ltr 1998-12-31
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'
o 0 TDLEDO ED 10N .
A Centerior Energy Company o AVENdE*
ToLEyr pHlo 43652-0001 l
April 25, 1996 Mr. Robert Plotts, Environmental Specialist Division of Water Pollution Control Ohio Environmental Protection Agency ,
Northwest District Office 347 North Dunbridge Road $O - 3L Q, l P. O. Box 466 w.,
Bowling Green, Ohio 43402-0466 ~ " " ' " =
Dear Mr. Plotts:
1
Subject:
Unauthorized Discharge for Ohio Environmental Protection Agency National Pollutant Discharge Elimination System Permit Number 2IB00011*ED This notification is being provided in accordance with Part III, Section 12(D) ,
of the Ohio Environmental Protection Agency (EPA) National Pollutant Discharge l Elimination System (NPDES) Permit Number 2IB00011*ED for the Davis-Besse ;
Nuclear Power Station. l On April 10, 1996, the station began draining water from the feedwater system, which contains hydrazine, an oxygen scavenger, to the facility's north settling i basin, Number 2 Basin (see Attachment 1). Approximately every 18 months, the i feedwater system, like the other station equipment, is drained for inspection and maintenance. 1 l
To prevent any discharge of hydrazine, the Outfall 602 pumps were.immediately l locked out. However, by April 14, 1996, the north settling basin was filled to '
capacity. On April 14 at approximately 1320 hours0.0153 days <br />0.367 hours <br />0.00218 weeks <br />5.0226e-4 months <br />, one of the butfall 602 pumps had to be turned on to prevent the basin from overflowing. The pumps remained on until April 16, 1996, at 1940 hours0.0225 days <br />0.539 hours <br />0.00321 weeks <br />7.3817e-4 months <br />. The hydrazine concentrations i during this discharge were previously reported to you in a letter submitted on !
April 18, 1996. j Due to the north settling basin again reaching capacity, the Outfall 602 pumps were turned on April 19, 1996, at 1053 hours0.0122 days <br />0.293 hours <br />0.00174 weeks <br />4.006665e-4 months <br /> to prevent the basin from overflowing. The hydrazine concentration in the basin at that time was 24.7 ug/L.
Following discovery of this exceedance on Friday, April 19, 1996, both the
, internal Outfall 602 and the external Outfall Op1 have been closely monitored for hydrazin'e. A list of these results is enclosed (see Attachment 2).
The remainder of the systems containing hydrazine are being drained to the middle settling basin, Number 1 Basin. This basin has been isolated to allow the hydrazine to dissipate prior to discharge.
9605290038 960425
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PDR s
ADOCK 05000346 enn g
.;80047 e g
i Page 2 This incident was first reported to your office on April 19, 1996, at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />. Then, at the request of Mr. Richard Zuzik of your office, a call was made to the Ohio EPA Emergency Response Center on April 19, 1996, at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, in accordance with Section 12(A) of our NPDES permit. This event was -
given Incident Identification Number 9604-62-1560. y.
Should you have any questions regarding this matter, please contact Mr. James L. Freels, Manager - Regulatory Affairs, at (419) 321-8466.
Sincerely yours, b
J hn K. Wood Plant Manager Davis-Besse Nuclear Power Station TKW/lkm Attachments 4
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i Davis-Bases Nuc. Powcr Station
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.. Evaporothre Loss io MGD Unit No.1
Meksua circulating Toledo Edison Co.
2s.7 MGD
' Water ino m Ottawa County ,,
system Oak Harbor, Ohio tsumnte ,
Intake Cnb
~ ' es '
Cooling Tower Make up Intake 48.5 MGD - c OMD O
O serweewater l
~
T tment
- ' k OW 0.22 MGD
[ ik7 MGD berles) )A f
m em 02: mD Lake Erie
.MGDQ .
NcL2
@-g \
Basing WaterTreatment I T g. _gy Keat Exchangers , 0.15MGD 0.07 MGD Make up r% e g No.1 e
' Primary'. '[i se a'ry' i ction ; d
+ M 0.08 MOD Outtan set
. . rC' . . J;i Wast 6. vater Stat 100 Basin f(
(( Effluent 0 os MGD 28.7 mod (Mt001)
,5 / es' -
(
(
em 0.005 MGD (
x> .
Padwaste Systems ( Navarre Marsh O j " (Poci No. 2) 2 m mpg 0.009 M GD m $ -
andsarmary 3 g -
' n S y -
4
'b$tlon Dha$i% 002 Navarre Marsh VN Sumps 4 O' I g 0.10 MGD Water 0.05 MGD (to Toussaint Rver) h Toussaint River
1 l
l - .+
- l. HYDRAZINE LEVELS (ug/L) l OUTFALL 602 OUTFALL 001 l
! DATE TIME CONCENTRATION CONCENTRATION L 4/14/96 1505 hrs. 63 NA 4/14/96 1800 hrs. 55 5.6 y "a ,
4/15/96 0140 hrs. 56 5.2 l 4/15/96 1020 hrs. 56 <5 4/15/96 1735 hrs. 65 5.2 4/16/96 0140 hrs. 61 5.6 4/1S/96 0840 hrs. 12 <S l 4/16/96 1310 hrs. 56 NA 4/16/96 1920 hrs. 45 8.1 4/16/96 1940 hrs. Pumps tumed off l *The above values were previously reported on 4/18/96*
l 4/19/96 1053 hrs. Pumps tumed on
- 4/19/96 1150 hrs. 24.7 NA l 4/19/96 2015 hrs. 26 NA 4/20/96 0440 hrs. 23 6.6 i 4/20/96 1000 hrs. 22 2.7 i 4/20/96 1115 hrs. Pumps tumed off 4/23/96 0955 hrs. 12 NA 4/23/96 1219 hrs. Pumps turned on
- 4/23/96 1415 hrs. NA <5 j 4/23/96 2005 hrs. 10 <5 4/24/96 0215 hrs. 11 <5
- 4/24/96 1005 hrs. 7 <5 4/24/96 1925 hrs. 10 <5 4/24/96 2255 hrs. Pumps tumed off I
l i
j '.
- i l Attachment 2 Page 1 of 1
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