ML20117G283
| ML20117G283 | |
| Person / Time | |
|---|---|
| Site: | Limerick |
| Issue date: | 08/26/1996 |
| From: | Boyce R PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML20117G286 | List: |
| References | |
| NUDOCS 9609050097 | |
| Download: ML20117G283 (1) | |
Text
'
1 Robert W.Boyc3 i
Plant Manager i
Limerick Generaung Station j
V PECO NUCLEAR ncO ene,gv c-v Limerick Generating Station A Unit of PECO Energy PO Box 2300 Sanatoga, PA 194644920 610 718 2000 10CFR50.73 i
August 26, 1996 l
Docket No. 50-352 j
License No. NPF-39 U.S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, DC 20555 l
SUBJECT:
- Licensee Event Reoort Limerick Generatino i*tation - Unit 1 This LER reports an automatic Unit 1 reactor scram, a i
Reactor Protection System (RPS) actuation, caused by high neutron flux following feedwater heater string isolations l
during a plant transient initiated by a main turbine j
electrohydraulic control system malfunction.
This LER also reports a non-compliance with the requirements of Facility
[
Operating License NPF-39, Condition 2.C.1 in that the Unit 1
(
maximum power level of 100 percent was exceeded by approximately 7.5 percent during the transient.
J
Reference:
Docket No. 50-352 f
Report Number:
1-96-016 Revision Number:
00 Event Date:
July 25, 1996 l
l Report Date:
August 26, 1996 f
Facility:
Limerick Generating Station P.O. Box 2300, Sanatoga, PA 19464-2300 l
This LER is being submitted pursuant to the requirements of 10CFR50.73 (a) (2) (iv), and License Condition 2.F, which requires & 30-day written followup report.
Very truly yours, j
I cc:
H. J. Miller, Administrator Region I, USNRC j
N.,S.
Perry, USNRC Senior Resident Inspector, LGS 4
9609050097 960826
"[h22 PDR ADOCK 05000352 S
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