ML20117D953

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Responds to NRC Re Violations Noted in Insp Repts 50-272/85-03 & 50-311/85-03.Corrective Actions:Operator Disciplined & Shift & Senior Shift Supervisors Reprimanded. Discussion of Violation Scheduled for Next Training Program
ML20117D953
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/29/1985
From: Corbin McNeil
Public Service Enterprise Group
To: Collins S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
NUDOCS 8505100275
Download: ML20117D953 (3)


Text

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9" OPSEG Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, NJ 08038 609 3394800 Corbin A. McNeHI Jr. Vice Presdent - Nuclear April 29, 1985 Regional Administrator, Region 1 U..S.

Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 Attention:

Samuel J. Collins, Chief Projects Branch No. 2 Division of Reactor Projects Gentlemen:

COMBINED INSPECTION 50-272/85-03 AND 50-311/85-03 SALEM GENERATING STATION UNIT NOS. 1 AND 2 DOCKET NOS. 50-272 AND 50-311 Public Service Electric and Gas Company is in receipt of your letter dated March 28, 1985, which transmitted a Notice of. Violation of a limiting condition for operation resulting from failure to follow procedures for conducting containment pressure relief operations.

Pursuant to the provisions of 10 CFR 2.201, our response to the Notice of Violation is provided in Attachment 1.

Sincerely, AkkMg Attachment PDR C

Mr. Donald C. Fischer Licensing Project Manager Mr. Thomas J.

Kenny Senior Resident Inspector The Energy People

4 e-ATTACHMENT 1 10 CFR PART 2.201 INFORMATION PUBLIC SERVICE ELECTRIC AND GAS COMPANY SALEM GENERATING STATION RESPONSE TO NOTICE OF VIOLATION Your letter of March 28, 1985, identified a violation of technical specifications 3.3.3.1 and 3.9.9 involving f ailure to follow an operating procedure for conducting containment pressure relief operations.

f On February 13, 1985, the containment iodine channel, IR12B, was j

made inoperable as a result of testing.

The plant vent iodine monitor isolation channel setpoint was not reduced, resulting in a loss of automatic purge and pressure / vacuum relief isolation capability.

During this period, each of the purge and pressure / vacuum relief penetrations providing direct access from the containment atmosphere to the outside atmosphere were not kept closed in that two containment venting operations were conducted.

I 1.

PSE&G DOES NOT DISPUTE THIS VIOLATION 2.

THE ROOT CAUSE OF THIS VIOLATION WAS PERSONNEL ERROR Specifically, the operator f ailed to follow the procedure.

Contributing to the event was the lack of adequate supervision by the shift supervisor concerning the inoperability of the IR12B monitor and its effect on plant operations.

3.

IMMEDIATE CORRECTIVE ACTION TAKEN AND RESULTS ACHIEVED On February 14, the day after the incident, the shift supervisor found that the procedure had been violated.

The violation was immediately reported to the NRC Resident Inspector and subsequently a Licensee Event Report was submitted.

The operator was disciplined and the shift supervisor and senior shift supervisor were reprimanded.

The operators were informed of the incident via the Operations Department Newsletter.

4.

LONG-TERM CORRECTIVE ACTION THAT WILL BE TAKEN TO AVOID FURTHER VIOLATIONS A discussion of this violation will be included in the next scheduled training program for individual station depa r tments.

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.A'lamacoid label has been affixed to the console on each unit.next to the pressure / vacuum relief-valve,pushbuttons to

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caution the operators that when the containment monitor is l

out~of service and the plant vent monitor is functioning in this capacity, the setpoints must be reduced to provide l

automatic purge and. pressure / vacuum relief isolation l

capability.

A review of this and another incident which occurred on May 28, _1984 has been performed.

The conclusion is that even though the same Limiting Condition for Operation (LCO) was violated, the root causes were not the same.

The first violation was caused by the inappropriate use of the procedure for implementing on-the-spot changes.

The second violation resulted from failure to follow the operating j

procedure for conducting containment pressure relief l

operations.

A review of the procedure was performed and no j

procedural inadequacies were found.

A review of the l

Corrective Action for the first violation has concluded that

[

the steps taken were adequate.

l Notwithstanding the above conclusions, we share the NRC's concern regarding the two violations of the same LCO.

The occurrence of repeat violations will receive particular management' attention during the next training cycle to assure that similar incidents do not recur.

Additionally, L

there have been other recent station occurrences indicating a lack of procedural compliance.

A plan of action to address this issue is being formulated.

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m

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